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34-031-24113

Well Details

Well ID: 34-031-24113
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Country: United States
State: Ohio
County: Coshocton
Municipality: Perry Township
Operator Name: DUGAN GUY E
Well Pad ID:
Farm/Lease Name: CAMACHO-WALTON
License Status: Final Restoration
License Date: 2013-10-18
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1980-11-18
Well Total Depth:
Configuration: Vertical
Latitude: 40.240000
Longitude: -82.190000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-10-24 490 HILL DAVID R INC GeoDate 10/24/80
Reached Total Depth 1980-11-18 PERMIT EXPIRED
APP 2011-03-25 Proposed Formations:CLINTON, Issued Date:3/25/2011, Expired Date:3/24/2013 12:00:00 PM, Drilling unit acres:58, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2013-07-16 Operator changed from 490, HILL DAVID R INC to 882, DUGAN GUY E
APP 2013-10-18 Proposed Formations:CLINTON, Issued Date:10/18/2013, Expired Date:10/18/2015 12:00:00 PM, Drilling unit acres:58, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-05-01 PERMIT EXPIRED
Record Last Modified 2015-05-06 PERMIT EXPIRED
Construction Permit Expires 2015-10-18 PERMIT EXPIRED

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DAVID R HILL INC 120.00 584.00 0
1985 DAVID R HILL INC 164.00 453.00 365
1986 DAVID R HILL INC 695.00 404.00 365
1987 DAVID R HILL INC 320.00 304.00 365
1988 DAVID R HILL INC 1.00 268.00 365
1989 DAVID R HILL INC 0.00 219.00 365
1990 DAVID R HILL INC 0.00 208.00 365
1991 DAVID R HILL INC 0.00 142.00 365
1992 DAVID R HILL INC 0.00 114.00 365
1993 DAVID R HILL INC 0.00 152.00 365
1994 DAVID R HILL INC 0.00 38.00 365
1995 DAVID R HILL INC 0.00 74.00 365
1996 DAVID R HILL INC 0.00 37.00 365
2000 DAVID R HILL INC 0.00 34.00 365
2001 DAVID R HILL INC 0.00 0.00 365
2003 DAVID R HILL INC 0.00 64.00 365
2004 DAVID R HILL INC 0.00 69.00 365
2005 DAVID R HILL INC 0.00 42.00 365
2006 DAVID R HILL INC 0.00 0.00 0
2007 DAVID R HILL INC 0.00 66.00 365
2008 DAVID R HILL INC 0.00 0.00 0
2009 DAVID R HILL INC 0.00 0.00 0
2010 DAVID R HILL INC 0.00 0.00 0
2011 DAVID R HILL INC 0.00 0.00 0
2013 DAVID R HILL INC 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DAVID R HILL INC Brine 0 0
1985 DAVID R HILL INC Brine 45 365
1986 DAVID R HILL INC Brine 45 365
1987 DAVID R HILL INC Brine 45 365
1988 DAVID R HILL INC Brine 40 365
1989 DAVID R HILL INC Brine 25 365
1990 DAVID R HILL INC Brine 60 365
1991 DAVID R HILL INC Brine 50 365
1992 DAVID R HILL INC Brine 45 365
1993 DAVID R HILL INC Brine 30 365
1994 DAVID R HILL INC Brine 0 365
1995 DAVID R HILL INC Brine 15 365
1996 DAVID R HILL INC Brine 0 365
2000 DAVID R HILL INC Brine 0 365
2001 DAVID R HILL INC Brine 40 365
2003 DAVID R HILL INC Brine 0 365
2004 DAVID R HILL INC Brine 24 365
2005 DAVID R HILL INC Brine 0 365
2006 DAVID R HILL INC Brine 0 0
2007 DAVID R HILL INC Brine 0 365
2008 DAVID R HILL INC Brine 0 0
2009 DAVID R HILL INC Brine 0 0
2010 DAVID R HILL INC Brine 0 0
2011 DAVID R HILL INC Brine 0 0
2013 DAVID R HILL INC Brine 15 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1232720307 2004-1-7 0:00:0 PW No Violations
-1753662594 2014-4-23 0:00: PB No Violations
-30876894 2014-4-21 0:00: PB No Violations
0030876894 2014-04-21 Plug / Plug Back No Violations FOLLOW UP TO CA #1366911327: This inspection correlates with complaint #4300. On the day of my inspection Randy Moran pulled the rods and tubing from the well. They found that the fluid level was down approximately 700. I instructed them to tag bottom with their tools before washing any clay down the well.
0852052894 2014-04-15 Production Wells No Violations FOLLOW UP TO CA #1366911327: This inspection correlates with complaint #4300. On the day of my inspection I found that the well was still sitting idle with rods and tubing. The tank battery has been diked and there was peat moss spread over the area of contamination. I called Barry Dugan again. This time he claimed that Randy Moran was moving in to plug the well on 4/17/14. I made it clear to Mr. Dugan that this was his last warning. The next step would be referral for a Chiefs Order. I also advised him that Clark Clay was not approved for the plugging of an oil and gas well at this time.
1181599517 2011-02-28 Administrative Inspection No Violations Call from Dan Walker with Dave hill. Said company was applying for plugging permit.
1232720307 2004-01-07 Production Wells No Violations Well in production . Pumping well
1335411343 2014-04-24 Plug / Plug Back No Violations FOLLOW UP TO CA# 1366911327: This inspection correlates with complaint # 4300. On the day of my inspection Randy Moran pulled 440 of 8.625 casing from the well. Then they washed 13 tons of clay into the well and let it settle overnight.
1366911327 2013-04-25 Production Wells Violations Noted I received a call from Mr. Reuben Byler in regards to an idle well on his property. On the day of my inspection I found that the well head was equipped for a pumping unit. The pump had been removed, the well was overgrown with multiflora rose, and the rods were extending from the tubing. The tank battery consisted of one 100 barrel stock tank and one separator, with a poly brine tank sitting down hill from the main components. The tank battery was in heavy vegetation, there was no dike, the identification was barely legible and there was a 2 ft x 3 ft pool of standing crude oil at the base of the stock tank. The standing oil and contaminated soil must be cleaned up and legible identification must be posted. In its current state this well is incapable of production. Make well capable of commercial production within 30 days; or plugging is required within 90 days. Failure to comply may result in forfeiture of bond.
1389901389 2014-01-16 Administrative Inspection No Violations FOLLOW UP TO CA# 1366911327: This inspection correlates with complaint # 4300. The well was transferred to Dugan Drilling on 7/16/13, they obtained a plugging permit on 10/18/13. I contacted Barry Dugan to inquire as to when they planned to plug the well. He claims he will try to get it done in the next couple of weeks.
1389975587 2014-01-17 Administrative Inspection No Violations FOLLOW UP TO CA #1366911327: Barry Dugan called to inform me that Randy Moran was scheduled to plug the well next week.
1397760328 2014-04-17 Production Wells No Violations FOLLOW UP TO CA #1366911327: This inspection correlates with complaint #4300. On the day of my inspection I found that Randy Moran was moving in and rigging up to pull the rods and tubing form the well.
1398262929 2014-04-22 Plug / Plug Back No Violations FOLLOW UP TO CA #1366911327: This inspection correlates with complaint #4300. On the day of my inspection Randy Moran ran his ripping tools in to a depth of 3000, then they pulled up to find a telegraph. They got the 4.5 casing parted at 2664 and washed 2 tons of clay down the casing. They pulled 20 joints and shut down to let the clay settle.
1398433635 2014-04-25 Plug / Plug Back No Violations FOLLOW UP TO CA# 1366911327: This inspection correlates with complaint # 4300. On the day of my inspection I found that the fluid level was approximately 200 down. I contacted Barry Dugan to request that they top it off with more clay and leave the well open over the weekend.
1398865315 2014-04-29 Administrative Inspection No Violations FOLLOW UP TO CA# 1366911327: This inspection correlates with complaint # 4300. I received notification from Barry Dugan that they washed another 6 tons of clay into the well. He claimed that the well was filled to surface. I requested that he leave the well open for another 24 hours to let the clay settle.
1399040928 2014-05-01 Plug / Plug Back No Violations FOLLOW UP TO CA# 1366911327: This inspection correlates with complaint # 4300. On the day of my inspection I found that the clay was sitting firm at the surface. This well is plugged and abandoned. The area of contamination at the tank battery was cleaned up. This violation is resolved.
1430400518 2015-04-30 Final Restoration No Violations On the day of my inspection I found that the well site, lease road and tank battery site were never graded and seeded. The final restoration on this site was due on 11/01/2014. I called Barry Dugan about the restoration. He claimed that he had a signed landowner waiver. He met me in the field with a copy of the waiver.
1753662594 2014-04-23 Plug / Plug Back No Violations FOLLOW UP TO CA #1366911327: This inspection correlates with complaint #4300. On the day of my inspection Randy Moran washed 5 tons of clay into the well and pulled the 4.5 casing. They set a pre-cast cement plug at 935.
852052894 2014-4-15 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1366911327 US-OH-110809 2014-05-05 Well operation causing pollution and contamination
1366911327 US-OH-110810 2014-05-05 Well shall be plugged

For data sources see[7]

References