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34-067-21521

Well Details

Well ID: 34-067-21521
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Country: United States
State: Ohio
County: Harrison
Municipality: Nottingham Township
Operator Name: ASCENT RESOURCES UTICA LLC
Well Pad ID: US-OH-001355
Farm/Lease Name: ROSE S NTG HR
License Status: Producing
License Date: 2016-01-28
Spud Date: 2017-03-01
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2017-03-21
Well Total Depth: 14665.00 ft
Configuration: Horizontal
Latitude: 40.280000
Longitude: -81.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2016-01-28 Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:1/28/2016, Expired Date:1/27/2018 12:00:00 PM, Drilling unit acres:514.559, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2017-03-21 STATUS UPDATE PER AS-DRILLED PLAT RCVD ALE 12/19/17. SPUD DATE IS ESTIMATED; STATUS UPDATED FROM PRODUCTION
Completion Report Received 2017-12-19 STATUS UPDATE PER AS-DRILLED PLAT RCVD ALE 12/19/17. SPUD DATE IS ESTIMATED; STATUS UPDATED FROM PRODUCTION
Conversion to Producer 2017-12-19 UPDATE TARGET/TAKE PER AS-DRILLED PLAT
Construction Permit Expires 2018-01-27 STATUS UPDATE PER AS-DRILLED PLAT RCVD ALE 12/19/17. SPUD DATE IS ESTIMATED; STATUS UPDATED FROM PRODUCTION
Record Last Modified 2018-02-09 STATUS UPDATE PER AS-DRILLED PLAT RCVD ALE 12/19/17. SPUD DATE IS ESTIMATED; STATUS UPDATED FROM PRODUCTION

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2017-12-27 13175 13316 30
2017-12-27 14396 14500 18
14396 14500 18
13175 13316 30
13175 13316 30

For data sources see[3]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 06/15/2017 06/24/2017 8083 8,596,810.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Water Ascent Carrier/Base Fluid Water 7732-18-5 100 87.9024 71,740,400.0
KFR-23 Keane Friction Reducer copolymer of 2-propenamide Proprietary 10 0.00638824 5213.68
Distillates (petroleum), hydrotreated light 64742-47-8 45 0.0287471 23461.6
oleic acid diethanolamide 93-83-4 2 0.00127765 1042.74
Alcohols, C12-16, ethoxylated 68551-12-2 2 0.00127765 1042.74
Other Chemical(s) Listed Above See Trade Name(s) List copolymer of 2-propenamide Proprietary 10 0.00638824 5213.68
Ethoxylated alcohol 68131-39-5 10 0.000238345 194.522
proprietary proprietary 10 0 0
oleic acid diethanolamide 93-83-4 2 0.00127765 1042.74
Polyanionic cellulose polymer 9004-32-4 50 0 0
Tar bases, quinoline derivs., benzyl chloride-quaternized 72480-70-7 10 0.000238345 194.522
quaternary ammonium compounds,

benzyl-C12-16-alkyldimethyl, chlorides

68424-85-1 5.3 0.00111664 911.335
Citric acid 77-92-9 40 0.00483131 3943.01
didecyldimethylammonium chloride 7173-51-5 8 0.00167602 1367.86
propan-2-ol 67-63-0 5 0.000119172 97.261
Alcohols, C12-16, ethoxylated 68551-12-2 2 0.00127765 1042.74
formic acid 64-18-6 10 0.000238345 194.522
Water 7732-18-5 92.5 0.0594417 48512.5
Cinnamaldehyde 104-55-2 10 0.000238345 194.522
Distillates (petroleum), hydrotreated light 64742-47-8 55 0.00711377 5805.81
dipropylene gylcol, monomethyl ether 34590-94-8 20 0.000476689 389.044
Water 7732-18-5 85 0.950414 775668
KSI-19 Keane Scale Inhibitor Methanol 67-56-1 30 0.0132842 10841.7
Hydrochloric Acid (7.5%) Keane Acid Inhibitor Water 7732-18-5 92.5 0.0594417 48512.5
Hydrochloric Acid 7647-01-0 7.5 0.0048196 3933.45
KFEAC-30 Keane Iron Control Citric acid 77-92-9 40 0.00483131 3943.01
acetic acid 64-19-7 60 0.00724697 5914.52
MBC-516 Keane Biocide didecyldimethylammonium chloride 7173-51-5 8 0.00167602 1367.86
glutaral 111-30-8 26.7 0.00561477 4582.42
quaternary ammonium compounds,

benzyl-C12-16-alkyldimethyl, chlorides

68424-85-1 5.3 0.00111664 911.335
KWBO-2 Keane Breaker Sodium persulfate 7775-27-1 99 0.00015357 125.334
KAI-13 Keane Acid Inhibitor ethanediol 107-21-1 40 0.000953379 778.088
formic acid 64-18-6 10 0.000238345 194.522
Tar bases, quinoline derivs., benzyl chloride-quaternized 72480-70-7 10 0.000238345 194.522
propan-2-ol 67-63-0 5 0.000119172 97.261
Ethoxylated alcohol 68131-39-5 10 0.000238345 194.522
Cinnamaldehyde 104-55-2 10 0.000238345 194.522
dipropylene gylcol, monomethyl ether 34590-94-8 20 0.000476689 389.044
KWG-111L Keane Gel Distillates (petroleum), hydrotreated light 64742-47-8 55 0.00711377 5805.81
Guar gum 9000-30-0 55 0.00711377 5805.81
Hydrochloric Acid (15%) Keane Acidizing Hydrochloric Acid 7647-01-0 15 0.16772 136883
Water 7732-18-5 85 0.950414 775668
Sand (Proppant) Keane Proppant Crystalline silica: Quartz (SiO2) 14808-60-7 100 10.7585 8,780,370.0

For data sources see[4]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2017-06-15 H2O 15 6447 Bbl 233090 Keane Frac STAGE 1/35

STAGES 2-34 SEE IMAGES

2017-06-18 H2O 15 5688 Bbl 256693 Keane Frac STAGE 35/35

STAGES 2-34 SEE IMAGES

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 20981.00 112.00 325
2017 ASCENT RESOURCES UTICA LLC 299501 50768 133
2018 ASCENT RESOURCES UTICA LLC 443358 42205 316
2019 ASCENT RESOURCES UTICA LLC 81242 14006 82

For data sources see[6] [7]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 905 325
2017 ASCENT RESOURCES UTICA LLC Brine 9162 133
2018 ASCENT RESOURCES UTICA LLC Brine 4318 316
2019 ASCENT RESOURCES UTICA LLC Brine 7318 82

For data sources see[8] [9]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1497046893 2017-3-7 0:00:0 DD No Violations 6.00
-826482964 2017-11-6 0:00: PW No Violations 1.00
0826482964 2017-11-06 Production Wells No Violations On the day of my inspection I found this pad to contain 4 properly labled wellheads. Surface casing annular pressure is 0 and the intermeidate casing annualr pressure is 700. Production equipment includes six 400 barrel steel tanks inside steel containment, a vapor recovery system, combustor, two compressors, four gas production units and four sand seperators. No production records in RBDMS.
1417834974 2019-11-8 0:00: PW No Violations 1.00
1488308391 2017-02-28 Drill / Deepen / Reopen No Violations Upon arrival on location I found the rig crew rigging up on the well pad. They will be starting on the Rose 2H. Rig up is about 25 % complete.
1488463487 2017-03-02 Drill / Deepen / Reopen No Violations Upon arrival on location I found the rig crew rigging up on the well pad. They are projecting the to start drilling on Sunday March 4.
1489584063 2017-03-15 Drill / Deepen / Reopen No Violations Up no arrival on location I found the rig crew had run 9 5/8 inch casing to the depth of 7305 feet, with a two stage tool at 3504 feet. The first stage was complete when I arrived, and the second stage was in progress. Upon further inspection there were no issues at this time.
1497046893 2017-03-07 Drill / Deepen / Reopen No Violations Upon arrival on location I found the rig crew running 13 3/8 inch casing in a 17.5 inch hole to a depth of 1326 feet. The surface casing will be cemented by Halliburton. 1270 sacks at a yield of 1.24 was pumped and displaced with 195 bbl. of fresh water. Circulation was established and circulated 45 bbl. of good cement returns to surface.
1672666814 2018-03-19 Preliminary Restoration No Violations On the day of my inspection I found this pad to contain 4 properly labled wellheads. Surface casing annular pressure is 8 and the intermediate casing annular pressure is 808. Production equipment includes six 400 barrel steel tanks inside steel containment, a vapor recovery system, combustor, two compressors, four gas production units and four sand seperators. Site meets the requirements of ORC 1509.072A for preliminary restoration. A hydraulic line blew on a tanker truck today on location. A skid steer arrived on location during my inspection and removed the contaminated gravel. Gravel was already shoveled into piles by hand tools. Estimated 3 gallons of hydraulic oil spilled.

For data sources see[10]

References