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| Well ID: 34-073-21336 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Hocking | |
| Municipality: Falls Township | |
| Operator Name: HOCKING HILLS ENERGY AND WELL | |
| Well Pad ID: | |
| Farm/Lease Name: BROWN HARRY & JOE | |
| License Status: Producing | |
| License Date: 1967-08-22 | |
| Spud Date: 1967-09-12 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1967-10-06 | |
| Well Total Depth: 2772.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.550000 | |
| Longitude: -82.390000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1967-08-22 | 3175 BROCO INDUSTRIES GeoDate 8/22/67 |
| Original Spud | 1967-09-12 | |
| Completed | 1967-10-06 | |
| Reached Total Depth | 1967-10-06 | |
| Change of Owner | 2009-08-11 | Operator changed from 3175, BROCO INDUSTRIES to 5755, CHIEFTAIN ENERGY CORP |
| Record Last Modified | 2013-10-03 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 2326 Bbl | 30000 | 800# HULLS |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1987 | WNT OPERATING INC | 0.00 | 202.00 | 365 |
| 1988 | WNT OPERATING INC | 0.00 | 131.00 | 199 |
| 2007 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
| 2008 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
| 2009 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
| 2010 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
| 2011 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
| 2012 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 366 |
| 2013 | HOCKING HILLS ENERGY AND WELL | 0.00 | 166.00 | 365 |
| 2014 | HOCKING HILLS ENERGY AND WELL | 0.00 | 199.00 | 365 |
| 2015 | HOCKING HILLS ENERGY AND WELL | 0.00 | 37.00 | 365 |
| 2016 | HOCKING HILLS ENERGY AND WELL | 0.00 | 27.00 | 365 |
| 2017 | HOCKING HILLS ENERGY AND WELL | 0.00 | 6.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1987 | WNT OPERATING INC | Brine | 315 | 365 |
| 1988 | WNT OPERATING INC | Brine | 240 | 199 |
| 2007 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
| 2008 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
| 2009 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
| 2010 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
| 2011 | HOCKING HILLS ENERGY AND WELL | Brine | 150 | |
| 2012 | HOCKING HILLS ENERGY AND WELL | Brine | 120 | 366 |
| 2013 | HOCKING HILLS ENERGY AND WELL | Brine | 3990 | 365 |
| 2014 | HOCKING HILLS ENERGY AND WELL | Brine | 2730 | 365 |
| 2015 | HOCKING HILLS ENERGY AND WELL | Brine | 510 | 365 |
| 2016 | HOCKING HILLS ENERGY AND WELL | Brine | 410 | 365 |
| 2017 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| 0394640947 | 2004-10-13 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
| 0870901098 | 2004-08-25 | Production Wells | Violations Noted | An inspection of the well revealed no ID at the well or tank battery, water knock out has over flowed allowing oil to run down tank into dike area. |
| 394640947 | 2004-10-13 0:00 | PW | No Violations | |
| 870901098 | 2004-8-25 0:00: | PW | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0870901098 | US-OH-129915 | 2004-08-25 | Well operation causing pollution and contamination | |
| 0870901098 | US-OH-129916 | 2004-08-25 | Failure to legibly identify well | |
| 0870901098 | US-OH-129917 | 2004-08-25 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[8]