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34-089-24865

Well Details

Well ID: 34-089-24865
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Country: United States
State: Ohio
County: Licking
Municipality: Mary Ann Township
Operator Name: ROYALTY ENTERPRISES INC
Well Pad ID:
Farm/Lease Name: KIRKBRIDGE RUSSELL & ELEANOR
License Status: Producing
License Date: 1984-08-01
Spud Date: 1984-08-02
Spud Drilling Contractor: R & J DRILLING
Final Drill Date: 1984-08-27
Well Total Depth: 2874.00 ft
Configuration: Vertical
Latitude: 40.150000
Longitude: -82.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-11-29 Issued Date 11/29/83 Expired Date 5/27/84 Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-08-01 604 ASHCRAFT PETROLEUM INC GeoDate 8/1/84
Oil and Gas 1984-08-01 Issued Date 8/1/84 Expired Date 1/28/85 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02874 Proposed Drill Depth 02874
Original Spud 1984-08-02 R.I. 8-4-84 FDT=RED ROCK
Completed 1984-08-27 R.I. 8-4-84 FDT=RED ROCK
Reached Total Depth 1984-08-27 R.I. 8-4-84 FDT=RED ROCK
CO 1984-09-03 1274 FORTUNE PETROLEUM CORP GeoDate 11/29/83
Completion Report Received 1984-10-26 R.I. 8-4-84 FDT=RED ROCK
Construction Permit Expires 1985-01-28 R.I. 8-4-84 FDT=RED ROCK
Change of Owner 2015-11-25 Operator changed from 604, AP PRODUCTION LLC to 4484, ROYALTY ENTERPRISES INC
Record Last Modified 2017-02-15 R.I. 8-4-84 FDT=RED ROCK

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2824 2852 0
2824 2852 0
2824 2852 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2700 Bbl 60000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 AP PRODUCTION LLC 5106.00 0.00 365
1987 AP PRODUCTION LLC 5951.00 76.00 365
1988 AP PRODUCTION LLC 5551.00 53.00 365
1989 AP PRODUCTION LLC 4810.00 0.00 365
1990 AP PRODUCTION LLC 3720.00 0.00 365
1991 AP PRODUCTION LLC 2720.00 0.00 365
1992 AP PRODUCTION LLC 2678.00 48.00 365
1993 AP PRODUCTION LLC 1822.00 0.00 365
1994 AP PRODUCTION LLC 1838.00 0.00 365
1995 AP PRODUCTION LLC 1620.00 0.00 365
1996 AP PRODUCTION LLC 755.00 0.00 365
1997 AP PRODUCTION LLC 507.00 0.00 365
1998 AP PRODUCTION LLC 937.00 0.00 365
1999 AP PRODUCTION LLC 343.00 0.00 365
2000 AP PRODUCTION LLC 0.00 0.00 365
2001 AP PRODUCTION LLC 0.00 0.00 365
2002 AP PRODUCTION LLC 0.00 0.00 365
2003 AP PRODUCTION LLC 0.00 0.00 365
2004 AP PRODUCTION LLC 0.00 0.00 365
2005 AP PRODUCTION LLC 0.00 0.00 365
2006 AP PRODUCTION LLC 0.00 0.00 365
2007 AP PRODUCTION LLC 0.00 0.00 365
2008 AP PRODUCTION LLC 0.00 0.00 365
2009 AP PRODUCTION LLC 0.00 0.00 365
2010 AP PRODUCTION LLC 0.00 0.00 365
2011 AP PRODUCTION LLC 0.00 0.00 365
2012 AP PRODUCTION LLC 0.00 0.00 366
2013 AP PRODUCTION LLC 0.00 0.00 365
2014 AP PRODUCTION LLC 0.00 0.00 365
2015 ROYALTY ENTERPRISES INC 0.00 0.00 0
2016 ROYALTY ENTERPRISES INC 0.00 0.00 0
2017 ROYALTY ENTERPRISES INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 AP PRODUCTION LLC Brine 0 365
1987 AP PRODUCTION LLC Brine 0 365
1988 AP PRODUCTION LLC Brine 0 365
1989 AP PRODUCTION LLC Brine 0 365
1990 AP PRODUCTION LLC Brine 0 365
1991 AP PRODUCTION LLC Brine 0 365
1992 AP PRODUCTION LLC Brine 0 365
1993 AP PRODUCTION LLC Brine 0 365
1994 AP PRODUCTION LLC Brine 0 365
1995 AP PRODUCTION LLC Brine 0 365
1996 AP PRODUCTION LLC Brine 0 365
1997 AP PRODUCTION LLC Brine 0 365
1998 AP PRODUCTION LLC Brine 0 365
1999 AP PRODUCTION LLC Brine 0 365
2000 AP PRODUCTION LLC Brine 0 365
2001 AP PRODUCTION LLC Brine 0 365
2002 AP PRODUCTION LLC Brine 0 365
2003 AP PRODUCTION LLC Brine 0 365
2004 AP PRODUCTION LLC Brine 0 365
2005 AP PRODUCTION LLC Brine 0 365
2006 AP PRODUCTION LLC Brine 0 365
2007 AP PRODUCTION LLC Brine 0 365
2008 AP PRODUCTION LLC Brine 0 365
2009 AP PRODUCTION LLC Brine 0 365
2010 AP PRODUCTION LLC Brine 0 365
2011 AP PRODUCTION LLC Brine 0 365
2012 AP PRODUCTION LLC Brine 0 366
2013 AP PRODUCTION LLC Brine 0 365
2014 AP PRODUCTION LLC Brine 0 365
2015 ROYALTY ENTERPRISES INC Brine 0 0
2016 ROYALTY ENTERPRISES INC Brine 0 0
2017 ROYALTY ENTERPRISES INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1351358736 2019-9-9 0:00:0 PW No Violations 1.00
-1720213471 2017-11-9 0:00: PW No Violations 0.50
-1883261234 2018-5-22 0:00: PW No Violations 0.50
-1991911813 2018-9-17 0:00: PW No Violations 0.50
-838239905 2018-7-5 0:00:0 PW No Violations 0.50
000PL13732 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
000VER1111 1996-11-19 Production Wells No Violations
0838239905 2018-07-05 Production Wells No Violations My inspection revealed that the tank has not been moved and the oil contamination inside the dike has not been cleaned up. I called the well owner Clayton King at 11:37 AM and discussed the well with him. I advised Mr. King to have the tank moved and the oil contamination cleaned up by 7/13/2018. Mr. King said he would try to have it done by then. Time of inspection: 10:55 AM. Weather: 89 degrees F, Partly cloudy
1513090284 2017-12-12 Production Wells No Violations My inspection revealed that the well owner did not bring the well into compliance by the date advised. Identification was not posted, oil was not removed from the dike, and the tank has not been moved at least 50 feet from the well. I called well owner Clayton King after the inspection and advised him that he needs to work on the compliance issues. Mr. King said he would get the identification posted and oil cleaned up this week. Mr. King will move the tank when he is able to bring in his backhoe. Mr. King said he would call me when these things are completed. Time of inspection: 9:15 AM. Weather: 28*F, Snowing
1550598681 2019-02-19 Production Wells No Violations My inspection revealed that the tank has not been moved and the oil contamination has not been cleaned up. I contacted Clayton King at 12:52 PM and advised him that the well is not in compliance. Mr. King said he still has not been able to access the well as he is locked out. Mr. King said he will work on getting a key within the next two days. Time of inspection: 10:00 AM.
1550819463 2018-03-23 Production Wells No Violations My inspection revealed that identification has been posted on a tank at the well. The tank has not been moved at least 50 feet from the well and oil has not been removed from the dike of the tank battery. The well owner can not access the well with a vehicle currently as the property is fenced and locked. Mr. Clayton King has attempted to contact the landowner to gain access to the well but has been unsuccessful. Time of inspection: 9:30 AM. Weather: 32 degrees F, Sunny
1720213471 2017-11-09 Production Wells Violations Noted This inspection was conducted as a Chiefs Order follow-up in regards to Chiefs Order 2016-177. The inspection revealed that the well is not capable of production as there was no pumping unit on the well. A 100 barrel tank was observed within 50 feet of the well. The tank battery consists of (2) 100 barrel tanks and a separator inside an earthen dike. Oil contamination was observed within the dike. Identification was not oberved at the well or tanks. Royalty Enterprises Inc. has reported (0) barrels of oil and (0) mcf of gas for 2015 and 2016. Photos were taken of the well and tank battery. The well owner will need to complete the following tasks within the specified time frames in order to bring well into compliance: 1) Remove oil contamination inside the dike within 5 days. 2) Post identification at the well or tank battery within 10 days. 3) Move the 100 barrel tank further than 50 feet from the well within 15 days. Time of inspection: 1:00 PM. Weather: 52*F, Sunny
1883261234 2018-05-22 Production Wells No Violations I conducted a compliance notice follow-up today on this well. The tank has not been moved at least 50 feet from the well and oil contamination has not been removed from the dike of the tank battery. I contacted well owner Clayton King regarding the inspection. Mr. King said he recently was able to contact the person that can provide him access to the well. Currently the well can not be accessed with a vehicle as the property is fenced and locked. I advised Mr. King to have the tank moved and oil contamination removed within a month. Time of inspection: 9:40 AM. Weather: 69 degrees F, Overcast
1991911813 2018-09-17 Production Wells No Violations My inspection revealed that the well location was not in compliance. The tank has not been moved at least 50 feet from the well and the oil contamination has not been cleaned up. I contacted Clayton King at 1:35 PM and advised him to work on bringing well into compliance. Time of inspection: 12:45 PM. Weather: 73 degrees F, Overcast
911949437 2020-4-9 0:00:0 PW No Violations 1.00
PL13732 PL No Violations
VER1111 1996-11-19 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1720213471 US-OH-117064 2017-11-21 9-1-07 Well operation causing pollution and contamination
1720213471 US-OH-117065 2017-11-21 9-9-05(A)10 Failure to legibly identify well
1720213471 US-OH-117066 2017-11-21 9-9-05(A)2 Violation of tank spacing requirements

For data sources see[9]

References