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34-053-20283

Well Details

Well ID: 34-053-20283
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Country: United States
State: Ohio
County: Gallia
Municipality: Addison Township
Operator Name: J T PLUS WELL SERVICE LLC
Well Pad ID:
Farm/Lease Name: ARROWOOD JACKIE & MYRNA
License Status: Producing
License Date: 1977-10-17
Spud Date: 1977-11-25
Spud Drilling Contractor:
Final Drill Date: 1977-12-11
Well Total Depth: 1865.00 ft
Configuration: Vertical
Latitude: 38.870000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-10-17 137 ALTHEIRS OIL INC GeoDate 10/17/77
Original Spud 1977-11-25 REV. LOC. 11-2-77
Completed 1977-12-11 REV. LOC. 11-2-77
Reached Total Depth 1977-12-11 REV. LOC. 11-2-77
Last Compliance Report 2017-03-17 REV. LOC. 11-2-77
Record Last Modified 2017-03-17 REV. LOC. 11-2-77

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ALTHEIRS OIL INC 595.00 737.00 365
1985 ALTHEIRS OIL INC 905.00 567.00 260
1986 ALTHEIRS OIL INC 759.00 507.00 365
1987 ALTHEIRS OIL INC 1153.00 563.00 365
1988 ALTHEIRS OIL INC 1170.00 506.00 365
1989 ALTHEIRS OIL INC 272.00 124.00 365
1990 ALTHEIRS OIL INC 1055.00 460.00 365
1991 ALTHEIRS OIL INC 1380.00 482.00 365
1992 ALTHEIRS OIL INC 1255.00 463.00 365
1993 ALTHEIRS OIL INC 1144.00 405.00 365
1994 ALTHEIRS OIL INC 823.00 273.00 365
1995 ALTHEIRS OIL INC 1020.00 288.00 365
1996 ALTHEIRS OIL INC 971.00 346.00 365
1999 ALTHEIRS OIL INC 582.00 213.00 365
2000 ALTHEIRS OIL INC 588.00 204.00 365
2001 ALTHEIRS OIL INC 600.00 188.00 365
2002 ALTHEIRS OIL INC 445.00 203.00 365
2003 ALTHEIRS OIL INC 266.00 107.00 365
2005 ALTHEIRS OIL INC 316.00 136.00 365
2006 ALTHEIRS OIL INC 454.00 147.00 365
2007 ALTHEIRS OIL INC 360.00 136.00 365
2008 ALTHEIRS OIL INC 482.00 105.00 365
2009 ALTHEIRS OIL INC 339.00 107.00 365
2010 ALTHEIRS OIL INC 400.00 200.00 365
2011 ALTHEIRS OIL INC 519.00 207.00 365
2012 ALTHEIRS OIL INC 668.00 196.00 366
2013 ALTHEIRS OIL INC 362.00 166.00 365
2014 ALTHEIRS OIL INC 217.00 117.00 365
2015 ALTHEIRS OIL INC 196.00 157.00 365
2016 ALTHEIRS OIL INC 40.00 12.00 365
2017 ALTHEIRS OIL INC 389.00 186.00 365
2018 ALTHEIRS OIL INC 207.00 118.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ALTHEIRS OIL INC Brine 0 365
1985 ALTHEIRS OIL INC Brine 0 260
1986 ALTHEIRS OIL INC Brine 0 365
1987 ALTHEIRS OIL INC Brine 0 365
1988 ALTHEIRS OIL INC Brine 0 365
1989 ALTHEIRS OIL INC Brine 0 365
1990 ALTHEIRS OIL INC Brine 0 365
1991 ALTHEIRS OIL INC Brine 0 365
1992 ALTHEIRS OIL INC Brine 0 365
1993 ALTHEIRS OIL INC Brine 0 365
1994 ALTHEIRS OIL INC Brine 0 365
1995 ALTHEIRS OIL INC Brine 0 365
1996 ALTHEIRS OIL INC Brine 0 365
1999 ALTHEIRS OIL INC Brine 0 365
2000 ALTHEIRS OIL INC Brine 0 365
2001 ALTHEIRS OIL INC Brine 0 365
2002 ALTHEIRS OIL INC Brine 0 365
2003 ALTHEIRS OIL INC Brine 0 365
2005 ALTHEIRS OIL INC Brine 0 365
2006 ALTHEIRS OIL INC Brine 0 365
2007 ALTHEIRS OIL INC Brine 0 365
2008 ALTHEIRS OIL INC Brine 0 365
2009 ALTHEIRS OIL INC Brine 0 365
2010 ALTHEIRS OIL INC Brine 0 365
2011 ALTHEIRS OIL INC Brine 0 365
2012 ALTHEIRS OIL INC Brine 2 366
2013 ALTHEIRS OIL INC Brine 2 365
2014 ALTHEIRS OIL INC Brine 2 365
2015 ALTHEIRS OIL INC Brine 2 365
2016 ALTHEIRS OIL INC Brine 2 365
2017 ALTHEIRS OIL INC Brine 0 365
2018 ALTHEIRS OIL INC Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1190315865 2017-2-27 0:00: PW No Violations 0.50
-1351953932 2005-9-27 0:00: PW No Violations
-1496317058 2010-2-26 0:00: PW No Violations
-1833366106 2009-5-4 0:00:0 PW No Violations
-421989194 2010-12-9 0:00: PW No Violations
-580626158 2010-3-10 0:00: PW No Violations
-761922990 2010-2-22 0:00: PW No Violations
-774982511 2010-2-25 0:00: PW No Violations
-792408612 2010-3-2 0:00:0 PW No Violations
-793163368 2016-2-11 0:00: TD No Violations 1.00
-953187363 2005-8-18 0:00: PW No Violations
0058272669 2017-02-01 Production Wells Violations Noted Well was equipped with pumping unit, electric motor, tubing and rods. Valves were open and the well was capable of production. Identification was faded and needs touched up. I called Pat Altier to have him redo the identification on the well.
0098595024 2010-02-24 Production Wells No Violations Oil spill cleanup. Talked to Pete Jeffers about their clean up plan. Pete told me that they were not able to extract oil from underflow dam yesterday but are in process of doing so now. I suggested that they work down stream with a broom and rake to get oil flowing to under flow dam for extraction. Pete Agreed and implemented the plan. I walked entire location and photographed clean up efforts.
0236408665 2010-03-04 Production Wells No Violations Oil spill clean up. Walked entire location from Campaign Creek to slip site. Observed oil covered leaf piles along intermittent stream bank. These leaves were removed from the stream to allow oil to flow to underflow dam. They were not bagged up for disposal. I noticed a heavy use of Pete sorb material was used along stream bank. Hillside looks good. Contaminated soil has been removed. Drainage ditches have been installed to channel surface runoff and any oil residue to two underflow dams constructed on hillside. This will prevent oil from entering the intermittent stream. The large underflow dam is still in place off of Pole Cat Road. Past this dam there are three oil booms in place before Campaign Creek. I talked to Pete Jeffers and Paul Altier about the need to contain and remove the oil soaked leaves and debris along the stream bank. They agreed to bag up and remove the leaves. Overall assessment of the intermittent stream and hillside is that the water is flowing clear and the majority of the contamination has been removed. All efforts have been made in preparation for a rain event that will help in dislodging any oil residue that remains. Oil should be well contained in the underflow dams for removal.
0263960730 2017-02-01 Temporary Abandoned Annular Disposal No Violations This well was not equipped for annular disposal.
0421989194 2010-12-09 Production Wells No Violations Oil spill follow up. Met with Jim Davis (landowner and contractor doing restoration for Altheirs Oil). Site is graded with water bars installed approximately every 50 feet on steep portions of location. Bio remediation compost pile is at top of hill next to private road way. I discussed with Jim the methods used for Bio remediation. The soil has an odor with some dark areas, no crude oil was seen in pile. Jim was waiting for our meeting before seed and straw is applied to site. I told him to proceed with the seed and straw. Site is not eroding and looks good.
0523489575 2010-03-01 Production Wells No Violations Oil spill clean up. Continuing to remove contaminated soil with trac hoe and load it into dump trailer and haul to top of hill. Contaminated soil is still being stock piled until it can be removed to a landfill. Talked to Lewis Altier on location. Jim Davis is making a series of containment areas and channels on the hillside after the contamination has been removed. This directs any contamination that might work loose to be contained and cleaned up on the hill side. Slight oil seepage was noticed in a few spots. The majority of the contamination has been removed.
0580626158 2010-03-10 Production Wells No Violations Oil spill clean up inspection. I talked to Pete Jeffers and PD Altier. They told me that a total of 111 tons of contaminated soil has been taken to the Kilbarger land fill. Jim Davis hauled 46 tons and Matt (Altiers truck ) hauled 65 tons. All of the contaminated soil that was taken to the top of the hill has been taken to the land fill. Straw and 2 small underflow dams are in place on hillside. Diversion ditches are channeling all runoff to the underflow dams to allow collection of oil residue. Site looks good. The underflow dam by Pole Cat road is functioning properly. Site has been exposed to a strong rain event last night and this morning. Site is containing oil residue and allowing continued cleanup of location.
0761922990 2010-02-22 Production Wells No Violations Oil spill reported on Arrowood lease by USCG, Dan OLeary and Ben Thompson. USCG called OEPA Dennis Deavers. Dennis Deavers Called Me at 11:00am. I arrived on location at 11:30am and talked to USCG and Pete Jeffers (Altheirs Pumper) I directed Pete to install a under flow dam at N38.88018/ W 082.15114. The oil spill was caused by a slip (N38.87700 / W082.15416) which sent a mud slide into the gathering line. The gathering line was 1.5 orange plastic. When the mud slid hit the line it stretched and broke the plastic line. 1972 of intermittent stream was affected. The intermittent stream flowed into Campaign Creek (Tributary of the Ohio River). Oil sheen was observed at the end of Campaign Creek as it flows into the Ohio river. Clean up efforts continued all day.
0774982511 2010-02-25 Production Wells No Violations Oil spill clean up. Pump truck on location at under flow dam. Another crew is removing contaminated soil with a trac hoe and loading it into a dump trailer that is attached to a dozer. The dozer is hauling the material to the top of the hill and stock piling it in a contained area until it can be taken to a land fill.
0792408612 2010-03-02 Production Wells No Violations Oil spill clean up. Contamination removal in progress. Arrangements have been made to haul contaminated soil to Killbarger landfill.
0793163368 2016-02-11 Temporary Abandoned Annular Disposal No Violations Visual inspection of well head found no AD hook up was present. AD is not in use.
0953187363 2005-08-18 Production Wells Violations Noted ID too faded to read
1036168299 2010-02-23 Production Wells No Violations Oil spill clean up. Oil sheen was observed on Campaign Creek as it enters Ohio River near Rail Road Bridge. Boom placed at end of intermittent stream N38.88104 / W082.15070 is not containing all of the flow and has let contamination into Campaign Creek. I directed Altheirs workers to fix the boom. The under flow dam is effective at containing the oil flow in intermittent stream. I met with ODNR Wildlife Officer Roy Rucker on site. We walked entire location. Pictures were taken by myself and Officer Rucker.
1190315865 2017-02-27 Production Wells No Violations Well had proper identification at the wellhead. No other violations noted.
1351953932 2005-09-27 Production Wells No Violations ID at wellhead now; landowner will rebuild powerlines jointly with Altier.
1424735160 2010-03-03 Production Wells No Violations Oil spill cleanup. Removing contaminated soil and stockpiling at top of hill. Hauling contaminated soil to Kilbarger landfill. Coordinated with Pete Jeffers and Paul Altier on the final excavation and plans on cleaning up the residue after a rain event. Oil residue will flow in drainage ditches to collection points on hillside with a small underflow dam to contain the oil.
1432541814 2004-05-18 Production Wells No Violations Not bad- small amount of leakage in front of wellhead. No ID.
1496317058 2010-02-26 Production Wells No Violations Oil spill clean up. Continuing to remove contaminated soil with trac hoe and load it into dump trailer and haul to top of hill. Contaminated soil is still being stock piled until it can be removed to a landfill.
1675354080 2004-04-08 Production Wells No Violations Stuffing box leak and ground contamination; No ID.
1763869328 2009-11-20 Annular Disposal No Violations Well is not connected for Annular Disposal. Brine is stored in a steel 150 bbl tank. Tank is in a dike. Well is in production.
1781854462 2010-09-22 Production Wells No Violations Oil spill follow up. Access path made during clean up is eroding needs graded and water bars installed. First under flow dam is free of oil. Soil has black staining no fresh oil. Contaminated soil needs to be removed to suitable location for bio remediation. Called Dale Compston and he will have Pete Jeffers contact me for a meeting.
1833366106 2009-05-04 Production Wells No Violations Good identification. Well is equipped with tubing, rods, Baker pump jack, electric motor, electric service. Polish rod is bright. Well is connected to production line. Well is not connected for AD. Brine is stored in steel tank.
236408665 2010-3-4 0:00:0 PW No Violations
263960730 2017-2-1 0:00:0 TD No Violations 0.50
523489575 2010-3-1 0:00:0 PW No Violations
58272669 2017-2-1 0:00:0 PW No Violations 0.50
98595024 2010-2-24 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0058272669 US-OH-126538 2017-02-14 9-9-05(A)10 Failure to legibly identify well
0953187363 US-OH-130887 2005-12-14 Failure to legibly identify well

For data sources see[7]

References