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34-089-24138

Well Details

Well ID: 34-089-24138
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Country: United States
State: Ohio
County: Muskingum
Municipality: Hopewell Township
Operator Name: ELLEN P SHARP LLC
Well Pad ID:
Farm/Lease Name: CRUDE OIL CO
License Status: Final Restoration
License Date: 2016-06-13
Spud Date: 1981-04-22
Spud Drilling Contractor:
Final Drill Date: 1981-05-27
Well Total Depth: 3040.00 ft
Configuration: Vertical
Latitude: 40.010000
Longitude: -82.190000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-04-13 458 SHARP GEORGE W GeoDate 4/13/81
Oil and Gas 1981-04-13 Issued Date 4/13/81 Expired Date 4/13/82 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1981-04-22
Completed 1981-05-27
Reached Total Depth 1981-05-27
APP 2016-06-13 Proposed Formations:CLINTON, Issued Date:6/13/2016, Expired Date:6/13/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2016-08-29
Record Last Modified 2017-05-10
Construction Permit Expires 2018-06-13

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 3200 Bbl 28000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ELLEN P SHARP LLC 0.00 1002.00 0
1985 ELLEN P SHARP LLC 0.00 1378.00 0
1986 ELLEN P SHARP LLC 0.00 1201.00 365
1987 ELLEN P SHARP LLC 0.00 1368.00 365
1988 ELLEN P SHARP LLC 0.00 1033.00 365
1989 ELLEN P SHARP LLC 0.00 835.00 365
1992 ELLEN P SHARP LLC 0.00 309.00 365
1994 ELLEN P SHARP LLC 0.00 200.00 0
1995 ELLEN P SHARP LLC 0.00 181.00 0
1996 ELLEN P SHARP LLC 0.00 228.00 0
1997 ELLEN P SHARP LLC 0.00 218.00 0
1998 ELLEN P SHARP LLC 0.00 166.00 365
1999 ELLEN P SHARP LLC 0.00 165.00 365
2000 ELLEN P SHARP LLC 0.00 134.00 365
2001 ELLEN P SHARP LLC 0.00 0.00 0
2002 ELLEN P SHARP LLC 0.00 43.00 365
2003 ELLEN P SHARP LLC 0.00 0.00 365
2004 ELLEN P SHARP LLC 0.00 0.00 365
2005 ELLEN P SHARP LLC 0.00 0.00 365
2006 ELLEN P SHARP LLC 0.00 0.00 365
2007 ELLEN P SHARP LLC 0.00 0.00 365
2008 ELLEN P SHARP LLC 0.00 0.00 365
2009 ELLEN P SHARP LLC 0.00 0.00 365
2010 ELLEN P SHARP LLC 0.00 0.00 365
2011 ELLEN P SHARP LLC 0.00 0.00 365
2012 ELLEN P SHARP LLC 0.00 0.00 366
2013 ELLEN P SHARP LLC 0.00 0.00 365
2014 ELLEN P SHARP LLC 0.00 0.00 365
2015 ELLEN P SHARP LLC 0.00 0.00 365
2016 ELLEN P SHARP LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ELLEN P SHARP LLC Brine 0 0
1985 ELLEN P SHARP LLC Brine 60 0
1986 ELLEN P SHARP LLC Brine 0 365
1987 ELLEN P SHARP LLC Brine 0 365
1988 ELLEN P SHARP LLC Brine 0 365
1989 ELLEN P SHARP LLC Brine 0 365
1992 ELLEN P SHARP LLC Brine 0 365
1994 ELLEN P SHARP LLC Brine 0 0
1995 ELLEN P SHARP LLC Brine 0 0
1996 ELLEN P SHARP LLC Brine 0 0
1997 ELLEN P SHARP LLC Brine 0
1998 ELLEN P SHARP LLC Brine 0 365
1999 ELLEN P SHARP LLC Brine 0 365
2000 ELLEN P SHARP LLC Brine 0 365
2001 ELLEN P SHARP LLC Brine 0 0
2002 ELLEN P SHARP LLC Brine 0 365
2003 ELLEN P SHARP LLC Brine 0 365
2004 ELLEN P SHARP LLC Brine 0 365
2005 ELLEN P SHARP LLC Brine 0 365
2006 ELLEN P SHARP LLC Brine 0 365
2007 ELLEN P SHARP LLC Brine 0 365
2008 ELLEN P SHARP LLC Brine 0 365
2009 ELLEN P SHARP LLC Brine 0 365
2010 ELLEN P SHARP LLC Brine 0 365
2011 ELLEN P SHARP LLC Brine 0 365
2012 ELLEN P SHARP LLC Brine 0 366
2013 ELLEN P SHARP LLC Brine 0 365
2014 ELLEN P SHARP LLC Brine 0 365
2015 ELLEN P SHARP LLC Brine 0 365
2016 ELLEN P SHARP LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1254753729 2016-8-22 0:00: PB No Violations
-1948551787 2016-8-26 0:00: PB No Violations
000VER1154 1998-01-23 Production Wells No Violations
000VER1155 1998-01-23 Production Wells No Violations
0696056821 2017-04-20 Final Restoration No Violations This inspection was conducted as a final restoration status check. The well has been plugged and location restored. The well owner is also the landowner. The equipment was observed on the property. The inspection meets ORC 1509.072 requirements. Time of inspection: 3:00 PM.
1254753729 2016-08-22 Plug / Plug Back No Violations This inspection was conducted as a status check. Mr. Phil Moran has been contracted to plug this well. Phil Moran was running tubing in the well but could only get to approximately 2,500 feet. Phil stated that the tubing had encountered a soft obstruction. The tubing was pulled from the well. The bottom joints were observed to have a clay like substance on them. It was discussed that clay must have been previously washed on bottom without a permit or notification as 500 shovels wouldve put the top of the plug at approximately 2,500 feet. Phil was advised to rip the 4.5 diameter casing and add some clay to bottom.
1948551787 2016-08-26 Plug / Plug Back No Violations This inspection was conducted as a status check. No activity during inspection. The 8 casing has been recovered. Phil Moran has begun washing clay in to surface. Top of clay was not to surface as of this inspection. Time of inspection: 10:45 AM.
2051108755 2016-08-24 Plug / Plug Back No Violations I witnessed plugging operations accompanied by Central Office geologist Matt Erenpreiss. Refer to plug report for details. Time of inspection: 2:45 PM.
696056821 2017-4-20 0:00: FR No Violations 0.50
VER1154 1998-1-23 0:00: PW No Violations
VER1155 1998-1-23 0:00: PW No Violations

For data sources see[8]

References