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| Well ID: 34-067-21506 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Harrison | |
| Municipality: Archer Township | |
| Operator Name: CHESAPEAKE EXPLORATION LLC | |
| Well Pad ID: US-OH-001277 | |
| Farm/Lease Name: SADIE 33-10-4 | |
| License Status: Not Drilled | |
| License Date: 2015-07-15 | |
| Spud Date: | |
| Spud Drilling Contractor: | |
| Final Drill Date: | |
| Well Total Depth: | |
| Configuration: Vertical | |
| Latitude: 40.330000 | |
| Longitude: -80.970000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2015-07-15 | Proposed Formations:TRENTON THRU BLACK RIVER, Issued Date:7/15/2015, Expired Date:7/14/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
| Construction Permit Expires | 2017-07-14 | |
| Record Last Modified | 2018-11-01 |
For data sources see[2]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| 1508179288 | 2017-10-16 | Casing String Witnessed | No Violations | On the day of my inspection I witnessed express energy cement the 20 inch diameter conductor casing. A 30 inch diameter casing was set to 40 feet and the backside was ready-mixed. The pad is on strip ground and they had to stabilize the unconsolidated material to reach total depth. A 26 inch diameter hole was augered to 120 feet. Express cemented the 20 inch diameter casing with 237 sacks of class A cement. Cement weighed 15.6 with mud scale and has a yield of 1.18. Additives include 2% cacl and .5#/sk celloflake. 50% excess ran in open hole from 40 to 120. Cement displaced with 39 barrels of water. No cement returned to surface. Cement was tagged at 31 four hours later. Last 31 feet was ready mixed. |
For data sources see[3]