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34-059-22109

Well Details

Well ID: 34-059-22109
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Country: United States
State: Ohio
County: Guernsey
Municipality: Wills Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: HOSFELT HITCHCOCK
License Status: Final Restoration
License Date: 2013-02-27
Spud Date: 1977-08-22
Spud Drilling Contractor:
Final Drill Date: 1977-09-17
Well Total Depth: 5805.00 ft
Configuration: Vertical
Latitude: 40.040000
Longitude: -81.420000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-07-27 2143 CARLESS RESOURCES INC GeoDate 7/27/77
Original Spud 1977-08-22
Completed 1977-09-17
Reached Total Depth 1977-09-17
CO 1993-06-08 2143 CARLESS RESOURCES INC GeoDate 6/8/93
Unknown 1993-06-08 Issued Date 6/8/93 Expired Date 6/8/94 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 1998-06-15 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
APP 2003-09-17 Proposed Formations:CLINTON, Issued Date:9/17/2003, Expired Date:9/16/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2010-05-06 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2013-02-27 Proposed Formations:CLINTON, Issued Date:2/27/2013, Expired Date:2/27/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-06-24
Construction Permit Expires 2015-02-27
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5599 5700 0
5599 5700 0
5599 5700 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1916 Bbl 73500

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 2617.00 1.00 303
1987 ZILKHA ENERGY INC 2266.00 0.00 151
1988 CARLESS RESOURCES INC 2087.00 0.00 365
1989 CARLESS RESOURCES INC 1868.00 0.00 350
1990 CARLESS RESOURCES INC 1866.00 0.00 365
1991 CARLESS RESOURCES INC 1206.00 0.00 365
1992 CARLESS RESOURCES INC 0.00 0.00 0
1993 CARLESS RESOURCES INC 13.00 0.00 365
1994 CARLESS RESOURCES INC 0.00 0.00 0
1995 CARLESS RESOURCES INC 0.00 0.00 365
1996 CARLESS RESOURCES INC 0.00 0.00 0
1997 CARLESS RESOURCES INC 0.00 0.00 0
1998 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
1999 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2001 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2002 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2003 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2004 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2005 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2006 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2007 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 85.00 0.00 365
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 25 303
1987 ZILKHA ENERGY INC Brine 30 151
1988 CARLESS RESOURCES INC Brine 60 365
1989 CARLESS RESOURCES INC Brine 78 350
1990 CARLESS RESOURCES INC Brine 0 365
1991 CARLESS RESOURCES INC Brine 0 365
1992 CARLESS RESOURCES INC Brine 0 0
1993 CARLESS RESOURCES INC Brine 0 365
1994 CARLESS RESOURCES INC Brine 0 0
1995 CARLESS RESOURCES INC Brine 0 365
1996 CARLESS RESOURCES INC Brine 0 0
1997 CARLESS RESOURCES INC Brine 0 0
1998 EXCO - NORTH COAST ENERGY INC Brine 0 0
1999 EXCO - NORTH COAST ENERGY INC Brine 365
2000 EXCO - NORTH COAST ENERGY INC Brine 91 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 0
2002 EXCO - NORTH COAST ENERGY INC Brine 0 0
2003 EXCO - NORTH COAST ENERGY INC Brine 0 0
2004 EXCO - NORTH COAST ENERGY INC Brine 0 0
2005 EXCO - NORTH COAST ENERGY INC Brine 0 0
2006 EXCO - NORTH COAST ENERGY INC Brine 0 0
2007 EXCO - NORTH COAST ENERGY INC Brine 0 0
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0
2010 EXCO - NORTH COAST ENERGY INC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1128688381 2013-4-11 0:00: PW No Violations
0201467042 2014-05-29 Final Restoration No Violations On the day of my inspection the site passed final restoration according to 1509.072B.
0654717045 2012-11-27 Production Wells Violations Noted On the day of my inspection I seen the valves on the four inch casing were closed, there was no pumping unit at the well site, there is (1) two hundred ten barrel production tank/ separator/ setting inside a containment dike, the I.D. is posted on the production tank, the divisions records for the year of 2010 and 2011 do not meet division standards. The requirements will be to plug or produce or place in temporary inactive status, failure to comply will result in forfeiture of bond.
1128688381 2013-04-11 Production Wells No Violations On the day of my inspection I found there is no change in the status of the well, the permit issue date for plugging is 02/27/2013.
1371742075 2013-06-19 Plug / Plug Back No Violations I stopped in location and Chipco was milling on well with a junk mill. They pulled out the bit and it revealed that the bit was milling on a joint of crooked tubing or broke off 4.5casing. They had ran an impression tool. The company had been at 1600. They had pulled cork srew tubing and broke of 4.5casing 8 times. The mill would not go down any farther. They worked and made the attempt for two weeks. Per my discussion with supervisor we both agreed to start plugging. This is a Queenston well. There was no bottom hole plug or lime plug set. I took pictures of the pipe and tubing. There were four 2.875 collars and 2.375 tubing and mill to depth of 1669. Decided to Pull 4.5casing in morning and see what was retreived.
1371824341 2013-06-21 Plug / Plug Back No Violations Chipco is running in with 1.5tubing and tagged cement top at 1298.45. They are going to cement another 250 sacks of 50/50 poz in today. From 1298-582 is the calculated top.
1372078802 2013-06-24 Plug / Plug Back No Violations Rig tagged top at 650 and set plug there. Chipco pumped fresh water and broke circulation. Pumped 215 sacks of 50/50 poz and circulated back to surface. Topped off. Did not drop back.
1700072096 2013-06-20 Plug / Plug Back No Violations Chipco pulled up 4.5casing an pulled apart 1 joint beleow the graple tool at 1600. 1642of 4.5casing was retreived. Company than ran in with 1.5tubing and got to a depth on th annulus of the 4.5casing at 2140. Chipco will pump 250 sacks of 50/50 poz cement down 1.5tubing and tag in the morning.
201467042 2014-5-29 0:00: FR No Violations 0.50
2048099113 2013-06-05 Plug / Plug Back No Violations On the day of my inspection I witnessed the rig crew for Chipco assembling the over shot tool to retrieve the 4.5 casing that had parted, there was 1800 of 1.5 tubing laid out on the ground.
654717045 2012-11-27 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0654717045 US-OH-127415 2012-12-24 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[9]

References