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34-005-24186

Well Details

Well ID: 34-005-24186
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Country: United States
State: Ohio
County: Ashland
Municipality: Orange Township
Operator Name: MFC DRILLING INC
Well Pad ID:
Farm/Lease Name: ORANGE-ZACH UNIT
License Status: Producing
License Date: 2015-07-06
Spud Date: 2015-07-07
Spud Drilling Contractor: POULSON DRILLING
Final Drill Date: 2015-07-20
Well Total Depth: 4699.00 ft
Configuration: Vertical
Latitude: 40.970000
Longitude: -82.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2015-05-07 Proposed Formations:TREMPEALEAU B ZONE, Issued Date:5/7/2015, Expired Date:5/6/2017 12:00:00 PM, Drilling unit acres:180, Proposed Well Type:OG, Proposed Well Class:EDPW
APP 2015-07-06 Proposed Formations:TREMPEALEAU B ZONE, Issued Date:7/6/2015, Expired Date:7/5/2017 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2015-07-20
Completion Report Received 2015-09-24
Construction Permit Expires 2017-07-05
Record Last Modified 2017-10-23

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2016-06-20 ACID 0 1412 Gal 0 Producers Service Corporation The inspector was notified when the operator arrived on location to acidize the well. 500 gallons of acid was pumped through tubing and displaced with 912 gallons of water. The well was acidized following drill out of the sand and cement plug placed on bottom to facilitate casing repairs. The operator believes some of the cement made it to the formation. The well went on vaccuum following the job. No break was observed.

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2016 MFC DRILLING INC 969.00 0.00 350
2017 MFC DRILLING INC 148203.00 60.00 0
2018 MFC DRILLING INC 36367.00 793.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2016 MFC DRILLING INC Brine 1048 350
2017 MFC DRILLING INC Brine 783 0
2018 MFC DRILLING INC Brine 131 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-103538095 2016-4-7 0:00:0 PW No Violations 0.50
-1041410622 2016-6-7 0:00:0 DD No Violations 0.50
-1195047943 2016-1-8 0:00:0 PW No Violations 1.00
-1235676306 2016-6-16 0:00: DD No Violations 1.00
-1261943019 2015-7-12 0:00: DD No Violations 6.00
-1425928455 2015-8-14 0:00: DD No Violations 0.50
-1497744899 2016-5-20 0:00: DD No Violations 3.00
-160856966 2015-7-8 0:00:0 DD No Violations 3.00
-1814060663 2016-5-17 0:00: DD No Violations 1.00
-2032012790 2016-6-20 0:00: DD No Violations 2.00
-294105497 2015-7-29 0:00: DD No Violations 0.50
-30982409 2016-5-18 0:00: DD No Violations 0.50
-499141229 2016-5-10 0:00: DD No Violations 0.50
-559040714 2015-12-23 0:00 PW No Violations
-622809600 2015-7-14 0:00: DD No Violations 0.50
-707619327 2015-7-16 0:00: DD No Violations 0.50
-773593362 2016-9-19 0:00: DD No Violations 1.00
-8134973 2016-4-20 0:00: PW No Violations 0.50
-818252041 2016-4-22 0:00: PW No Violations 0.50
-881947381 2015-6-24 0:00: SC No Violations 1.00
-938148648 2016-5-9 0:00:0 DD No Violations 6.00
-955438266 2016-6-6 0:00:0 DD No Violations 1.00
-988039975 2015-7-9 0:00:0 DD No Violations 3.00
0008134973 2016-04-20 Production Wells No Violations The well remains all shut in with no gauges on the wellhead. No leakage observed. The operators service rig is in the county and was on the Shoup lease. It has not been brought to this location.
0009294602 2016-01-28 Administrative Inspection No Violations A conference call was conducted regarding gas pressure on the intermediate casing. Bob Worstall, Will Ziegler, Steve Opritza, Dave Claus and Tom Benko of ODNR participated. Current well status was discussed. Inspection of the well prior to the call revealed that the tubing and production casing are shut in. Gauges on the tubing and production casing indicated 900 psi and 400 psi respectively. A gauge on the flowline indicated 150 psi. The intermediate casing is valved to the line and is open to it. 50 psi was indicated on the outlet side of the heater treater. The operator indicated they are still testing the well and attempting to determine what course of action they will take. The well was not acidized. The 4.5 inch casing is cemented to 3850 feet. Deputy Chief Worstall requested daily pressure monitoring of the casing strings including surface casing. The operator stated they have no wellhead on the surface casing so monitoring that is not possible. The surface casing annulus was filled with cement when the intermediate string was cemented. The pumper was asked to submit daily pressures to the inspector. Jim Aslanides of MFC contacted the inspector and stated they would not do so. Mr. Aslanides requested Deputy Chief Worstalls phone number to contact him directly. MFC assured the inspector that they are keeping pressure on the 8 inch casing at a safe level. The welltender stated that the casing blows down to line pressure in a few minutes and that it has only pressured up to 350 to 400 pounds at most. Its not clear if gas is coming from the Clinton or Lime formations or if there is a leak in the 4.5 inch production casing. MFC is able to kill the well if necessary to reduce gas pressure on the intermediate casing. MFC is going to bring a service rig on the well by mid February to attempt to determine if they have a leak on the production casing and make repairs if necessary.
0030982409 2016-05-18 Drill / Deepen / Reopen No Violations The rig encountered a tight spot in the production casing when pulling the tubing from the well yesterday. The operator elected not to run a packer in the casing as a result. They are planning to run a wireline camera or pump a flag to attempt to locate the problems in the production casing.
0103538095 2016-04-07 Production Wells No Violations The well is all shut in and there are no gauges on the wellhead.
0160856966 2015-07-08 Drill / Deepen / Reopen No Violations The operator requested an inspection to witness surface casing cement. See the casing ticket for details.
0176953087 2016-03-01 Production Wells No Violations The pressure gauge has been removed from the tubing by the operator. 50 psi was indicated on the production casing gauge. All valves on the wellhead are shut in. The sales line pressure is approximately 50 psi.
0216503963 2016-06-15 Drill / Deepen / Reopen No Violations The rig is still drilling out the sand plug and cleaning out the hole.
0264577860 2015-12-11 Drill / Deepen / Reopen No Violations MFC is on site finish grading and resoiling the disturbed area. The well is shut in. Tanks and production equipment have not been installed yet.
0288815552 2016-06-10 Drill / Deepen / Reopen No Violations The production casing has been installed and the patch set. The casing was pressure tested to 1850 psi and held. The service rig drilled out a wireline bridge plug and 30 feet of cement. They are circulating the well and will drill out the sand and cement plug on Monday.
0294105497 2015-07-29 Drill / Deepen / Reopen No Violations All drilling equipment has been removed from the location. Water has been removed from the pits. MFC is moving equipment to the site to close pits.
0439876460 2016-05-19 Drill / Deepen / Reopen No Violations The rig crew is on location performing rig maintenance. They are not working on the well at this time. The operator has decided to run a camera in the well to inspect the production casing.
0499141229 2016-05-10 Drill / Deepen / Reopen No Violations The service rig is off the well location.
0499413508 2016-05-24 Drill / Deepen / Reopen No Violations The operator has pulled 1564 feet of the production casing out of the well. The threads on the bottom joint of pipe were dented in. The operator believes the casing wasnt tightened enough when the drilling rig installed it in the well. They also believe that the damage to the pipe was caused when tubing was pulled from the well. They will either be replacing the damaged joint or removing the collar from the casing still in the well and installing a casing patch.
0510368578 2016-06-14 Drill / Deepen / Reopen No Violations The rig is drilling out the sand and cement plug.
0559040714 2015-12-23 Production Wells No Violations Inspected well and met with operator on location as a result of an article in the Ashland Times-Gazette newspaper. The valve on the 8 inch intermediate casing was open and gas odor was observed. The Nankin Fire Department responded to a call at 10:40 am on December 22, 2015. The road was closed temporarily until the valve was closed and the site was released. No residences were evacuated during the event. The operator hired a pump truck to load the 4.5 inch production casing with 9 pound water and conduct tests on the well. Initially the 4.5 inch casing had 1750 psi; the well was loaded with 70 bbl of water, after 30 minutes the well was building pressure. An additional 25 bbl of water was loaded into the well and the well went onto a vacuum and had been killed. Upon arrival at 12:50 pm the well was on a vacuum for more than one hour. The location continued to be under control. The valve in question is normally maintained in the closed position. The well has not been put into production.
0622809600 2015-07-14 Drill / Deepen / Reopen No Violations Poulson Drilling is drilling on fluid at 2500 feet.
0707619327 2015-07-16 Drill / Deepen / Reopen No Violations Poulson Drilling is drilling on fluid at 3400 ft.
0773593362 2016-09-19 Drill / Deepen / Reopen No Violations ID has been posted at the tank. The operator has done some finish grading around the well. The well has been connected up to the flow line. The well is shut in.
0818252041 2016-04-22 Production Wells No Violations The well is all shut in and there are no gauges on the wellhead. Gas bubbles were observed coming from the slips on the 8 inch casing. Gas was bubbling through rain water accumulated on the wellhead. Photographs taken. MFC pumper Jeff Harmon disputed the fact that the wellhead is leaking.
0881947381 2015-06-24 Surface Facility Construction No Violations MFC personnel are on location stripping topsoil from the drill pad. They advised that the landowner reported them for trespassing and the sheriff was called. The original lessor passed away and his heirs are unhappy with the lease. MFC provided lease information to the county prosecutor to prove it was not a law enforcement matter. The sheriff stated that they will no longer be involved if further complaints are received.
0894465450 2015-07-30 Drill / Deepen / Reopen No Violations MFC is solidifying pits with lime and closing them. Water was removed from the pits prior to mixing in lime.
0938148648 2016-05-09 Drill / Deepen / Reopen Violations Noted The operator is on location with a service rig. Halliburton is also on location with a pump truck and bulk truck. Jim Aslanides of MFC stated they shot their drill bit off the tubing on Friday, 5/6/16. The bit became stuck when drilling out the formation packer to complete the well. A plug consisting of 25 sacks of sand was placed on bottom. The sand was followed by 40 sacks of Halliburton Halcem cement at 15.8 pounds per gallon, 1.18 cubic feet per sack. Halliburton states the plug is at 4482 feet. The operator intends to make repair to the production casing. MFC advised that they would be working on the well but they did not notify that they would be placing a sand and cement plug on bottom. Per Deputy Chief Worstall, this does not warrant a compliance notice.
0955438266 2016-06-06 Drill / Deepen / Reopen No Violations The operator replaced the defective joint of 4.5 inch casing. They attempted pressuring up the casing with water. The casing leaked during the test. The leak is at the same location as before. Appalachian Well Survey was re inspecting the casing with a camera. They believe the collar that was left in the hole may be bad also. They are going to attempt cutting the collar and installing a casing patch.
0988039975 2015-07-09 Drill / Deepen / Reopen No Violations The operator is drilling on air and fluid at 860 feet. The bit is stuck and circulation has been lost. Poulson Drilling is attempting to free the bit. MFC may decide to skid the rig. Followup in the afternoon revealed that the rig had been unable to free the bit. They are planning to shoot off the bit in the morning and attempt to recover it with an overshot tool.
1017041845 2016-04-18 Production Wells No Violations The well remains shut in. There are no pressure gauges on the well. No leakage observed.
1041410622 2016-06-07 Drill / Deepen / Reopen No Violations The service rig is running a casing cutter to cut the production casing below the bad spots in preparation to run a casing patch.
1072300850 2015-10-15 Drill / Deepen / Reopen No Violations The MFC service rig is on the well. They are drilling out cement and the formation packer to complete the well.
1148438781 2016-09-06 Drill / Deepen / Reopen No Violations The well remains shut in. The well has not been reconnected to production equipment or the sales line. The well is unidentified.
1195047943 2016-01-08 Production Wells No Violations The operator is boring sales line under County Road 620 to the east of State Route 58. The tank battery is being readied for production.
1206939018 2016-02-24 Production Wells No Violations The well continues to be completely shut in. Under 200 psi is showing on the 4.5 inch casing.
1235676306 2016-06-16 Drill / Deepen / Reopen No Violations The operator is swabbing the well. The well started to make gas and it was shut in. The rig operator believes the formation may have absorbed cement from the plug. They may have to run an acidization of the well to return it to production.
1261943019 2015-07-12 Drill / Deepen / Reopen No Violations The operator requested an inspection to witness intermediate casing cement. See the casing ticket for details.
1374898450 2015-06-29 Surface Facility Construction No Violations Heavy rain has the location muddy and partially under water. There is no work on building the surface location. Pits need to be dug and the location needs to be leveled before the rig can be brought on site.
1425928455 2015-08-14 Drill / Deepen / Reopen No Violations The operator is preparing to complete the well. A load of tubing has been delivered to the location. The service rig is not yet on site.
1436795876 2015-07-10 Drill / Deepen / Reopen No Violations Poulson Drilling shot the drill bit off in the well. They rigged up an overshot tool consisting of 8.625 inch casing and washed over the bit with heavy drill mud. No obstruction was encountered at the red rock. The bit was trapped by cuttings from an improperly conditioned hole caused by aerating the drilling fluid. They were able to hook onto the bit with drill pipe following cleanout of the hole.
1437484549 2015-07-20 Drill / Deepen / Reopen No Violations The operator requested an inspection to witness cementing the 4.5 inch production casing. The casing was ran in on a formation packer. The packer is set at 4677 feet. 2 cement baskets were installed above the packer at 90 feet and 172 feet from the packer. See the cement ticket.
1438694545 2015-08-03 Drill / Deepen / Reopen No Violations The pits have been closed and the location is rough graded. The location needs to be finish graded and topsoiled.
1450469831 2015-12-18 Preliminary Restoration No Violations MFC has completed finish grading of the disturbed area. The area is stable. The location is farm field and the farmer will be planting crops in the next growing season. MFC needs to pick up the dozer from the location. Production equipment has not been installed yet. The well is shut in. Preliminary restoration is approved.
1452284926 2016-01-04 Drill / Deepen / Reopen No Violations The well is shut in at all valves. A gauge on the tubing indicates 1700 psi, the 4.5 inch casing is indicating 500 psi and the 8 inch casing is indicating 0 psi. There is no leakage at this time.
1455727536 2016-02-16 Drill / Deepen / Reopen No Violations The pressure gauge on the production casing indicates 350 psi. No pressure was indicated on the tubing. The intermediate casing string is shut in and there is no pressure gauge on it.
1457531363 2016-03-07 Production Wells No Violations All gauges have been removed from the well by the operator. The well remains shut in at all valves.
1458052797 2016-03-14 Production Wells No Violations The well is shut in at all valves. There are no gauges on the well head.
1460395003 2016-04-11 Production Wells No Violations The well remains all shut in. There are no gauges at the well. Gas bubbles were observed coming from the wellhead on the intermediate casing. Ted Hershey of MFC was contacted to check the well. He did not arrive while the inspector was on location. Jim Aslanides of MFC Drilling stated in a phone conversation on 4/12/16 that the intermediate casing only pressures to a maximum of 20 to 25 psi and they are blowing it down every other day. He also stated the tubing and production casing have no pressure on them and the trempealeau formation is killed. They are coordinating with Halliburton to come and service the well. He does not have a timetable at this time.
1461596814 2016-04-25 Production Wells No Violations The well remains all shut in. There are no gauges on the wellhead.
1463510184 2016-05-16 Drill / Deepen / Reopen No Violations The well is shut in. A gauge on the tubing indicates no pressure. No personnel on site.
1465833417 2016-05-31 Drill / Deepen / Reopen No Violations The operator is running in the 4.5 inch casing with a replacement joint of pipe in place of the one with defective threads.
1497744899 2016-05-20 Drill / Deepen / Reopen No Violations Appalachian Well Survey ran a wireline camera to inspect the production casing. They were unable to get the camera past an obstruction at 1600 feet. There was some type of anomaly observed between 1500 and 1600 feet but they were not able to determine if there is damage to the casing pipe at that depth or if some other obstruction such as cement is at that depth. They are speculating that it may be a hole but they need to do further analysis before proceeding with a repair. The well is killed and there is a sand and cement plug on bottom. There is no gas leakage from the Trempealeau formation. The operator ran 2 year old used pipe in the well and provided information that it was tested and drifted. They believe the casing may have been damaged by handling or when it was installed in the well. The pipe was not observed when it was ran in the well.
1546294092 2017-08-08 Production Wells No Violations The well is equipped with tubing, production casing and intermediate casing and is in production. The production casing is shut in. Valves on the tubing and intermediate casing flow lines are open. There is a production unit on location. There is a 100 barrel tank in the tank battery. ID is posted at the tank.
1603562148 2015-06-23 Surface Facility Construction No Violations An excavator and dozer are on location. No personnel on site. Work has not started.
1759907266 2016-09-26 Preliminary Restoration No Violations All of the drilling equipment has been removed. The location is graded and the lease road has been surfaced with limestone. The preliminary restoration is approved.
176953087 2016-3-1 0:00:0 PW No Violations 0.50
1814060663 2016-05-17 Drill / Deepen / Reopen No Violations The service rig is on the well. The rig operator states they are pulling tubing to install a packer in the production casing. The packer will be installed at the depth of the top of cement on the backside of the 4.5 inch casing. The plan is to pump water through the tubing below the packer to pressurize the 4.5 inch in order to locate the hole. The rig will pull the packer up and repeat testing until the hole is located by loss of pressure. The well has been sealed by the bottom plug placed by Halliburton. No gas pressure was on the intermediate-production annulus when the rig crew checked it.
1889388751 2016-03-21 Production Wells No Violations The well remains shut in. There are no gauges at the well.
2017746715 2016-06-08 Drill / Deepen / Reopen No Violations The service rig cut and removed the 4.5 inch production casing. The joint above the cut was found to be cracked at the thread end and had a cracked collar. The rig crew was preparing a casing patch to install on the casing string.
2032012790 2016-06-20 Drill / Deepen / Reopen No Violations The operator requested an inspection to witness acidizing the well. The job was partially witnessed because notification was received when the crew arrived on location for the job.
216503963 2016-6-15 0:00: DD No Violations 1.50
264577860 2015-12-11 0:00 DD No Violations 1.00
288815552 2016-6-10 0:00: DD No Violations 2.00
439876460 2016-5-19 0:00: DD No Violations 0.50
499413508 2016-5-24 0:00: DD No Violations 4.00
510368578 2016-6-14 0:00: DD No Violations 1.00
894465450 2015-7-30 0:00: DD No Violations 3.00
9294602 2016-1-28 0:00: AM No Violations 4.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0938148648 US-OH-130734 2016-07-26 NONE(S) Failure to notify inspector; failure to submit cement tickets

For data sources see[8]

References