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34-045-20879

Well Details

Well ID: 34-045-20879
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Country: United States
State: Ohio
County: Fairfield
Municipality: Pleasant Township
Operator Name: B & B OIL/IRVIN & BURNS
Well Pad ID:
Farm/Lease Name: ROWLES HOWARD
License Status: Producing
License Date: 1983-09-14
Spud Date: 1983-10-25
Spud Drilling Contractor: SHOEMAKER DRLG
Final Drill Date: 1983-11-03
Well Total Depth: 572.00 ft
Configuration: Vertical
Latitude: 39.790000
Longitude: -82.490000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-09-14 2118 MERCURY OIL & GAS GeoDate 9/14/83
Oil and Gas 1983-09-14 Issued Date 9/14/83 Expired Date 3/12/84 Acres 0163340 Tool Type CT Proposed Formation NEWBURG Proposed Depth 00572 Proposed Drill Depth 00572
Original Spud 1983-10-25
Completed 1983-11-03
Reached Total Depth 1983-11-03
Completion Report Received 1983-12-09
Construction Permit Expires 1984-03-12
CO 1991-09-26 795 B & B OIL/IRVIN & BURNS GeoDate 9/14/83
Last Compliance Report 2018-04-05
Record Last Modified 2018-04-05

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 569 572 0
569 572 0
569 572 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NATURAL

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 QUESTA PETROLEUM CO 6619.00 0.00 0
1985 QUESTA PETROLEUM CO 7453.00 0.00 0
1986 QUESTA PETROLEUM CO 910.00 0.00 365
1987 QUESTA PETROLEUM CO 121.00 0.00 365
1988 QUESTA PETROLEUM CO 0.00 0.00 365
1989 QUESTA PETROLEUM CO 66.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 QUESTA PETROLEUM CO Brine 0 0
1985 QUESTA PETROLEUM CO Brine 0 0
1986 QUESTA PETROLEUM CO Brine 0 365
1987 QUESTA PETROLEUM CO Brine 0 365
1988 QUESTA PETROLEUM CO Brine 0 365
1989 QUESTA PETROLEUM CO Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1151888135 2018-1-23 0:00: TD No Violations 0.30
-1566523437 2003-11-3 0:00: PW No Violations
000CEN3176 1998-12-15 Production Wells No Violations 1509.12
1151888135 2018-01-23 Temporary Abandoned Annular Disposal No Violations I received a request from Central Office to determine if this well was being used for annular disposal. The well is not being used for annular disposal.
1566523437 2003-11-03 Production Wells No Violations Inspection for TOM TOMMASTIK for TAAD. Inspection revealed AD is not hooked-up. No violations noted this date. WEATHER CONDITIONS: Sunny and 75 degrees.
1608527079 2015-07-20 Production Wells No Violations I received a request from central office to determine the status of this well. The well consists of a rusted surface casing, 4.5 casing with a swage to 2.The well is not in production.
1961975741 2019-04-01 Orphan No Violations The well consisted of approximately 7 inch casing with 7 inch to 2 inch swage. Visible surface casing/conductor casing. There was a disconnected drip. The size of the casing is approximated due to unable to measure the casing. This well is being referred to the orphan well program.
CEN3176 1998-12-15 0:00 PW No Violations

For data sources see[9]

References