If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-059-23091 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.12,"lon":-81.25,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Londonderry Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: BOND R | |
License Status: Final Restoration | |
License Date: 2014-10-07 | |
Spud Date: 1981-10-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-10-31 | |
Well Total Depth: 6400.00 ft | |
Configuration: Vertical | |
Latitude: 40.120000 | |
Longitude: -81.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-09-01 | 2143 CARLESS RESOURCES INC GeoDate 9/1/81 |
Original Spud | 1981-10-26 | |
Completed | 1981-10-31 | |
Reached Total Depth | 1981-10-31 | |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2014-10-07 | Proposed Formations:CLINTON, Issued Date:10/7/2014, Expired Date:10/6/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-03-13 | |
Construction Permit Expires | 2016-10-06 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6158 | 6160 | 3 |
2006-09-11 | 6164 | 6177 | 13 |
6158 | 6160 | 3 | |
6158 | 6160 | 3 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 70000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | ZILKHA ENERGY INC | 4331.00 | 6.00 | 301 |
1987 | ZILKHA ENERGY INC | 4459.00 | 5.00 | 208 |
1988 | CARLESS RESOURCES INC | 3710.00 | 0.00 | 365 |
1989 | CARLESS RESOURCES INC | 2726.00 | 0.00 | 350 |
1990 | CARLESS RESOURCES INC | 3222.00 | 0.00 | 365 |
1991 | CARLESS RESOURCES INC | 3471.00 | 0.00 | 365 |
1992 | CARLESS RESOURCES INC | 3303.00 | 0.00 | 365 |
1993 | CARLESS RESOURCES INC | 3383.00 | 0.00 | 365 |
1994 | CARLESS RESOURCES INC | 3016.00 | 0.00 | 365 |
1995 | CARLESS RESOURCES INC | 2981.00 | 0.00 | 365 |
1996 | CARLESS RESOURCES INC | 2653.00 | 0.00 | 365 |
1997 | CARLESS RESOURCES INC | 2398.00 | 0.00 | 365 |
1998 | EXCO - NORTH COAST ENERGY INC | 2095.00 | 0.00 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | 1227.00 | 0.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 1897.00 | 0.00 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | 1423.00 | 0.00 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | 1264.00 | 0.00 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | 1404.00 | 0.00 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | 1226.00 | 0.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 1070.00 | 45.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 980.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 1225.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 1313.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 762.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 843.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 1041.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 157.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 70 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1123720868 | 2014-9-10 0:00: | PW | No Violations | 0.00 |
-1146314396 | 2006-10-5 0:00: | PW | No Violations | |
-1242089784 | 2015-3-6 0:00:0 | PB | No Violations | 2.00 |
-1827981930 | 2015-3-11 0:00: | PB | No Violations | 8.50 |
-1870676341 | 2003-12-9 0:00: | PW | No Violations | |
-1884326669 | 2015-2-25 0:00: | PB | No Violations | 0.50 |
-1921591394 | 2015-3-5 0:00:0 | PB | No Violations | 3.00 |
-1998375273 | 2015-3-3 0:00:0 | PB | No Violations | 1.50 |
-2030253996 | 2015-3-13 0:00: | PB | No Violations | 4.00 |
-2039744385 | 2015-3-12 0:00: | PB | No Violations | 6.50 |
-272993745 | 2015-2-26 0:00: | PB | No Violations | 3.50 |
-289162951 | 2007-11-26 0:00 | PW | No Violations | |
-29503930 | 2015-3-2 0:00:0 | PB | No Violations | 2.00 |
-393112825 | 2015-2-18 0:00: | PB | No Violations | 1.50 |
-423521337 | 2015-3-9 0:00:0 | PB | No Violations | 4.00 |
-864720376 | 2015-2-24 0:00: | PB | No Violations | 2.00 |
-913587204 | 2015-3-10 0:00: | PB | No Violations | 5.00 |
-966142678 | 2009-2-18 0:00: | PW | No Violations | |
0029503930 | 2015-03-02 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service was milling with a 3.875 inch taper mill at 1519 feet. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
0188996581 | 2015-02-03 | Production Wells | No Violations | On the day of my inspection following up on NOV-1123720868, I witnessed that the production equipment included a 210bbl tank which was shared with the 34059228860000 Bond 1, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system with valves open on the tubing and the flowline shut and disconnected. AEU is rigging up Nomac Drilling Rig #137 adjacent to well with plans to begin drilling in 30 days. I placed call to Enervest requesting an update and my concerns on well and Tim McConaha stated that he would see how soon Knox Energy could plug the well. |
0212334407 | 2015-02-17 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had treated the well with 500 gallons of sulfur clear with minimal readings of 1ppm. Berry Well Service rigged up to pull the 1.5 inch tubing and found the tubing was parted at 1498 feet. Berry Well Service hauled the 1.5 inch tubing back to the yard and will be bringing back 2.875 inch tubing to begin to fish remainder of tubing from wellbore. |
0230230731 | 2015-12-15 | Final Restoration | No Violations | On the day of my inspection the wellhead has been removed with the casing being cut off 30 inches below grade and backfilled. The site passed final restoration according to ORC 1509.072B. |
0272993745 | 2015-02-26 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service tripped back in the casing with a 3.875 inch taper mill down to 1517 feet. BWS hooked up a mud pump and began pumping 10# brine to keep the mill cool. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
0278755831 | 2008-09-30 | Production Wells | No Violations | PRODUCING WELL |
0283526772 | 2014-12-30 | Production Wells | No Violations | On the day of my inspection following up on NOV-1123720868, I witnessed that the production equipment included a 210bbl tank which was shared with the 34059228860000 Bond 1, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system with valves open on the tubing and the flowline shut and disconnected. Well identification was present and production records are current but do not meet the minimum requirements for 2013. Enervest has applied for a plug permit with plans to plug well. |
0289162951 | 2007-11-26 | Production Wells | No Violations | PRODUCING WELL |
0393112825 | 2015-02-18 | Plug / Plug Back | No Violations | On the day of my inspection at the time of my arrival I witnessed Berry Well Service was not on site. I placed call to Berry Well Service and they plan on continuing on Friday of this week weather permitting. |
0423521337 | 2015-03-09 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had reached 1517 feet with a 3.625 inch fish with a 2.20 grapple. BWS circulated on fish and it pressured up to 900psi then pulled 48,000 to free up fish. BWS tripped out and retrieved 2.5 joints of 1.5 inch tubing. BWS will trip back in with fish and try to get over 1.5inch tubing again in the morning. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
0864720376 | 2015-02-24 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had made a run with their fishing tool and could not wash over tubing with an obstruction at 1526 feet. Berry Well Service made several unsuccessful attempts at running their 3.5 inch jars down to the obstruction. They will begin to milling on the tubing tomorrow. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
0913587204 | 2015-03-10 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had tripped back in with a 3.625 inch fish with a 2.20 grapple to a depth of 1607 feet. Appalachian Well Service was on site and ran down inside 1.5 inch tubing and had trouble several spots before setting down at 3152 feet. Appalachian Well Service made multiple attempts to getOn the day of my inspection I witnessed Berry Well Service had tripped back in with a 3.625 inch fish with a 2.20 grapple to a depth of 1607 feet. Appalachian Well Service was on site and ran down inside 1.5 inch tubing and had trouble several spots before setting down at 3152 feet. Appalachian Well Service made multiple attempts to get their tool down the tubing past 3152 feet and then shot the tubing off 3130 feet. BWS tripped pipe out of the hole, retrieved fish and will trip 2.375 inch tubing back in preparation for cementing tomorrow. |
0966142678 | 2009-02-18 | Production Wells | No Violations | PANCAKE ON SEPERATOR CHANGED OUT |
1123720868 | 2014-09-10 | Production Wells | Violations Noted | On the day of my inspection I witnessed that the production equipment included a 210bbl tank which was shared with the 34059228860000 Bond 1, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system with valves open on the tubing and the flowline shut and disconnected. Well identification was present and production records are current but do not meet the minimum requirements for 2013. Owner shall plug well within 180days. |
1146314396 | 2006-10-05 | Production Wells | No Violations | PRODUCING WELL |
1242089784 | 2015-03-06 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had reached 1583 feet with a 3.875 inch taper mill. BWS is going to clean the hole with the taper mill and then trip out and trip back in and try to fish on parted tubing. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
1424451393 | 2015-02-20 | Plug / Plug Back | No Violations | On the day of my inspection at the time of my arrival I witnessed Berry Well Service was not on site. After placing a call to Berry Well Service Bill Mitton stated due to the weather they plan on commencing operations again on Monday. |
1427121645 | 2015-03-23 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed the top of cement on the surface plugs was at 3 feet the production equipment has been removed and the location has been roughed in. |
1827981930 | 2015-03-11 | Plug / Plug Back | No Violations | On the date of inspection I accompanied ODNR Inspector Doug Bennett to witness the perforating of the 4.5 inch casing, setting the first plug in the well, and verifying that 4.5 inch casing could be pulled. |
1870676341 | 2003-12-09 | Production Wells | No Violations | status check |
1884326669 | 2015-02-25 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service was milling on the parted 1.5 inch tubing at 1515 feet with a 3.75 inch mill and gained approximately 1 foot in 2 hours. |
188996581 | 2015-2-3 0:00:0 | PW | No Violations | 1.00 |
1921591394 | 2015-03-05 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service was milling with a 3.875 inch taper mill at 1531 feet making 7 feet since yesterday. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
1998375273 | 2015-03-03 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service was milling with a 3.875 inch taper mill at 1523 feet and made 4 feet at the time of inspection. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
2030253996 | 2015-03-13 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service was rigging down and had tagged the top of cement at 19 feet and cement was topped off to surface. Tim McConaha of Enervest requested to leave 8.625 inch wellhead in place for a few weeks incase cement would drop so that it could be topped off again before final restoration is completed. Instructed operator to cut casing off 30 inches below grade and install metal plate identifying well and reclaim according to ORC 1509.072B. |
2036122153 | 2015-03-11 | Plug / Plug Back | No Violations | On the day of my inspection accompanied by ODNR Inspector Brandon Trigg, I witnessed Berry Well Service had tripped back in with 2.375 inch tubing to 3087 feet. Appalachian Well Service was on site and perforated 4.5 inch casing at with 10-1 11/16 inch shots from 3120 feet to 3110 feet. Petroset was on site and pumped a 400 foot 100 sack Class A cement with 2% Gel plug from 3091 feet to 2691 feet through 2.375 inch tubing. BWS tripped out the 2.375 inch tubing and pulled 4.5 inch casing which was parted at 1498 feet. |
2039744385 | 2015-03-12 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had retrieved 1498 feet of 4.5 inch casing where it was parted and tripped back in with 2.375 inch tubing to 1496 feet. Petroset was on site and pumped a 300 foot 80 sack Class A cement bottom of the Surface casing plug from 1491 feet to 1191 feet through 2.375 inch tubing. BWS pulled 41 joint s of 2.375 inch tubing and Petroset pumped a 75 sack 200 foot Class A cement Surface plug from 200 feet to surface. BWS pulled remaining 7 joints of tubing and cement dropped and Petroset topped off with 35 sacks. Cement dropped again to 19 feet below surface and BWS was instructed to check level of plug tomorrow and let ODNR know level so I can be present for additional top off. NOV-1123720868 is resolved |
2101443595 | 2015-03-04 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service was milling with a 3.875 inch taper mill at 1524 feet. BWS is planning on tripping out of well this afternoon to see the condition of the mill. Readings taken with ODNR Honeywell PhD6 meter revealed no H2S at the time of inspection. |
212334407 | 2015-2-17 0:00: | PB | No Violations | 1.50 |
230230731 | 2015-12-15 0:00 | FR | No Violations | 1.00 |
278755831 | 2008-9-30 0:00: | PW | No Violations | |
283526772 | 2014-12-30 0:00 | PW | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1123720868 | US-OH-103122 | 2015-03-13 | Well shall be plugged |
For data sources see[9]