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| Well ID: 34-087-20478 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Lawrence | |
| Municipality: Mason Township | |
| Operator Name: PILLAR ENERGY LLC | |
| Well Pad ID: | |
| Farm/Lease Name: HAMM J | |
| License Status: Producing | |
| License Date: 1995-11-02 | |
| Spud Date: 1995-11-20 | |
| Spud Drilling Contractor: CENTURY WELL SERVICES,INC | |
| Final Drill Date: 1995-11-23 | |
| Well Total Depth: 875.00 ft | |
| Configuration: Vertical | |
| Latitude: 38.630000 | |
| Longitude: -82.440000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1995-11-02 | Issued Date 11/2/95 Expired Date 11/1/96 Acres 0001000 Tool Type RTF Proposed Formation COW RUN Proposed Depth 00875 Proposed Drill Depth 00875 |
| Original Spud | 1995-11-20 | |
| Completed | 1995-11-23 | |
| Reached Total Depth | 1995-11-23 | |
| CO | 1996-02-10 | 1089 MITCHELL ENERGY CORP GeoDate 11/2/95 |
| Completion Report Received | 1996-02-26 | |
| Construction Permit Expires | 1996-11-01 | |
| Change of Owner | 2001-04-12 | Operator changed from 1089, MITCHELL ENERGY CORP to 3793, ENERGY SEARCH INC |
| Change of Owner | 2008-02-26 | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC |
| Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
| Change of Owner | 2016-02-24 | Operator changed from 7578, ENERVEST OPERATING LLC to 9619, PILLAR ENERGY LLC |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 770 | 781 | 0 |
| 770 | 781 | 0 | |
| 2006-09-11 | 771 | 781 | 15 |
| 771 | 781 | 15 | |
| 770 | 781 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| Not Treated | 0 | 203 Bbl | 19100 | FRAC W/203 BW & 191 SX SAND |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1995 | MITCHELL ENERGY CORP | 0.00 | 0.00 | 0 |
| 1996 | MITCHELL ENERGY CORP | 0.00 | 129.00 | 315 |
| 1997 | MITCHELL ENERGY CORP | 0.00 | 102.00 | 344 |
| 1998 | MITCHELL ENERGY CORP | 0.00 | 227.00 | 335 |
| 1999 | ENERGY SEARCH INC | 0.00 | 44.00 | 60 |
| 2000 | ENERGY SEARCH INC | 0.00 | 238.00 | 365 |
| 2001 | ENERGY SEARCH INC | 0.00 | 414.00 | 365 |
| 2002 | ENERGY SEARCH INC | 0.00 | 155.00 | 365 |
| 2003 | ENERGY SEARCH INC | 0.00 | 211.00 | 365 |
| 2004 | ENERGY SEARCH INC | 0.00 | 224.00 | 365 |
| 2005 | ENERGY SEARCH INC | 0.00 | 226.00 | 365 |
| 2006 | ENERGY SEARCH INC | 0.00 | 208.00 | 365 |
| 2007 | ENERGY SEARCH INC | 0.00 | 133.00 | 365 |
| 2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 69.00 | 366 |
| 2009 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| 2010 | ENERVEST OPERATING LLC | 0.00 | 197.00 | 365 |
| 2011 | ENERVEST OPERATING LLC | 0.00 | 257.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 0.00 | 283.00 | 366 |
| 2013 | ENERVEST OPERATING LLC | 0.00 | 282.00 | 365 |
| 2014 | ENERVEST OPERATING LLC | 0.00 | 193.00 | 365 |
| 2015 | ENERVEST OPERATING LLC | 0.00 | 190.00 | 365 |
| 2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| 2017 | PILLAR ENERGY LLC | 0.00 | 101.00 | 365 |
| 2018 | PILLAR ENERGY LLC | 0.00 | 90.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1995 | MITCHELL ENERGY CORP | Brine | 0 | 0 |
| 1996 | MITCHELL ENERGY CORP | Brine | 2764 | 315 |
| 1997 | MITCHELL ENERGY CORP | Brine | 0 | 344 |
| 1998 | MITCHELL ENERGY CORP | Brine | 2332 | 335 |
| 1999 | MITCHELL ENERGY CORP | Brine | 2074 | 299 |
| 2000 | ENERGY SEARCH INC | Brine | 365 | |
| 2001 | ENERGY SEARCH INC | Brine | 0 | 365 |
| 2002 | ENERGY SEARCH INC | Brine | 365 | |
| 2003 | ENERGY SEARCH INC | Brine | 365 | |
| 2004 | ENERGY SEARCH INC | Brine | 0 | 365 |
| 2005 | ENERGY SEARCH INC | Brine | 0 | 365 |
| 2006 | ENERGY SEARCH INC | Brine | 1679 | 365 |
| 2007 | ENERGY SEARCH INC | Brine | 1228 | 365 |
| 2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
| 2009 | EXCO - NORTH COAST ENERGY INC | Brine | 568 | 365 |
| 2010 | ENERVEST OPERATING LLC | Brine | 604 | 365 |
| 2011 | ENERVEST OPERATING LLC | Brine | 695 | |
| 2012 | ENERVEST OPERATING LLC | Brine | 1164 | 366 |
| 2013 | ENERVEST OPERATING LLC | Brine | 1162 | 365 |
| 2014 | ENERVEST OPERATING LLC | Brine | 1023 | 365 |
| 2015 | ENERVEST OPERATING LLC | Brine | 1008 | 365 |
| 2016 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
| 2017 | PILLAR ENERGY LLC | Brine | 0 | 365 |
| 2018 | PILLAR ENERGY LLC | Brine | 0 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -105132312 | 2017-6-8 0:00:0 | PW | No Violations | 4.50 |
| -123336469 | 2017-6-21 0:00: | PW | No Violations | 4.50 |
| -453574731 | 2017-6-1 0:00:0 | PW | No Violations | 7.50 |
| 0000009216 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 8/14/96 INSPECTOR MARK MCGUIRE DATE 08/1419/96 DATA FROM OLD VAX INFO | |
| 001269i499 | 2001-11-08 | Production Wells | No Violations | No violations. |
| 0105132312 | 2017-06-08 | Production Wells | No Violations | Went down and still found 3-4 pockets of oil in the small stream. Spoke with the well tender and explained that would need attention. I suggested flushing the stream again and building another siphon dam near the source of the oil coming from the bank. He said that they already discussed that and were going to do it on Monday when the field supervisor came back from vacation. I put down about 5 diapers in different spots up the stream. I also spoke with them about some straw near another dike. They said they had a small release resulting from having the lines shut down because of this spill. They said they would remediate the area of about 4x10 feet on Monday when they have the track hoe here. |
| 0123336469 | 2017-06-21 | Production Wells | No Violations | Follow up inspection found that the creek was void of pools of oil today. The lower siphon dam was still in place and functioning correctly. The upper siphon dam was washed out, however the socks placed across the creek were still in place. This upper area is where the oil came out after going subsurface. There was no visible oil today. |
| 0453574731 | 2017-06-01 | Production Wells | Violations Noted | I responded to a release of 3-4 barrels of oil as estimated by Mike Carr field supervisor for Pillar Energy. I arrived at the location and they were using a pump and their water truck to suck oil out of the creek/ditch. I assessed the situation and went to a location that had cell service to give Mr. Scott King an update of my findings. I explained that the spill was from a flow line that was buried. The oil came to surface near the origin then traveled downslope and disappeared subsurface. The oil then came out of the ground just above the creek line. The oil traveled approximately 175 yards down the stream where it pooled up in front of a concrete spillway that was a culvert that crossed St.Rt. 775. I stayed until the siphon dam was installed and operational. Once the track hoe arrived the source was fixed then the siphon dam was installed. One 40 barrel load of fresh water was flushed down the creek. |
| 1269i499 | 2001-11-8 0:00: | PW | No Violations | |
| 1500387786 | 2017-07-18 | Production Wells | No Violations | The spill has been cleaned up and site on top of hill where the oil went subsurface is starting to sprout vegetation. No oil or evidence of oil was found in the creek. |
| 1968347600 | 2017-11-15 | Production Wells | No Violations | On the day of this inspection, I found an oil and gas well equipped with 4.5 inch diameter casing, 1.5 inch diameter tubing with a pumping unit. Identification was located at the wellhead and is legible. |
| 9216 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0453574731 | US-OH-124914 | 2017-06-13 | Well operation causing pollution and contamination | |
| 0453574731 | US-OH-124915 | 2017-06-13 | Equipment pressure rated below operating pressure |
For data sources see[9]