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34-089-62853

Well Details

Well ID: 34-089-62853
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Country: United States
State: Ohio
County: Licking
Municipality: Perry Township
Operator Name: H & A DRILLING
Well Pad ID:
Farm/Lease Name: STEVENS BERNARD & JANE
License Status: Producing
License Date: 1989-03-03
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 40.150000
Longitude: -82.210000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 677 WALLICK PETROLEUM CO
Oil and Gas 1802-01-01
Change of Owner 2014-05-02 Operator changed from 677, WALLICK PETROLEUM CO to 448, H & A DRILLING CARL W BEVARD
Record Last Modified 2014-05-02 NEW ASSIGNED PERMIT NUMBER = 62853

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1998 PORTERFIELD NELSON BUD 0.00 0.00 0
1999 PORTERFIELD NELSON BUD 0.00 0.00 0
2000 PORTERFIELD NELSON BUD 0.00 0.00 0
2001 PORTERFIELD NELSON BUD 0.00 0.00 0
2002 PORTERFIELD NELSON BUD 0.00 0.00 0
2003 PORTERFIELD NELSON BUD 0.00 0.00 0
2004 PORTERFIELD NELSON BUD 0.00 0.00 0
2005 PORTERFIELD NELSON BUD 0.00 0.00 0
2006 PORTERFIELD NELSON BUD 0.00 0.00 0
2007 PORTERFIELD NELSON BUD 0.00 0.00 0
2008 PORTERFIELD NELSON BUD 0.00 0.00 0
2009 PORTERFIELD NELSON BUD 0.00 0.00 0
2010 PORTERFIELD NELSON BUD 0.00 0.00 0
2011 PORTERFIELD NELSON BUD 0.00 0.00 0
2013 H & A DRILLING 0.00 0.00 0
2014 H & A DRILLING 0.00 0.00 0
2015 H & A DRILLING 0.00 0.00 0
2016 H & A DRILLING 0.00 0.00 0
2017 H & A DRILLING 0.00 0.00 0
2018 H & A DRILLING 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1998 PORTERFIELD NELSON BUD Brine 0 0
1999 PORTERFIELD NELSON BUD Brine 0 0
2000 PORTERFIELD NELSON BUD Brine 0 0
2001 PORTERFIELD NELSON BUD Brine 0 0
2002 PORTERFIELD NELSON BUD Brine 0 0
2003 PORTERFIELD NELSON BUD Brine 0 0
2004 PORTERFIELD NELSON BUD Brine 0 0
2005 PORTERFIELD NELSON BUD Brine 0 0
2006 PORTERFIELD NELSON BUD Brine 0 0
2007 PORTERFIELD NELSON BUD Brine 0 0
2008 PORTERFIELD NELSON BUD Brine 0 0
2009 PORTERFIELD NELSON BUD Brine 0 0
2010 PORTERFIELD NELSON BUD Brine 0 0
2011 PORTERFIELD NELSON BUD Brine 0 0
2013 H & A DRILLING Brine 0 0
2014 H & A DRILLING Brine 0 0
2015 H & A DRILLING Brine 0 0
2016 H & A DRILLING Brine 0 0
2017 H & A DRILLING Brine 0 0
2018 H & A DRILLING Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1278671993 2012-4-5 0:00:0 PW No Violations
-1317957240 2019-1-17 0:00: PW No Violations 0.10
-1400819490 2016-4-5 0:00:0 PW No Violations
-140213164 2012-4-9 0:00:0 AM No Violations
-1916400566 2018-6-12 0:00: PW No Violations 0.20
-1980142818 2016-6-21 0:00: AM No Violations
-1994541562 2017-11-2 0:00: PW No Violations 0.50
-2010619809 2019-10-1 0:00: PW No Violations 0.10
-2512762 2016-6-6 0:00:0 AM No Violations
-283326552 2020-8-24 0:00: PW No Violations 0.20
-5367175 2018-10-24 0:00 PW No Violations 0.10
-823964661 2018-2-12 0:00: PW No Violations 0.30
-86651393 2018-4-12 0:00: PW No Violations 0.30
-888712335 2016-4-5 0:00:0 PW No Violations
0002512762 2016-06-06 Administrative Inspection No Violations I spoke with Cheri Bevard at 10:32 AM regarding the compliance notice that was issued on 4/14/2016. The Division has not received a plugging schedule from H & A Drilling/Carl W. Bevard as of 6/6/2016. Mrs. Bevard said that she would get a plugging schedule to me by the end of the week.
0005367175 2018-10-24 Production Wells No Violations My inspection revealed that no attempt has been made to bring well into compliance. It was not capable of production as there was no pumping unit on the well. I issued a compliance notice on 4/14/2016 to have the well plugged. A request for enforcement action was submitted to DOGRM management in September of 2018. I two photos of the well during this inspection. I placed a phone call to Mr. Carl Bevard at 1:40 PM but did not get an answer. Mr. Bevards voicemail box was full and I could not leave a message. Time of inspection: 12:47 PM.
0026674191 2002-02-26 Production Wells No Violations WEATHER CONDITIONS: Cloudy with snow furies and 33 degrees. CHIEFS ORDERS 93-304 & 305. Accompanied by Mr. Porterfield. Inspection revealed the well is capable of production. No ID.
0086651393 2018-04-12 Production Wells No Violations I conducted a compliance notice follow-up on this well today. My inspection revealed that the well has not been plugged or placed into production. It was not capable of production as there was no pumping unit on the well. I issued a compliance notice on 4/14/2016 to have the well plugged. The well was also in violation for failure to identify well and failure to report production. Mr. Bevard has posted identification and reported production since the compliance notice was issued. I placed a phone call to Mr. Bevard at 4:00 PM. I did not get an answer and could not leave a message as his voicemail box was full. I left a voicemail message with Mr. Bevards father Albert Bevard to have his son call me. I took one photo of the well. Time of inspection: 12:54 PM. Weather: 70 degrees F, Sunny
0140213164 2012-04-09 Administrative Inspection No Violations At 8:54 AM, I called Mr. Bud Porterfield to discuss landowner complaint and status of well(s). Mr. Porterfield confirmed non-production for several years and has focused his attention on wells in Kentucky. He mentioned non-related wells and not on Stevens property, in which he let a guy have these wells and called him a year ago and nothing was done. Informed that wells still remain under his name and when asked if there would be an assignment he stated at Licking Co. Recorders office he stated that attorney took care of transfer and was not sure. Mr. Porterfield stated that he talked to 3-4 people about wells on Stevens property and will talk with his attorney today. Informed Mr. Porterfield of SB 165, a recent change to Ohio oil and gas law and asked for cooperation. Mr. Porterfield agreed to work with the Division to achieve compliance and will talk with attorney today. At 3:28 PM, I had a missed call from Mr. Porterfield. I returned his call and answered questions about well ownership transfer and provided Erica Freemans contact number at Central Office. Mr. Porterfield spoke with attorney and would like to sell all wells on Stevens property to a company; and will also work on transfer of wells on non-related property. The wells listed under Wallick Petroleum and Unknown Owner, on Stevens property, were also brought to his attention, in which he confirmed ownership. Central Office will be notified of ownership status.
0217438980 2017-07-24 Production Wells No Violations Inspect well as a compliance notice follow-up. The inspection revealed that the well has not been plugged or placed in production. The well was not capable of production at the time of inspection. Time of inspection: 1:44 PM. Weather: 79*F, Partly cloudy
0823964661 2018-02-12 Production Wells No Violations I conducted a compliance notice follow-up on this well today. My inspection revealed that the well has not been plugged or placed into production. It was not capable of production as there was no pumping unit on the well. I issued a compliance notice on 4/14/2016 to have the well plugged. The well was also in violation for failure to identify well and failure to report production. Mr. Bevard has posted identification and reported production since the compliance notice was issued. I placed a phone call to Mr. Bevard at 2:38 PM and spoke to him about bringing the well into compliance. Mr. Bevard said he needs to put his rig on the well to evaluate if it needs plugged or not. I took one photo of the well. Time of inspection: 11:35 AM. Weather: 29*F, Sunny
0888712335 2016-04-05 Production Wells Violations Noted This inspection was conducted as a production well status check. The inspection revealed a pumping unit and motor at the well but was not connected to the well due to a broken bridle cable. Identification was not posted at the well. The well did not show signs of recent production. H & A Drilling has failed to report production for 2014 and reported zero barrels of oil and zero MCF of gas for 2013. The landowner, Mr. Brad Stevens, filed a complaint with the Division regarding nonproduction of the wells on this lease in 2012. The well owner has changed since the complaint was filed and the new owner has failed to bring well into compliance. The well owner/operator shall submit a written plugging schedule to Brandon Mitchell at 5880 Memory Road Zanesville, Ohio 43701-9553 within 30 days, per ORC 1509.12(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. Time of inspection: 2:00 PM. Weather: 40*F, Sunny
1106555912 2017-03-21 Production Wells No Violations Inspect well as a compliance notice follow-up. The inspection revealed that the well has not been plugged or placed in production. The well was not capable of production at the time of inspection. Mr. Bevard has brought five of the 16 wells on this lease into compliance and is working on bringing the remainder of the wells into compliance. Time of inspection: 1:18 PM. Weather: 54*F, Sunny
1176121573 2019-03-19 Production Wells No Violations My inspection revealed that no attempt has been made to bring well into compliance. It was not capable of production as there was no pumping unit on the well. I issued a compliance notice on 4/14/2016 to have the well plugged. I took one photo of the well during this inspection. I placed a phone call to Mr. Carl Bevard at 1:05 PM but did not get an answer. Mr. Bevards voicemail was full and I could not leave a message. Time of inspection: 9:36 AM. Weather: 23 degrees F, Mostly sunny
1278671993 2012-04-05 Production Wells Violations Noted The Division received a landowner complaint alleging all Berea wells owned by Bud Porterfield have been idle for approximately 12 years. An inspection revealed an idle well with a pumping unit,motor, but with no belts or electric. This well does not provide house gasl. The polish rod showed no signs of production and flowline from pumping tee was not connected to the tank battery. Note: Tank battery consisting of (3) 100 bbl tanks are located opposite side of road on SR 586. A GPS reading obtained for the well. No identification observed at well or tank battery. At time of inspection, this well was listed under previous well owner, Wallick Petroleum Co., and not transferred to Bud Porterfield. Mr. Porterfield confirmed well ownership and the landowner has also stated that he owns the well. Mr. Porterfield will need to complete Form 7A for well ownership per Central Office. Records show no reported production. On 4/9/2012, at 8:54 AM, Mr. Porterfield was verbally informed of complaint and status of well(s) and instructed to plug or produce. Furthermore, additional wells would need to be inspected to cover all wells on Stevens property. Mr. Porterfield stated that he sold wells 2-3 years ago on non-related property to a guy and called 1 year ago and nothing done; and no assignment at Licking Co. Recorders Office; Spoke with 3-4 people about wells on Stevens property; and would talk with his attorney today.
1317957240 2019-01-17 Production Wells No Violations My inspection revealed that no attempt has been made to bring well into compliance. It was not capable of production as there was no pumping unit on the well. I issued a compliance notice on 4/14/2016 to have the well plugged. A request for enforcement action was submitted to DOGRM management in September of 2018. I took one photo of the well during this inspection. I placed a phone call to Mr. Carl Bevard at 12:41 PM and discussed his plans for the wells on the lease. Time of inspection: 10:42 AM. Weather: 31 degrees F, Overcast
1347579790 2020-2-11 0:00: PW No Violations 0.10
1400819490 2016-04-05 Production Wells No Violations This inspection was conducted as a compliance notice follow-up. The well status has not changed since previous inspection. On 5/2/2014 Nelson Bud Porterfield sold the wells on this lease to Owner#448 H & A Drilling/Carl W. Bevard. This inspection will void the compliance notice issued to Mr. Porterfield and a new compliance notice will be issued to H & A Drilling/Carl W. Bevard.
1551170731 2012-04-05 Production Wells No Violations FOLLOW UP TO NOV # -1278671993 The Division received a landowner complaint alleging all Berea wells owned by Bud Porterfield have been idle for approximately 12 years. An inspection revealed an idle well with a pumping unit,motor, but with no belts or electric. This well does not provide house gasl. The polish rod showed no signs of production and flowline from pumping tee was not connected to the tank battery. Note: Tank battery consisting of (3) 100 bbl tanks are located opposite side of road on SR 586. A GPS reading obtained for the well. No identification observed at well or tank battery. At time of inspection, this well was listed under previous well owner, Wallick Petroleum Co., and not transferred to Bud Porterfield. Mr. Porterfield confirmed well ownership and the landowner has also stated that he owns the well. Mr. Porterfield will need to complete Form 7A for well ownership per Central Office. Records show no reported production. On 4/9/2012, at 8:54 AM, Mr. Porterfield was verbally informed of complaint and status of well(s) and instructed to plug or produce. Furthermore, additional wells would need to be inspected to cover all wells on Stevens property. Mr. Porterfield stated that he sold wells 2-3 years ago on non-related property to a guy and called 1 year ago and nothing done; and no assignment at Licking Co. Recorders Office; Spoke with 3-4 people about wells on Stevens property; and would talk with his attorney today.
1916400566 2018-06-12 Production Wells No Violations My inspection revealed that the well has not been plugged or placed into production. It was not capable of production as there was no pumping unit on the well. I issued a compliance notice on 4/14/2016 to have the well plugged. I took one photo of the well. I left a voicemail message for Carl Bevard at 11:55 AM. I received a phone call from Cheri Bevard at 12:04 PM. Cheri asked what Carl Bevard needs to do to be in compliance. I told Cheri that he needs to plug or produce the wells that are still idle and that if no changes are made within 2 months I am going to refer these wells to the enforcement section. Time of inspection: 10:01 AM. Weather: 65 degrees F, Overcast
1980142818 2016-06-21 Administrative Inspection No Violations A written plugging schedule has been received and approved from Mr. Carl W. Bevard. The plugging schedule states that all wells on the Stevens lease will be either in production or plugged by 10/10/2016.
1994541562 2017-11-02 Production Wells No Violations This inspection was conducted as a follow-up. The well has not been plugged and was not capable of production. The inspection revealed the well is not in compliance. (2) photos were taken of the well. A voicemail message was left for the well owner Mr. Carl Bevard. Time of inspection: 1:40 PM.
217438980 2017-7-24 0:00: PW No Violations 0.50
26674191 2002-2-26 0:00: PW No Violations
402462761 2020-4-6 0:00:0 PW No Violations 0.30

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0888712335 US-OH-130130 2016-04-18 Failure to legibly identify well
0888712335 US-OH-130131 2016-04-18 Well shall be plugged
0888712335 US-OH-130132 2016-04-18 Statement of annual production not filed
1278671993 US-OH-107742 2012-04-28 Well shall be plugged
1278671993 US-OH-107743 2012-04-28 Statement of annual production not filed

For data sources see[7]

References