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| Well ID: 34-083-23995 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Knox | |
| Municipality: Butler Township | |
| Operator Name: VALLEY PETROLEUM MANAGEMENT | |
| Well Pad ID: | |
| Farm/Lease Name: MYRYAL LITTLETON | |
| License Status: Final Restoration | |
| License Date: 2016-12-12 | |
| Spud Date: 1992-09-20 | |
| Spud Drilling Contractor: CO TOOLS | |
| Final Drill Date: 1993-01-15 | |
| Well Total Depth: 3050.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.340000 | |
| Longitude: -82.220000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1992-08-03 | Issued Date 8/3/92 Expired Date 8/3/93 Acres 0030000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03050 Proposed Drill Depth 03050 |
| Original Spud | 1992-10-10 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
| Completed | 1993-01-15 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
| Reached Total Depth | 1993-01-15 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
| CO | 1993-02-01 | 231 VALLEY PETROLEUM MANAGMNT GeoDate 8/3/92 |
| Completion Report Received | 1993-03-05 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
| APP | 2016-12-12 | Proposed Formations:CLINTON, Issued Date:12/12/2016, Expired Date:12/12/2018 12:00:00 PM, Drilling unit acres:30, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2017-03-09 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
| Record Last Modified | 2017-05-01 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
| Construction Permit Expires | 2018-12-12 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 3004 | 3050 | 0 |
| 3004 | 3050 | 0 | |
| 3004 | 3050 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 76000 Gal | 20000 | FRAC W/76M GAL WATER & 20M# SAND |
For data sources see[4]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -249460812 | 2017-2-23 0:00: | PB | No Violations | 1.00 |
| -397641404 | 2017-2-22 0:00: | PB | No Violations | |
| -867149077 | 2017-1-27 0:00: | PB | No Violations | |
| 0000009770 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 8/11/93 INSPECTOR LEWIS BELL DATE 08/1119/93 DATA FROM OLD VAX INFO | |
| 0052791189 | 2017-03-15 | Production Wells | Violations Noted | This well has been plugged and satisfies the compliance notice. |
| 0249460812 | 2017-02-23 | Plug / Plug Back | No Violations | On the day of my inspection I found that R&J Well Service had their service rig moved into the location. They were not rigged up on the well yet. The rods and tubing were still in the well. I spoke with Randy Moran and he estimated that he would start the job on Monday. |
| 0397641404 | 2017-02-22 | Plug / Plug Back | No Violations | Plugging operations have began on this well. R & J Well service moved in their surface rig and rigged up to begin pulling the rods and tubing from the well. |
| 0407316114 | 2017-08-30 | Final Restoration | No Violations | This site was inspected for the final restoration completion. The area still needs some reclaiming and reseeding. I called Denny Dugan of Valley Petroleum Management and informed him of what needed to be done to complete the requirements for the final restoration to be compliant. |
| 0760097772 | 2017-09-18 | Final Restoration | No Violations | They just finished up reshaping the location back to its natural state conforming it to the lay of the land. They still have to seed it and cover it with material to stop any erosion. |
| 0867149077 | 2017-01-27 | Plug / Plug Back | No Violations | Met with Surveyor Thomas Smith to locate this well to get a final GPS reading on this well. |
| 1351131628 | 2017-03-01 | Plug / Plug Back | No Violations | On the day of my inspection I found that R&J Well Service was not plugging. No one was present at the well site. The rods and tubing had been removed from the well and transported off site. I called Randy Moran and left a message to update me on his intended schedule. |
| 1475606812 | 2016-10-04 | Production Wells | Violations Noted | This well has had the pump jack removed and lines have been disconnected and the well is incapable of production and shall be plugged in 90 days from todays date 10/4/2016. The well has no identification posted. Valley Petroleum Management shall submit a written plugging schedule to Mark McCombs at 116 East High Street Mt. Vernon Ohio 43050-3402 within 30 days, per OAC 1501:9-11-05(B)(B) Prior to commencement of plugging operations for a dry hole or lost hole, the owner, or his authorized agent, shall furnish the inspector with a record of the depth of the top and the base of formations penetrated during the drilling of the well, the depths where oil, gas or water were encountered, and a record of any casing present in the well. If reasonably available, the information furnished shall include a copy of the geophysical, electrical, or mechanical log and/ or the drilling contractors report. Based on the furnished information the inspector shall approve a plugging program in accordance with rules 1501:9-11-01 to 1501-9-11-13 of the Administrative Code and plug emplacement methods and plugging materials approved by the chief. When no records are available, the owner, or his agent, shall make every reasonable effort to obtain sufficient formation and casing data on the well, to assist the inspector in determining the plugging procedure. Exceptions may be granted at the discretion of the chief., and plug the well within 180 days. Valley Petroleum Management will be notified if the plugging schedule is approved or denied. |
| 1483988628 | 2017-01-09 | Production Wells | Violations Noted | Talked with Denny Dugan from Valley Petroleum Management to discuss when he intends to plug this well. He stated that R&J well service was moving in to plug the well and satisfy this compliance notice. |
| 1488387342 | 2017-02-27 | Plug / Plug Back | No Violations | On the day of my inspection I found that Randy Moran was rigged up on the well. He was starting to pull rods and tubing. There had not been any clay delivered to the site yet. |
| 1488570361 | 2017-03-03 | Plug / Plug Back | No Violations | On the day of my inspection Denny Dugan of Valley Petroleum delivered 20 tons of clay from Logan Clay. R&J Well Service washed 2 tons of clay down the 5.5 inch casing and went in to rip. Randy Moran got a telegraph at a depth of 2500 feet and parted the casing there. Randy pulled 20 joints and shut down for the evening. |
| 1488634663 | 2017-03-04 | Plug / Plug Back | No Violations | On the day of my inspection R&J Well Service washed another 6 tons of clay in the well, for a total of 8 tons in the bottom plug. They also started to pull the rest of the 5.5 inch casing from the well. |
| 1488989931 | 2017-03-08 | Plug / Plug Back | No Violations | On the day of my inspection Randy Moran ran in with a pre-cast cement plug to find the 7 inch seat. There were no records of 7 inch casing ever being ran when this well was drilled. Denny Dugan claimed that they did run 7 inch casing. Randy also said that the hole would have been reduced at some point below the Berea, regardless of whether 7 inch casing was used. The pre-cast set down at a depth of 994 feet. Randy set the pre-cast and then bailed the hole dry. Once the hole was bailed dry down to the pre-cast they washed clay in until they got up into the surface casing. The surface casing is cemented, and will be left in the well. Randy wanted to fill the casing with dry clay. They shoveled dry in the surface casing up to 300 feet and shut down for the night. |
| 1489072409 | 2017-03-09 | Plug / Plug Back | No Violations | On the day of my inspection R&J Drilling shoveled the rest of the clay into the well, filling the surface casing to within 5 feet of ground level. There is a total of 12 tons of clay from the pre-cast at 994 feet to surface. |
| 1489670145 | 2017-02-22 | Plug / Plug Back | No Violations | R & J Well Service Has their Service rig setting on location rigged up preparing to plug this well. |
| 1514491335 | 2017-12-28 0:00 | FR | No Violations | |
| 1844811916 | 2017-03-06 | Plug / Plug Back | No Violations | On the day of my inspection I found that the 5.5 inch casing had been pulled from the well. R&J Well Services was not present. I spoke with JR Moran, who claimed that they would not be out for at least three days to finish the job. He said that they did not do anything else after pulling the casing on Saturday. |
| 407316114 | 2017-8-30 0:00: | FR | No Violations | |
| 52791189 | 2017-3-15 0:00: | PW | No Violations | |
| 760097772 | 2017-9-18 0:00: | FR | No Violations | |
| 9770 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0052791189 | US-OH-125767 | 2017-03-20 | Failure to legibly identify well | |
| 0052791189 | US-OH-125768 | 2017-03-20 | Well shall be plugged | |
| 1475606812 | US-OH-113618 | 2017-04-10 | 9-9-05(A)10 | Failure to legibly identify well |
| 1475606812 | US-OH-113619 | 2017-04-10 | NONE | Well shall be plugged |
| 1483988628 | US-OH-113772 | 2017-04-10 | 9-9-05(A)10 | Failure to legibly identify well |
| 1483988628 | US-OH-113773 | 2017-04-10 | NONE E | Well shall be plugged |
For data sources see[9]