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34-079-20138

Well Details

Well ID: 34-079-20138
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Country: United States
State: Ohio
County: Jackson
Municipality: Franklin Township
Operator Name: ARTEX OIL COMPANY
Well Pad ID:
Farm/Lease Name: TREPAINER FRED & CLAREBELL
License Status: Producing
License Date: 1981-11-09
Spud Date: 1981-12-16
Spud Drilling Contractor:
Final Drill Date: 1981-12-18
Well Total Depth: 1735.00 ft
Configuration: Vertical
Latitude: 39.000000
Longitude: -82.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-11-09 518 GOODYEAR TIRE & RUBBER GeoDate 11/9/81
Original Spud 1981-12-16
Completed 1981-12-18
Reached Total Depth 1981-12-18
Change of Owner 2006-01-11 Operator changed from 518, GOODYEAR TIRE & RUBBER to 5352, ARTEX OIL COMPANY
Record Last Modified 2017-02-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1448 1474 14
1448 1474 14
1448 1474 14

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 709 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 GOODYEAR TIRE & RUBBER 1961.00 0.00 365
1985 GOODYEAR TIRE & RUBBER 1546.00 0.00 0
1986 GOODYEAR TIRE & RUBBER 1336.00 0.00 365
1995 GOODYEAR TIRE & RUBBER 885.00 0.00 365
1996 GOODYEAR TIRE & RUBBER 1148.00 0.00 365
2005 ARTEX OIL COMPANY 0.00 0.00 365
2006 ARTEX OIL COMPANY 606.00 0.00 365
2007 ARTEX OIL COMPANY 1966.00 0.00 365
2008 ARTEX OIL COMPANY 0.00 0.00 365
2009 ARTEX OIL COMPANY 0.00 0.00 365
2010 ARTEX OIL COMPANY 0.00 0.00 365
2011 ARTEX OIL COMPANY 0.00 0.00 365
2012 ARTEX OIL COMPANY 0.00 0.00 366
2013 ARTEX OIL COMPANY 0.00 0.00 365
2014 ARTEX OIL COMPANY 0.00 0.00 365
2015 ARTEX OIL COMPANY 0.00 0.00 365
2016 ARTEX OIL COMPANY 0.00 0.00 365
2017 ARTEX OIL COMPANY 0.00 0.00 365
2018 ARTEX OIL COMPANY 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 GOODYEAR TIRE & RUBBER Brine 0 365
1985 GOODYEAR TIRE & RUBBER Brine 0 0
1986 GOODYEAR TIRE & RUBBER Brine 0 365
1995 GOODYEAR TIRE & RUBBER Brine 0 365
1996 GOODYEAR TIRE & RUBBER Brine 0 365
2005 ARTEX OIL COMPANY Brine 0 365
2006 ARTEX OIL COMPANY Brine 0 365
2007 ARTEX OIL COMPANY Brine 0 365
2008 ARTEX OIL COMPANY Brine 0 365
2009 ARTEX OIL COMPANY Brine 0 365
2010 ARTEX OIL COMPANY Brine 0 365
2011 ARTEX OIL COMPANY Brine 0 365
2012 ARTEX OIL COMPANY Brine 0 366
2013 ARTEX OIL COMPANY Brine 0 365
2014 ARTEX OIL COMPANY Brine 0 365
2015 ARTEX OIL COMPANY Brine 0 365
2016 ARTEX OIL COMPANY Brine 0 365
2017 ARTEX OIL COMPANY Brine 0 365
2018 ARTEX OIL COMPANY Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1188408547 2007-8-2 0:00:0 PW No Violations
-1193717496 2004-10-13 0:00 PW No Violations
-157175075 2004-10-13 0:00 PW No Violations
-2094333585 2012-9-18 0:00: PW No Violations 1.00
0157175075 2004-10-13 Production Wells Violations Noted Extension of NOV correction deadline.
0309870370 2012-11-08 Administrative Inspection No Violations Performed Temporary Inactive Audit for Artexs TI application. Dean Price, Artexs well tender for this well, accompanied me on this audit and provided access to this well. Checked all valves to be sure they were closed; no leaks were measured with the Honeywell PhD6 gas meter nor observed by myself; all gas lines on the sales side of the well head including the gas line to Jackson were empty according to Dean Harris and have been since this well was shut in. The well meets the requirements for TI status.
1188408547 2007-08-02 Production Wells No Violations Well is capable of production, all valves are open. Id is on the ground beside the well.
1193717496 2004-10-13 Production Wells Violations Noted FOLLOW UP TO NOV # 1537997171 No ID; small brine scald area. Shut-off.
1537997171 2004-10-13 Production Wells No Violations No ID; small brine scald area. Shut-off.
2094333585 2012-09-18 Production Wells Violations Noted Inspected the three shut-in ARTEX wells (Trepanier 1&2, API 34079201020000 & API 34079201380000) and Garrett #2 (API 3407920206) with Don Huck (Exploration Manager for Artex) and Dean Harris (oiler for Artex). Found all three wells were leaking gas between the 2-3/8 inch production tubing and the $-1/2 inch intermediate csg at the tubing ring on the casing head. I expect them to contact me by this coming Thursday 09/20/2012 on what they plan to do or that they have corrected the problem. Don contacted me on Wednesday 09/19/2012 that the leak has been fixed. I field checked the wells with the Honeywell PHD 6/ PID gas meter and doused with bottle water covering where the leaks occurred and there was no reading on the meter and no bubbles where the leaks occurred earlier.
309870370 2012-11-8 0:00: AM No Violations 2.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0157175075 US-OH-115373 2005-07-25 Well shall be plugged
1193717496 US-OH-105115 2005-07-25 Well shall be plugged
2094333585 US-OH-121382 2012-10-09 Defective casing, leaking well

For data sources see[9]

References