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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-019-02141 | | Well ID: 37-019-02141 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.791833, -79.840528 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | Municipality: [[Jefferson Township, | + | | State: Pennsylvania |
+ | |- | ||
+ | | County: [[Butler_County,_Pennsylvania|Butler]] | ||
+ | |- | ||
+ | | Municipality: [[Jefferson Township,_Butler_County,_Pennsylvania|Jefferson Township]] | ||
|- | |- | ||
| Operator Name: [[UNKNOWN OPR]] | | Operator Name: [[UNKNOWN OPR]] | ||
Line 13: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: KRETZER |
+ | |- | ||
+ | | License Status: Plugged and Abandoned | ||
|- | |- | ||
− | | | + | | Spud Date: |
|- | |- | ||
− | | | + | | Permit Date: |
|- | |- | ||
− | | | + | | Well Type: GAS |
|- | |- | ||
− | | Unconventional: | + | | Unconventional Well: N |
|- | |- | ||
| Configuration: Vertical Well | | Configuration: Vertical Well | ||
|- | |- | ||
− | | Well | + | | Conservation: No |
+ | |- | ||
+ | | Latitude: 40.791833 | ||
+ | |- | ||
+ | | Longitude: -79.840528 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Permits Issued Detail Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-05-20 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref><ref>{{cite web | ||
+ | | title = Spud Data Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-04-30 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-16 }}</ref><ref>{{cite web | ||
+ | | title = Oil and Gas Well Pad Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-05-20 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Date | ||
+ | !scope="col" | Event | ||
+ | |- | ||
+ | | 1901-01-01 | ||
+ | | Drilling Completion | ||
+ | |- | ||
+ | | 2004-03-04 | ||
+ | | Old Well | ||
+ | |- | ||
+ | | 2018-09-11 | ||
+ | | Begin Plugging | ||
+ | |- | ||
+ | | 2018-10-02 | ||
+ | | Finished Plugging | ||
+ | |- | ||
+ | | 2019-05-31 | ||
+ | | Fully Plugged | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources | ||
+ | | date = 2020-02-27 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-02-27 }}</ref> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Job Start Date | ||
+ | !scope="col" | Job End Date | ||
+ | !scope="col" | True Vertical Depth (ft) | ||
+ | !scope="col" | Total Water Volume (gal) | ||
+ | !scope="col" | Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Trade Name | ||
+ | !scope="col" | Supplier | ||
+ | !scope="col" | Purpose | ||
+ | !scope="col" | Ingredient Name | ||
+ | !scope="col" | CAS Number | ||
+ | !scope="col" | Additive Percentage by Mass | ||
+ | !scope="col" | Job Percentage by Mass | ||
+ | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Stimulation Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Stimulation Date | ||
+ | !scope="col" | Phase Number | ||
+ | !scope="col" | Chemical Agent | ||
+ | !scope="col" | Volume (gal) | ||
+ | !scope="col" | Treating Pressure (psi) | ||
+ | !scope="col" | Breakdown Pressure (psi) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Period | ||
+ | !scope="col" | Operator Name | ||
+ | !scope="col" | Gas Quantity (mcf) | ||
+ | !scope="col" | Gas Production Days | ||
+ | !scope="col" | Oil Quantity (bbl) | ||
+ | !scope="col" | Oil Production Days | ||
+ | !scope="col" | Water Quantity (bbl) | ||
+ | !scope="col" | Water Production Days | ||
|- | |- | ||
− | | | + | |}--> |
+ | |||
+ | <!--== Waste Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Period | ||
+ | !scope="col" | Operator | ||
+ | !scope="col" | Waste Type | ||
+ | !scope="col" | Quantity | ||
+ | !scope="col" | Disposal Method | ||
+ | !scope="col" | Waste Facility ID | ||
|- | |- | ||
− | | | + | |}--> |
+ | |||
+ | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Inspection ID | ||
+ | !scope="col" | Inspection Category | ||
+ | !scope="col" | Inspection Date | ||
+ | !scope="col" | Inspection Type | ||
+ | !scope="col" | Inspection Result | ||
+ | !scope="col" | Inspection Comments | ||
|- | |- | ||
− | | | + | | 2375997 |
+ | | Primary Facility | ||
+ | | 2015-04-21 | ||
+ | | Routine/Partial Inspection | ||
+ | | Outstanding Violations - No Viols Req'd | ||
+ | | | ||
+ | |- | ||
+ | | 2701978 | ||
+ | | Primary Facility | ||
+ | | 2018-03-06 | ||
+ | | Preoperation Inspection | ||
+ | | No Violations Noted | ||
+ | | Site visit with contractors for contract 17-3 prebid meeting. A gas odor was present between casing and production tubing. Bubbling can be heard in the well. | ||
+ | |- | ||
+ | | 2774602 | ||
+ | | Primary Facility | ||
+ | | 2018-09-13 | ||
+ | | Plugging(Includes Plugged/Mined Through) | ||
+ | | No Violations Noted | ||
+ | | Well is being plugged under contract OOGM 17-3R and is in a gas migration area. S&T Service and Supply (contractor) mobilized equipment on 9/10 and set up. On 9/11, they tried to take a reading of the well pressure but a 100# gauge was pegged. The well was blown down over several hours. On 9/12, they ran their downhole camera to a depth of 1575' (max for camera) and were still in 4". They said there are some noticeable holes in the 4". | ||
+ | Today they are running approximately 2056' of 1 1/2" in an attempt to find bottom. More 1 1/2" will be brought in as needed. | ||
+ | After the 4" is pulled and casing seat plug is set, we will run a down hole camera in to look for holes in the casing. | ||
+ | |- | ||
+ | | 2775629 | ||
+ | | Primary Facility | ||
+ | | 2018-09-17 | ||
+ | | Plugging(Includes Plugged/Mined Through) | ||
+ | | No Violations Noted | ||
+ | | Well being plugged under contract OOGM 17-3R. | ||
+ | The well continues to vent a high volume of gas. S&T (contractor) hauled in additional 1 1/2" tubing in an attempt to get to bottom. Pipe hit bottom at 2618'. S&T plans to set 30 sacks of cement at bottom, tag TOC, then pull 4". | ||
+ | |- | ||
+ | | 2776365 | ||
+ | | Primary Facility | ||
+ | | 2018-09-18 | ||
+ | | Plugging(Includes Plugged/Mined Through) | ||
+ | | No Violations Noted | ||
+ | | Bottom plug tagged around 2400'. Plugging string removed and 4" locating tool run to determine amount of 4" in hole. Approximately 1900' of 4" is in hole. S&T is setting cement up to 1900', then will shoot the 4" off. | ||
+ | |- | ||
+ | | 2779151 | ||
+ | | Primary Facility | ||
+ | | 2018-09-25 | ||
+ | | Plugging(Includes Plugged/Mined Through) | ||
+ | | No Violations Noted | ||
+ | | Well being plugged under contract OOGM 17-3R. | ||
+ | 1904' of 4" in well. 4" was shot at 1816 and would not budge. They shot again at 1663' and 4" was still stuck. A third shot at 1508' finally caused the 4" to break free. Approximately 600' still needs to be pulled. | ||
+ | |- | ||
+ | | 2780403 | ||
+ | | Primary Facility | ||
+ | | 2018-09-27 | ||
+ | | Plugging(Includes Plugged/Mined Through) | ||
+ | | No Violations Noted | ||
+ | | Well being plugged under contract OOGM 17-3R. | ||
+ | 1508' of 4" pulled. 30 sacks of cement inside and over where the 4" was shot. Plug tagged at 1291' yesterday. Casing seat plug tagged at 500' this morning. Well is being bailed out before topholing well. During bailing it was noticed that the water level is decreasing slowly, which would indicate a hole in the surface casing. | ||
+ | |- | ||
+ | | 2787319 | ||
+ | | Primary Facility | ||
+ | | 2018-10-11 | ||
+ | | Plugging(Includes Plugged/Mined Through) | ||
+ | | No Violations Noted | ||
+ | | Well has been plugged. Marker buried below ground surface. Site seeded and mulched. | ||
+ | |- | ||
+ | | 2793116 | ||
+ | | Primary Facility | ||
+ | | 2018-10-23 | ||
+ | | Administrative/File Review | ||
+ | | No Violations Noted | ||
+ | | Admin review on plugging certificate. | ||
|- | |- | ||
|} | |} | ||
− | == | + | <!--==== Violations Commited ==== |
− | {{ | + | {| class="wikitable sortable" width="95%" |
+ | !scope="col" | Inspection ID | ||
+ | !scope="col" | Violation ID | ||
+ | !scope="col" | Violation Date | ||
+ | !scope="col" | Date Resolved | ||
+ | !scope="col" | Violation Code | ||
+ | !scope="col" | Violation Type | ||
+ | !scope="col" | Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Penalties Applied ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Violation ID | ||
+ | !scope="col" | Penalty ID | ||
+ | !scope="col" | Penalty Code | ||
+ | !scope="col" | Penalty Status | ||
+ | !scope="col" | Penalty Date | ||
+ | !scope="col" | Enforcement Date | ||
+ | !scope="col" | Penalty Amount | ||
+ | !scope="col" | Amount Collected | ||
+ | |- | ||
+ | |}--> | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title =Oil and Gas Compliance Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-05-20 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | ==References== | ||
+ | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Pennsylvania Wells]] |
Well ID: 37-019-02141 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Butler | |
Municipality: Jefferson Township | |
Operator Name: UNKNOWN OPR | |
Well Pad ID: | |
Farm/Lease Name: KRETZER | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.791833 | |
Longitude: -79.840528 |
Date | Event |
---|---|
1901-01-01 | Drilling Completion |
2004-03-04 | Old Well |
2018-09-11 | Begin Plugging |
2018-10-02 | Finished Plugging |
2019-05-31 | Fully Plugged |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2375997 | Primary Facility | 2015-04-21 | Routine/Partial Inspection | Outstanding Violations - No Viols Req'd | |
2701978 | Primary Facility | 2018-03-06 | Preoperation Inspection | No Violations Noted | Site visit with contractors for contract 17-3 prebid meeting. A gas odor was present between casing and production tubing. Bubbling can be heard in the well. |
2774602 | Primary Facility | 2018-09-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Well is being plugged under contract OOGM 17-3R and is in a gas migration area. S&T Service and Supply (contractor) mobilized equipment on 9/10 and set up. On 9/11, they tried to take a reading of the well pressure but a 100# gauge was pegged. The well was blown down over several hours. On 9/12, they ran their downhole camera to a depth of 1575' (max for camera) and were still in 4". They said there are some noticeable holes in the 4".
Today they are running approximately 2056' of 1 1/2" in an attempt to find bottom. More 1 1/2" will be brought in as needed. After the 4" is pulled and casing seat plug is set, we will run a down hole camera in to look for holes in the casing. |
2775629 | Primary Facility | 2018-09-17 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Well being plugged under contract OOGM 17-3R.
The well continues to vent a high volume of gas. S&T (contractor) hauled in additional 1 1/2" tubing in an attempt to get to bottom. Pipe hit bottom at 2618'. S&T plans to set 30 sacks of cement at bottom, tag TOC, then pull 4". |
2776365 | Primary Facility | 2018-09-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Bottom plug tagged around 2400'. Plugging string removed and 4" locating tool run to determine amount of 4" in hole. Approximately 1900' of 4" is in hole. S&T is setting cement up to 1900', then will shoot the 4" off. |
2779151 | Primary Facility | 2018-09-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Well being plugged under contract OOGM 17-3R.
1904' of 4" in well. 4" was shot at 1816 and would not budge. They shot again at 1663' and 4" was still stuck. A third shot at 1508' finally caused the 4" to break free. Approximately 600' still needs to be pulled. |
2780403 | Primary Facility | 2018-09-27 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Well being plugged under contract OOGM 17-3R.
1508' of 4" pulled. 30 sacks of cement inside and over where the 4" was shot. Plug tagged at 1291' yesterday. Casing seat plug tagged at 500' this morning. Well is being bailed out before topholing well. During bailing it was noticed that the water level is decreasing slowly, which would indicate a hole in the surface casing. |
2787319 | Primary Facility | 2018-10-11 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Well has been plugged. Marker buried below ground surface. Site seeded and mulched. |
2793116 | Primary Facility | 2018-10-23 | Administrative/File Review | No Violations Noted | Admin review on plugging certificate. |
For data sources see[5]