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Well ID: 34-059-24183 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Wheeling Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: US-OH-000415 | |
Farm/Lease Name: RHDK INVESTMENTS 21-4-4 1 | |
License Status: Final Restoration | |
License Date: 2011-05-18 | |
Spud Date: 2011-08-03 | |
Spud Drilling Contractor: NOMAC DRILLING CORP | |
Final Drill Date: 2011-08-23 | |
Well Total Depth: 6460.00 ft | |
Configuration: Vertical | |
Latitude: 40.150000 | |
Longitude: -81.630000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-05-18 | Proposed Formations:TRENTON-BLACK RIVER, Issued Date:5/18/2011, Expired Date:5/17/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:ST, Proposed Well Class:STRT |
Reached Total Depth | 2011-08-23 | |
Plugged Back | 2011-08-24 | |
Construction Permit Expires | 2013-05-17 | |
Record Last Modified | 2015-07-01 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2012-07-19 | 7149 | 7383 | 60 |
2012-07-02 | 9750 | 9756 | 37 |
2012-07-02 | 8309 | 8543 | 60 |
2012-07-02 | 8599 | 8833 | 60 |
2012-07-02 | 8889 | 9123 | 60 |
2012-07-02 | 7439 | 7673 | 60 |
7149 | 7383 | 60 | |
6859 | 7093 | 60 | |
9469 | 9703 | 60 | |
9750 | 9756 | 37 | |
9179 | 9413 | 60 | |
8889 | 9123 | 60 | |
8599 | 8833 | 60 | |
8309 | 8543 | 60 | |
8019 | 8253 | 60 | |
7729 | 7963 | 60 | |
7439 | 7673 | 60 | |
6569 | 6803 | 60 | |
6279 | 6513 | 60 | |
6279 | 6513 | 60 | |
2012-07-02 | 7729 | 7963 | 60 |
2012-07-02 | 6279 | 6513 | 60 |
2012-07-02 | 6569 | 6803 | 60 |
2012-07-19 | 6859 | 7093 | 60 |
2012-07-02 | 8019 | 8253 | 60 |
2012-07-02 | 9179 | 9413 | 60 |
2012-07-02 | 9469 | 9703 | 60 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 04/20/2012 | 04/20/2012 | 6154.0 | 4142536.0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Schlumberger | Aliphatic acids | Trade Secret | 0.0015 | 0.00023 | |||
Glutaraldehyde | 111-30-8 | 0.03015 | 0.00462 | |||||
Methanol | 67-56-1 | 0.00196 | 0.0003 | |||||
Hydrochloric Acid | 7647-01-0 | 0.84627 | 0.12967 | |||||
Ethane-1,2-diol | 107-21-1 | 0.00313 | 0.00048 | |||||
Aliphatic polyol | Trade Secret | 0.2993 | 0.04586 | |||||
Carbohydrate polymer | Trade Secret | 1.09368 | 0.16758 | |||||
Aliphatic alcohols, ethoxylated #1 | Trade Secret | 0.0015 | 0.00023 | |||||
Diammonium peroxidisulphate | 7727-54-0 | 0.04203 | 0.00644 | |||||
Ammonium sulfate | 7783-20-2 | 0.03563 | 0.00546 | |||||
Trisodium ortho phosphate | 7601-54-9 | 0.00313 | 0.00048 | |||||
Sodium erythorbate | 6381-77-7 | 0.00352 | 0.00054 | |||||
Sodium tetraborate decahydrate | 1303-96-4 | 0.22451 | 0.0344 | |||||
Ceramic materials and wares, chemicals | 66402-68-4 | 4.67325 | 0.71606 | |||||
Prop-2-yn-1-ol | 107-19-7 | 0.00052 | 0.00008000 | |||||
Crystalline silica | 14808-60-7 | 90.11005 | 13.80713 | |||||
Slickwater, Crosslinked Fluid, WF100 | Schlumberger | Base Fluid, Bactericide, Breaker, Ceramic Proppant, Corrosion Inhibitor, Crosslinker, Friction Reducer, Gelling Agent, Hydrochloric Acid, Iron Stabilizer, Sand, Scale Inhibitor | Water (Including Mix Water Supplied by Client) | - | None | 84.67748 |
For data sources see[4]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2012 | ENERVEST OPERATING LLC | Brine | 6201 | 111 |
2013 | ENERVEST OPERATING LLC | Brine | 1230 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 1201 | 365 |
2015 | ENERVEST OPERATING LLC | Brine | 1940 | 365 |
2016 | ENERVEST OPERATING LLC | Brine | 157 | 366 |
2017 | ENERVEST OPERATING LLC | Brine | 150 | 365 |
2018 | ENERVEST OPERATING LLC | Brine | 204 | 365 |
2019 | ENERVEST OPERATING LLC | Brine | 13 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1001766348 | 2011-8-9 0:00:0 | DD | No Violations | |
-1102077970 | 2011-8-5 0:00:0 | DD | No Violations | |
-142642668 | 2012-4-16 0:00: | CT | No Violations | |
-1758630881 | 2013-6-27 0:00: | FR | No Violations | 1.00 |
-2006381387 | 2013-10-21 0:00 | PW | No Violations | |
-747978736 | 2011-6-1 0:00:0 | NW | No Violations | |
-93671075 | 2011-7-7 0:00:0 | DD | No Violations | |
0093671075 | 2011-07-07 | Drill / Deepen / Reopen | No Violations | On site to witness conductor pipe being set and cemented in place and also 75 of 16 casing being set for operational purposes(mousehole). |
0142642668 | 2012-04-16 | Completion Testing | No Violations | On site with supervisor to witness first stage of frac job. |
0187055215 | 2016-02-22 | Production Wells | No Violations | On the day of my inspection I witnessed the access to the location was gated, fenced and locked with proper current owner Enervest Operating emergency contact and well information in place on the gate. The well was equipped with 5.5 inch production tree, tubing, rods and a Lufkin pumping unit with valves in the open position along with the unit in operation. The production equipment included a sand trap, a 50bbl sand tank, a GP unit, a disconnected heater treater and 12-210bbl tanks within a lined containment. Identification was displayed at the wellhead with production records current. |
0747978736 | 2011-06-01 | Non Well | No Violations | Multi well drilling pad site construction began. |
0875601591 | 2011-07-06 | Drill / Deepen / Reopen | No Violations | Stopped by drill site to check on upcoming conductor job. |
1001766348 | 2011-08-09 | Drill / Deepen / Reopen | No Violations | On site to witness bond logging of 13.375 surface casing and testing of Blowout Preventer Stack,Greenes Testing preformed testing they tested blind rams at 2500 psi and pipe rams at 2500 psi and annular element at 1500 psi ad we also checked choke manifold at 2500 psi all test passed and they will resume drilling 12.250 hole and set 9.625 casing later on in the week. |
1102077970 | 2011-08-05 | Drill / Deepen / Reopen | No Violations | On site to with operator run conductor pipe in well they ran 296 of 20 casing in hole and cemented it in place. |
1311024859 | 2012-06-08 | Preliminary Restoration | No Violations | Restoration work at site satisfactory . |
1314570597 | 2011-08-28 | Drill / Deepen / Reopen | No Violations | Inspected site at request of company rep they had drilling fluid spill within containment area 42 bbl was lost due to fact that 4 hose broke 25 bbl was contained in dike area and 17 bbl was spilled into lined area covered in stone they removed stone and had vac truck clean entire area and then new stone was applied to area, all affected material was hauled to approved landfill. |
1314744348 | 2011-08-30 | Drill / Deepen / Reopen | No Violations | Stopped by drill rig for update on depth they were drilling lateral section of hole@9428 site consultant stated they should be ready to run 5.5 sometime early Thursday morning. |
1541685688 | 2018-11-07 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with 5.5-inch production casing with a production tree, tubing, rods, and a pumping unit. Production valves were in the open position. The production equipment consisted of one sand trap, one gas production unit, one disconnected heater treater, one 50-barrel, and twelve 210-barrel tanks. Identification was posted at the wellhead with production records current. |
1758630881 | 2013-06-27 | Final Restoration | No Violations | Everything passed according to 1509.072B. |
187055215 | 2016-2-22 0:00: | PW | No Violations | 2.00 |
1942784318 | 2012-04-19 | Completion Testing | No Violations | Stopped by frac job and witnessed stage 11&12 and starting of pump down process of setting plug for stage 13 to be preformed tomorrow. |
2006381387 | 2013-10-21 | Production Wells | No Violations | On the day of my inspection, I found at the well head 5.5 production casing and gate valves, the valves were open, there is a pumping unit at the well head that was not operating at the time of my inspection, there are twelve four hundred barrel production tanks setting inside containment, the I.D. is posted on the entry gate. |
2113395950 | 2011-07-31 | Drill / Deepen / Reopen | No Violations | Nomac rig 43 moving in on site according to drilling supervisor they should be up and running by 8/2/11. |
2142668271 | 2011-08-26 | Drill / Deepen / Reopen | No Violations | Stopped by drill rig for update they were drilling@5622 and top of cement kick plug was at 4930 and they started there kick@5310they stated that they would drill to total depth by late next week. |
875601591 | 2011-7-6 0:00:0 | DD | No Violations |
For data sources see[7]