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| Well ID: 34-087-20438 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Lawrence | |
| Municipality: Mason Township | |
| Operator Name: PILLAR ENERGY LLC | |
| Well Pad ID: | |
| Farm/Lease Name: PAYNE PEARL V | |
| License Status: Active Injection | |
| License Date: 1992-09-29 | |
| Spud Date: 1988-08-01 | |
| Spud Drilling Contractor: GARD DRILLING | |
| Final Drill Date: 1988-08-02 | |
| Well Total Depth: 745.00 ft | |
| Configuration: Vertical | |
| Latitude: 38.630000 | |
| Longitude: -82.450000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1988-07-18 | Issued Date 7/18/88 Expired Date 7/18/89 Acres 0001000 Tool Type RTF Proposed Formation COW RUN Proposed Depth 00745 Proposed Drill Depth 00745 |
| Original Spud | 1988-08-01 | CONVERT 10-3-92 PERMIT EXPIRED. |
| Completed | 1988-08-02 | CONVERT 10-3-92 PERMIT EXPIRED. |
| Reached Total Depth | 1988-08-02 | CONVERT 10-3-92 PERMIT EXPIRED. |
| CO | 1988-08-25 | 1089 MITCHELL ENERGY CORP GeoDate 7/18/88 |
| Completion Report Received | 1988-08-25 | CONVERT 10-3-92 PERMIT EXPIRED. |
| First Injection | 1988-08-25 | CONVERT 10-3-92 PERMIT EXPIRED. |
| CO | 1992-09-29 | 1089 MITCHELL ENERGY CORP GeoDate 9/29/92 |
| Enhanced Recovery | 1992-09-29 | Issued Date 9/29/92 Expired Date 9/29/93 Acres 0001000 Tool Type RTF Proposed Formation COW RUN Proposed Depth Proposed Drill Depth |
| Annulus Pressure Monitoring Approved | 1992-11-24 | CONVERT 10-3-92 PERMIT EXPIRED. |
| Construction Permit Expires | 1993-09-29 | CONVERT 10-3-92 PERMIT EXPIRED. |
| Change of Owner | 1999-10-22 | Operator changed from 1089, MITCHELL ENERGY CORP to 3793, ENERGY SEARCH INC |
| Last Compliance Report | 2000-02-25 | CONVERT 10-3-92 PERMIT EXPIRED. |
| Change of Owner | 2008-02-26 | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC |
| Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
| Change of Owner | 2016-02-24 | Operator changed from 7578, ENERVEST OPERATING LLC to 9619, PILLAR ENERGY LLC |
| Record Last Modified | 2017-02-15 | CONVERT 10-3-92 PERMIT EXPIRED. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2000-02-25 | 627 | 649 | 1 |
| 627 | 649 | 1 | |
| 627 | 649 | 1 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 223 Bbl | 12900 | FRAC WITH 223 BBLS OF GELLED H2O AND 12,900# OF SAND |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1988 | MITCHELL ENERGY CORP | 0.00 | 630.00 | 118 |
| 1989 | MITCHELL ENERGY CORP | 0.00 | 1229.00 | 355 |
| 1990 | MITCHELL ENERGY CORP | 12.00 | 720.00 | 365 |
| 1991 | MITCHELL ENERGY CORP | 12.00 | 436.00 | 346 |
| 1992 | MITCHELL ENERGY CORP | 11.00 | 484.00 | 324 |
| 1993 | MITCHELL ENERGY CORP | 0.00 | 0.00 | 0 |
| 1994 | MITCHELL ENERGY CORP | 0.00 | 0.00 | 365 |
| 1995 | MITCHELL ENERGY CORP | 0.00 | 0.00 | 0 |
| 1997 | MITCHELL ENERGY CORP | 0.00 | 0.00 | 0 |
| 1998 | MITCHELL ENERGY CORP | 0.00 | 0.00 | 0 |
| 1999 | ENERGY SEARCH INC | 0.00 | 0.00 | 60 |
| 2000 | ENERGY SEARCH INC | 0.00 | 0.00 | 365 |
| 2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 366 |
| 2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
| 2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| 2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1988 | MITCHELL ENERGY CORP | Brine | 26 | 118 |
| 1989 | MITCHELL ENERGY CORP | Brine | 117 | 355 |
| 1990 | MITCHELL ENERGY CORP | Brine | 144 | 365 |
| 1991 | MITCHELL ENERGY CORP | Brine | 361 | 346 |
| 1992 | MITCHELL ENERGY CORP | Brine | 297 | 324 |
| 1993 | MITCHELL ENERGY CORP | Brine | 0 | 0 |
| 1994 | MITCHELL ENERGY CORP | Brine | 0 | 365 |
| 1995 | MITCHELL ENERGY CORP | Brine | 0 | 0 |
| 1997 | MITCHELL ENERGY CORP | Brine | 0 | 0 |
| 1998 | MITCHELL ENERGY CORP | Brine | ||
| 1999 | MITCHELL ENERGY CORP | Brine | ||
| 2000 | ENERGY SEARCH INC | Brine | 365 | |
| 2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
| 2009 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
| 2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
| 2011 | ENERVEST OPERATING LLC | Brine | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1030049379 | 2017-6-7 0:00:0 | SW | No Violations | |
| -1215986078 | 2015-4-6 0:00:0 | ER | No Violations | 0.50 |
| -1277553933 | 2004-11-3 0:00: | SW | No Violations | |
| -1279248998 | 2013-10-21 0:00 | ER | No Violations | 0.50 |
| -1298696730 | 2013-12-11 0:00 | SC | No Violations | 2.00 |
| -1389488328 | 2011-4-6 0:00:0 | ER | No Violations | |
| -1413591800 | 2010-12-30 0:00 | ER | No Violations | |
| -1483636873 | 2007-5-31 0:00: | ER | No Violations | |
| -149554210 | 2019-5-28 0:00: | ER | No Violations | 1.00 |
| -1555707384 | 2012-12-28 0:00 | ER | No Violations | 2.30 |
| -1596219828 | 2020-7-20 0:00: | ER | No Violations | 0.50 |
| -1616539057 | 2020-6-17 0:00: | ER | No Violations | 0.40 |
| -1655104043 | 2006-11-21 0:00 | ER | No Violations | |
| -1835946439 | 2005-9-20 0:00: | ER | No Violations | |
| -1880676247 | 2003-2-6 0:00:0 | ER | No Violations | |
| -1967215915 | 2013-1-7 0:00:0 | SC | No Violations | 2.50 |
| -1968730941 | 2007-2-23 0:00: | ER | No Violations | |
| -1991357609 | 2009-8-17 0:00: | ER | No Violations | |
| -2058698062 | 2014-2-13 0:00: | ER | No Violations | 1.50 |
| -2059284144 | 2019-10-15 0:00 | ER | No Violations | 0.40 |
| -2127062742 | 2004-3-4 0:00:0 | SW | No Violations | |
| -328405040 | 2006-3-16 0:00: | ER | No Violations | |
| -542694396 | 2004-1-28 0:00: | SW | No Violations | |
| -629316975 | 2008-1-23 0:00: | ER | No Violations | |
| -641144324 | 2014-11-10 0:00 | ER | No Violations | 0.70 |
| -684143806 | 2013-5-3 0:00:0 | ER | No Violations | 0.70 |
| -690441411 | 2010-3-8 0:00:0 | ER | No Violations | |
| -698905952 | 2010-6-7 0:00:0 | ER | No Violations | 1.00 |
| -784282316 | 2008-7-17 0:00: | ER | No Violations | |
| -806196880 | 2007-9-25 0:00: | ER | No Violations | |
| -823408389 | 2012-8-21 0:00: | ER | No Violations | |
| -857441075 | 2019-2-19 0:00: | ER | No Violations | 1.00 |
| -86061179 | 2006-5-24 0:00: | ER | No Violations | |
| -863336367 | 2004-5-20 0:00: | SW | No Violations | |
| 000PL14074 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0086061179 | 2006-05-24 | Enhanced Recovery Project | No Violations | Within limits. |
| 0108087242 | 2011-12-09 | Enhanced Recovery Project | No Violations | Accompanied Jon Scott for ERP training. Site clean, not exceeding max injection. |
| 0129550261 | 2015-10-13 | Enhanced Recovery Project | No Violations | Inspected the containment dike, tanks, unloading pad, injection pump, injection pressure, and annulus pressure. Identification posted at the well. |
| 0131237092 | 2016-08-25 | Enhanced Recovery Project | No Violations | Inspected the containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well. |
| 0185831542 | 2005-02-09 | Salt Water Injection Well | No Violations | Within limits. |
| 0205460118 | 2006-08-15 | Enhanced Recovery Project | No Violations | Within limits - lower pressure because well has been shut in for a day. Drip leaking. |
| 0323483513 | 2018-03-19 | Salt Water Injection Well | No Violations | I was on location today to check the pressures of this salt water injection well. The annulus pressure was 130 psi, the injection tubing pressure was 160 psi. No violations were noted during my inspection. |
| 0328405040 | 2006-03-16 | Enhanced Recovery Project | No Violations | Slightly over - had producer shut well in |
| 0338650887 | 2003-02-06 | Enhanced Recovery Project | Violations Noted | Injection pressure measured was 81 psi over maximum. Notified operator. |
| 0372735459 | 2004-10-28 | Salt Water Injection Well | No Violations | Within limits. |
| 0528026493 | 2010-09-13 | Enhanced Recovery Project | No Violations | Good identification. No violations observed. |
| 0542694396 | 2004-01-28 | Salt Water Injection Well | No Violations | |
| 0570319285 | 2005-11-22 | Enhanced Recovery Project | No Violations | passed. |
| 0593830489 | 2006-01-24 | Enhanced Recovery Project | No Violations | Pressures below maximum allowable; pressure on the annulus. |
| 0622016108 | 2003-06-19 | Enhanced Recovery Project | Violations Noted | The injection pressure measured was 258 psi, which exceeds the maximum allowable injection pressure of 191 psi.
On June 19, 2003, Tim Ross was informed of the violation and advised to immediately decrease the injection pressure below 191 psi. |
| 0629316975 | 2008-01-23 | Enhanced Recovery Project | No Violations | Pressure regulators made by Jordan Valves have been installed and are working great. The valves have a max. back pressure of 400psi, and a max. working pressure of 600psi. They are being set slightly below max. injection pressures. Well id missing. I told Jim Ross about it. |
| 0641144324 | 2014-11-10 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, injection pump, injection pressure and annulus pressure. Good identification on the well. |
| 0684143806 | 2013-05-03 | Enhanced Recovery Project | No Violations | Inspected the injection pressure, annulus pressure. Good identification. Access road has been graded. |
| 0687712522 | 2011-07-20 | Enhanced Recovery Project | No Violations | Hole in top joint of tubing. Francis Brothers service rig on well. Cut off tubing, then spear tubing and release packer. Pull to next collar and replace top joint of tubing. Reset packer , (at 21,000 lbs) and fill annulus with fresh water and corrosion inhibitor. Test at 315 psi for 15 minutes. Good test. |
| 0690441411 | 2010-03-08 | Enhanced Recovery Project | No Violations | Good identification. No problems observed during inspection. |
| 0698905952 | 2010-06-07 | Enhanced Recovery Project | No Violations | Well id for Exco-North Coast, Needs to have Enervest information and contact phone numbers. I have talked to Jim Ross (Enervest contractor) about this needing to be changed as soon as possible. |
| 0732277957 | 2012-04-05 | Enhanced Recovery Project | No Violations | No violations at the time of inspection. |
| 0733535241 | 2003-10-08 | Enhanced Recovery Project | No Violations | Well is in compliance.. |
| 0778765355 | 2008-06-12 | Enhanced Recovery Project | No Violations | No violations at this time. |
| 0779875872 | 2005-04-28 | Enhanced Recovery Project | No Violations | Passed |
| 0784282316 | 2008-07-17 | Enhanced Recovery Project | No Violations | Good Identification. No violations at this time. |
| 0806196880 | 2007-09-25 | Enhanced Recovery Project | No Violations | No violations at this time. |
| 0823408389 | 2012-08-21 | Enhanced Recovery Project | No Violations | UIC Training and well inspection. Accompanied by Morgan Button MRI 2. Injection pump is off line due to maintenance. |
| 0850745997 | 2018-09-04 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pressure and annulus pressure. Identification is posted at the well. The containment dike is free of fluids. |
| 0857441075 | 2019-02-19 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification is posted. The containment dike is free of fluids. |
| 0863336367 | 2004-05-20 | Salt Water Injection Well | No Violations | Within allowable limits. |
| 1030049379 | 2017-06-07 | Salt Water Injection Well | No Violations | Salt water injection well inspection. The annulus pressure was 63 PSI, the injection tubing pressure was 158 PSI. No violations noted. |
| 1057612158 | 2004-11-03 | Enhanced Recovery Project | No Violations | Passed. |
| 1057612158150273 | 2004-11-3 0:00: | ER | No Violations | |
| 1057612158175038 | 2004-11-3 0:00: | PW | No Violations | |
| 108087242 | 2011-12-9 0:00: | ER | No Violations | 0.30 |
| 1215986078 | 2015-04-06 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Walked injection line to well. Identification posted at the well. |
| 1258557977 | 2009-11-04 | Enhanced Recovery Project | No Violations | Good Identification. No violations were observed. |
| 1277553933 | 2004-11-03 | Salt Water Injection Well | No Violations | Random pressure check. |
| 1279248998 | 2013-10-21 | Enhanced Recovery Project | No Violations | Inspected the injection wells in this ERP field with Jon Scott. The sign for this well are in good shape. Parts of the wellhead plumbing are not wrapped in insulation. Return pipe on wellhead from pump house is spalding badly. Will need to be replaced. No leaks were detected at this time. |
| 129550261 | 2015-10-13 0:00 | ER | No Violations | 0.70 |
| 1298696730 | 2013-12-11 | Surface Facility Construction | No Violations | Inspected the changes that have been made to the pump house injection line manifolds and the change over to a different injection pump. Inspected the unloading pad, containment dike and tanks. |
| 131237092 | 2016-8-25 0:00: | ER | No Violations | 1.50 |
| 1356718842 | 2012-12-28 | Enhanced Recovery Project | No Violations | Inspected enhanced recovery well injection tubing pressure and annulus pressure. Good identification at well head. Accompanied by Morgan Button MRI 2. |
| 1363349242 | 2013-03-14 | Enhanced Recovery Project | No Violations | Jon Scott and I conducted the bimonthly inspection for this ERP field. We split up to cover more ground and try to complete this inspection in a timely manor. Wellhead identification sign is in good shape. Pipe and wellhead wrapped with silver coated insulation. |
| 1374001791 | 2013-07-15 | Enhanced Recovery Project | No Violations | Bimonthly UIC monitoring of Greasy Ridge ERP injection wells with Jon Scott. Wellhead and well identification sign are in good shape. |
| 1377578258 | 2015-06-23 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, pump house, injection pressure and annulus pressure. Good identification posted at the well. |
| 1378413664 | 2013-09-05 | Enhanced Recovery Project | No Violations | Jon Scott and I performed the bimonthly UIC inspection on the injection wells in this field. There were no leaks and the identification sign was in good shape. |
| 1389488328 | 2011-04-06 | Enhanced Recovery Project | No Violations | No violations at this time. |
| 1392328621 | 2014-02-13 | Enhanced Recovery Project | No Violations | Well injection line was shut off and the pressure regulator was replaced. |
| 1413591800 | 2010-12-30 | Enhanced Recovery Project | No Violations | Has Enervest identification. |
| 1452269491 | 2016-01-07 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well. |
| 1474026426 | 2016-03-30 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification has not been changed from Enervest to Pillar Energy. |
| 1478553869 | 2016-11-07 | Enhanced Recovery Project | Violations Noted | An inspection of the well revealed a stream of brine coming between the 1/4 inch valve for the injection pressure gauge and the injection line. A 2 inch ball valve on the injection line was closed to stop the leak. High range Quantabs were used to delineate the contaminated area. All Quantabs were maxed out (Levels over 6,215 ppm Cl) The contaminated area is 25 feet by 32 feet by 15 feet by 27 feet. The contamination originates at the wellhead and flows down slope to the access road. The brine flow was stopped by deep ruts in the access road. Doug Miller (well tender) was notified and responded to the well site. A call was made to Jeff Isner (Pillar Energy) a voice message was left for Jeff. All brine contaminated soil must be removed and taken to an EPA approved landfill for disposal. |
| 1478784892 | 2016-11-08 | Enhanced Recovery Project | No Violations | Compliance notice # 1478553869 follow up inspection. The leaking 1/4 inch nipple has been replaced. The contaminated soil was removed and placed into a plastic lined dump truck for disposal. The site was field tested with Quantabs during excavation by the UIC Inspector, Lawrence County Inspector and the South West Emergency Operations Coordinator. The site has been graded for positive drainage. Lime was applied to the location. The injection pressure and annulus pressure was recorded. |
| 1483636873 | 2007-05-31 | Enhanced Recovery Project | No Violations | No violations at this time. |
| 1528847252 | 2017-04-27 | Enhanced Recovery Project | No Violations | Inspected the containment dike, tanks, unloading pad, injection pump, injection pressure and annulus pressure. The injection pressure was 12 psi. I talked to Mike Carr about this low pressure and Mike stated that they had the injection pump off line for service and had just resumed injection operations. The containment dike was free of fluids. Identification was posted at the well. |
| 1555707384 | 2012-12-28 | Enhanced Recovery Project | No Violations | Inspected injection tubing and annulus pressures for this well with Jon Scott. Well identification sign in good shape. |
| 1565245914 | 2008-11-12 | Enhanced Recovery Project | No Violations | Good id. No problems observed. |
| 1632388829 | 2009-05-12 | Enhanced Recovery Project | No Violations | Good id. No violations were observed at time of inspection. |
| 1655104043 | 2006-11-21 | Enhanced Recovery Project | No Violations | No problems |
| 1709246078 | 2018-10-24 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well. The containment dike is free of fluids. |
| 1741303486 | 2018-05-24 | Enhanced Recovery Project | No Violations | Inspected the containment dike, tanks, injection pumps, injection pressure and annulus pressure. Identification is posted. The containment dike is free of fluids. |
| 1823772970 | 2007-04-05 | Enhanced Recovery Project | No Violations | No problems, Jim Ross has grated the lease roads. |
| 1833154932 | 2008-09-18 | Enhanced Recovery Project | No Violations | Good id. No violations at this time. |
| 1835946439 | 2005-09-20 | Enhanced Recovery Project | No Violations | OK |
| 185831542 | 2005-2-9 0:00:0 | SW | No Violations | |
| 1879171227 | 2008-03-25 | Enhanced Recovery Project | No Violations | No violations were observed. The new pressure regulator is working well. |
| 1880676247 | 2003-02-06 | Enhanced Recovery Project | Violations Noted | FOLLOW UP TO NOV # 338650887 Injection pressure measured was 81 psi over maximum. Notified operator. |
| 1899936505 | 2004-04-29 | Salt Water Injection Well | No Violations | Well is within pressure limits |
| 1964202601 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspected the containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification has not been changed from Enervest to Pillar Energy. |
| 1967215915 | 2013-01-07 | Surface Facility Construction | No Violations | Concrete dike pad has been poured. Concrete block and mortar is on site. Extended concrete apron to unloading pad. |
| 1968661993 | 2014-08-18 | Enhanced Recovery Project | No Violations | Inspected the unloading pad, containment dike, tanks, injection pump, walked the injection line, checked the injection pressure and annulus pressure. Good identification at wellhead. |
| 1968730941 | 2007-02-23 | Enhanced Recovery Project | No Violations | No problems at this time. |
| 1976772320 | 2014-06-12 | Salt Water Injection Well | No Violations | No noted violations. |
| 1991357609 | 2009-08-17 | Enhanced Recovery Project | No Violations | Good identification. No violations observed during inspection. |
| 205460118 | 2006-8-15 0:00: | ER | No Violations | |
| 2058698062 | 2014-02-13 | Enhanced Recovery Project | Violations Noted | Inspected containment dike, tanks, Pump house, injection pressure and annulus pressure. Good identification at well. Injection pressure was 220 psi. that is over the max allowable injection pressure of 191 psi. I told Jonathan Ross and he shut in the well and then checked the pressure regulator that is installed at the wellhead on the injection tubing. The regulator had frozen. Jonathan replaced the regulator. |
| 2083982403 | 2009-02-25 | Enhanced Recovery Project | No Violations | Good id. No violations observed during inspection. |
| 2127062742 | 2004-03-04 | Salt Water Injection Well | No Violations | Tested within range |
| 2133097299 | 2004-08-08 | Salt Water Injection Well | No Violations | Within specified range |
| 23469450 | 2019-9-5 0:00:0 | ER | No Violations | 1.00 |
| 323483513 | 2018-3-19 0:00: | SW | No Violations | 0.40 |
| 338650887 | 2003-2-6 0:00:0 | ER | No Violations | |
| 372735459 | 2004-10-28 0:00 | SW | No Violations | |
| 528026493 | 2010-9-13 0:00: | ER | No Violations | 0.50 |
| 570319285 | 2005-11-22 0:00 | ER | No Violations | |
| 593830489 | 2006-1-24 0:00: | ER | No Violations | |
| 622016108 | 2003-6-19 0:00: | ER | No Violations | |
| 687712522 | 2011-7-20 0:00: | ER | No Violations | |
| 732277957 | 2012-4-5 0:00:0 | ER | No Violations | 0.50 |
| 733535241 | 2003-10-8 0:00: | ER | No Violations | |
| 746427654 | 2020-1-22 0:00: | ER | No Violations | 1.00 |
| 778765355 | 2008-6-12 0:00: | ER | No Violations | |
| 779875872 | 2005-4-28 0:00: | ER | No Violations | |
| 850745997 | 2018-9-4 0:00:0 | ER | No Violations | 0.30 |
| PL14074 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0338650887 | US-OH-123538 | 2003-02-19 | Exceeding maximum allowable injection pressure | |
| 0622016108 | US-OH-127022 | 2003-06-23 | Exceeding maximum allowable injection pressure | |
| 1478553869 | US-OH-113676 | 2016-11-23 | Pollution/Contamination | |
| 1880676247 | US-OH-118880 | 2003-02-19 | Exceeding maximum allowable injection pressure | |
| 2058698062 | US-OH-120975 | 2014-02-14 | Exceeding maximum allowable injection pressure |
For data sources see[9]