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34-029-21683

Well Details

Well ID: 34-029-21683
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Country: United States
State: Ohio
County: Columbiana
Municipality: Butler Township
Operator Name: VANGUARD OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: KIKO-BERGER UNIT # 1
License Status: Final Restoration
License Date: 2008-10-03
Spud Date: 2008-10-15
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 781.00 ft
Configuration: Vertical
Latitude: 40.840000
Longitude: -80.950000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-10-03 6970 VANGUARD OIL & GAS LLC Proposed Formation CLINTON Issued Date 10/3/2008 Expired Date 10/3/2009 6:00:00 AM
Plugged/Abandoned 2008-10-17 LOST HOLE
Construction Permit Expires 2009-10-03 LOST HOLE
Record Last Modified 2013-07-01 LOST HOLE

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1513901531 2013-6-21 0:00: FR No Violations
-1969533326 2008-10-17 0:00 PB No Violations
-527266483 2008-10-16 0:00 DD No Violations 2.00
0527266483 2008-10-16 Drill / Deepen / Reopen No Violations Inspection revealed that G&H Drilling is still having trouble getting the casing out of the hole. Appalachian Well Services arrived on site and shot holes in the bottom joint of the surface casing in an attempt to break circulation. This didnt work to break circulation so they kept trying to work the casing up and down . I advised that I was going to be out of town this weekend so if they needed an inspector for plugging the well or running surface casing to contact Inspector Claus.
0860676978 2008-10-14 Drill / Deepen / Reopen No Violations Inspection revealed that G&H Drilling is at 475 . No violations at this time.
1513901531 2013-06-21 Final Restoration No Violations No indication of well equipment, access road or tank battery.
1626390174 2008-10-15 Drill / Deepen / Reopen No Violations
1969533326 2008-10-17 Plug / Plug Back No Violations The surface hole was lost. 40 of 11-3/4 dia conductor casing and 511 of 8-5/8 dia surface casing was left in the hole. Cement plugs were set from 781 - 581 and from 200 - 0. On 10-18-2008, the surface plug had fallen to 24. Russell Miller topped off the hole with 40 sacks of sackrete. The drilling rig was skidded 20 to the north and a new well was spudded.
860676978 2008-10-14 0:00 DD No Violations 1.00

For data sources see[3]

References