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| Well ID: 34-029-21683 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Columbiana | |
| Municipality: Butler Township | |
| Operator Name: VANGUARD OIL & GAS LLC | |
| Well Pad ID: | |
| Farm/Lease Name: KIKO-BERGER UNIT # 1 | |
| License Status: Final Restoration | |
| License Date: 2008-10-03 | |
| Spud Date: 2008-10-15 | |
| Spud Drilling Contractor: | |
| Final Drill Date: | |
| Well Total Depth: 781.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.840000 | |
| Longitude: -80.950000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2008-10-03 | 6970 VANGUARD OIL & GAS LLC Proposed Formation CLINTON Issued Date 10/3/2008 Expired Date 10/3/2009 6:00:00 AM |
| Plugged/Abandoned | 2008-10-17 | LOST HOLE |
| Construction Permit Expires | 2009-10-03 | LOST HOLE |
| Record Last Modified | 2013-07-01 | LOST HOLE |
For data sources see[2]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1513901531 | 2013-6-21 0:00: | FR | No Violations | |
| -1969533326 | 2008-10-17 0:00 | PB | No Violations | |
| -527266483 | 2008-10-16 0:00 | DD | No Violations | 2.00 |
| 0527266483 | 2008-10-16 | Drill / Deepen / Reopen | No Violations | Inspection revealed that G&H Drilling is still having trouble getting the casing out of the hole. Appalachian Well Services arrived on site and shot holes in the bottom joint of the surface casing in an attempt to break circulation. This didnt work to break circulation so they kept trying to work the casing up and down . I advised that I was going to be out of town this weekend so if they needed an inspector for plugging the well or running surface casing to contact Inspector Claus. |
| 0860676978 | 2008-10-14 | Drill / Deepen / Reopen | No Violations | Inspection revealed that G&H Drilling is at 475 . No violations at this time. |
| 1513901531 | 2013-06-21 | Final Restoration | No Violations | No indication of well equipment, access road or tank battery. |
| 1626390174 | 2008-10-15 | Drill / Deepen / Reopen | No Violations | |
| 1969533326 | 2008-10-17 | Plug / Plug Back | No Violations | The surface hole was lost. 40 of 11-3/4 dia conductor casing and 511 of 8-5/8 dia surface casing was left in the hole. Cement plugs were set from 781 - 581 and from 200 - 0. On 10-18-2008, the surface plug had fallen to 24. Russell Miller topped off the hole with 40 sacks of sackrete. The drilling rig was skidded 20 to the north and a new well was spudded. |
| 860676978 | 2008-10-14 0:00 | DD | No Violations | 1.00 |
For data sources see[3]