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34-089-24314

Well Details

Well ID: 34-089-24314
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Country: United States
State: Ohio
County: Licking
Municipality: Hopewell Township
Operator Name: MACKENCO INC
Well Pad ID:
Farm/Lease Name: MCCOY
License Status: Final Restoration
License Date: 2006-05-04
Spud Date: 1981-11-09
Spud Drilling Contractor:
Final Drill Date: 1982-01-26
Well Total Depth: 3000.00 ft
Configuration: Vertical
Latitude: 39.990000
Longitude: -82.280000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-10-22 1637 MACKENCO INC GeoDate 10/22/81
Original Spud 1981-11-09
Completed 1982-01-26
Reached Total Depth 1982-01-26
APP 2004-06-02 Proposed Formations:CLINTON, Issued Date:6/2/2004, Expired Date:6/2/2005 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2006-05-04 Proposed Formations:CLINTON, Issued Date:5/4/2006, Expired Date:5/4/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2006-08-17
Construction Permit Expires 2007-05-04
Record Last Modified 2013-03-14

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 57500 Gal 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 LANGASCO ENERGY CORP 377.00 99.00 275
1986 LANGASCO ENERGY CORP 613.00 63.00 365
1987 LANGASCO ENERGY CORP 1139.00 105.00 365
1990 MACKENCO INC 1366.00 62.00 365
1991 MACKENCO INC 1172.00 66.00 365
1992 MACKENCO INC 1357.00 0.00 365
1993 MACKENCO INC 1068.00 73.00 365
1994 MACKENCO INC 1172.00 68.00 365
1995 MACKENCO INC 1013.00 0.00 365
1996 MACKENCO INC 1089.00 62.00 365
1997 MACKENCO INC 1367.00 115.00 365
1998 MACKENCO INC 1243.00 0.00 365
1999 MACKENCO INC 1227.00 76.00 365
2000 MACKENCO INC 1068.00 0.00 365
2001 MACKENCO INC 1053.00 40.00 365
2002 MACKENCO INC 1514.00 54.00 365
2003 MACKENCO INC 999.00 27.00 365
2004 MACKENCO INC 896.00 0.00 365
2005 MACKENCO INC 653.00 26.00 365
2006 MACKENCO INC 444.00 0.00 270
2007 MACKENCO INC 0.00 0.00 270
2009 MACKENCO INC 0.00 0.00 365
2011 MACKENCO INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 LANGASCO ENERGY CORP Brine 37 275
1986 LANGASCO ENERGY CORP Brine 0 365
1987 LANGASCO ENERGY CORP Brine 70 365
1990 MACKENCO INC Brine 190 365
1991 MACKENCO INC Brine 280 365
1992 MACKENCO INC Brine 0 365
1993 MACKENCO INC Brine 210 365
1994 MACKENCO INC Brine 355 365
1995 MACKENCO INC Brine 200 365
1996 MACKENCO INC Brine 225 365
1997 MACKENCO INC Brine 75 365
1998 MACKENCO INC Brine 220 365
1999 MACKENCO INC Brine 80 365
2000 MACKENCO INC Brine 75 365
2001 MACKENCO INC Brine 70 365
2002 MACKENCO INC Brine 100 365
2003 MACKENCO INC Brine 210 365
2004 MACKENCO INC Brine 210 365
2005 MACKENCO INC Brine 320 365
2006 MACKENCO INC Brine 145 270
2007 MACKENCO INC Brine 0 270
2009 MACKENCO INC Brine 6 365
2011 MACKENCO INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1256616542 2013-11-13 0:00 AM No Violations
-785744874 2006-8-9 0:00:0 PB No Violations
0785744874 2006-08-09 Plug / Plug Back No Violations Met on site with Mackenco owner along with Mike Wheeler and Wes Drake of OEPA to review complaint area re: oil on ground. Rods had been steamed into unlined pit and paraffin with small amount of oil was in the pit with water. Advised Mackenco to pump out pit and to have lined pit prepared if additional fluids are expected to be encountered during plugging. No oil was noted in trees as reported.n No violation issued as pit at the time appeared to be liquid tight.
1033089979 2014-07-16 Administrative Inspection No Violations With Brandon Mitchell. Review plugged well site, and records on water well Investigation. See Brandons report this date for details,.
1155823506 2006-08-17 Plug / Plug Back No Violations 4 inch and portion of 8 inch pipe has been removed. Mike Wheeler indicated that 8 inch pulled apart. He will be getting additional clay on site to finish plugging top of hole and then will grade and reclaim area with dozer. Told Mike to submit plugging report affidavit on phone message.
1256616542 2013-11-13 Administrative Inspection No Violations Inspect location utilizing coordinates in RBDMS in regards to a water well complaint. No leaks at the surface.
1749779294 2007-04-11 Final Restoration No Violations Inspection revealed that all pits have been closed and the area has been properly graded. Vegetation has begun to grow on the old well location which is located in a wooded area.

For data sources see[8]

References