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34-099-20897

Well Details

Well ID: 34-099-20897
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Country: United States
State: Ohio
County: Mahoning
Municipality: Austintown Township
Operator Name: STK INVESTMENTS LLC
Well Pad ID:
Farm/Lease Name: SCHNURRENBERGER
License Status: Producing
License Date: 2017-06-02
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1995-03-15
Well Total Depth: 5324.00 ft
Configuration: Vertical
Latitude: 41.080000
Longitude: -80.760000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-09-12 1388 NORTH COAST ENERGY INC GeoDate 9/12/77
Completed 1977-12-06 RI 9-14-77 LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE.
Completion Report Received 1978-03-14 RI 9-14-77 LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE.
CO 1995-02-14 1388 NORTH COAST ENERGY INC GeoDate 2/14/95
Unknown 1995-02-14 Issued Date 2/14/95 Expired Date 2/14/96 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Plugged Back 1995-03-15 RI 9-14-77 LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE.
Reached Total Depth 1995-03-15 RI 9-14-77 LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE.
CO 1995-05-30 1388 NORTH COAST ENERGY INC GeoDate 5/30/95
Oil and Gas 1995-05-30 Issued Date 5/30/95 Expired Date 5/29/96 Acres 0075730 Tool Type NT Proposed Formation NEWBERG Proposed Depth 00000 Proposed Drill Depth 00000
Change of Owner 2004-03-03 Operator changed from 1388, NORTH COAST ENERGY INC to 6805, GAS ACQUISITION COMPANY LTD
APP 2004-06-02 Proposed Formations:NEWBURG, Issued Date:6/2/2004, Expired Date:6/2/2005 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2008-05-30 Proposed Formations:NEWBURG, Issued Date:5/30/2008, Expired Date:5/30/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2011-11-22 Operator changed from 6805, GAS ACQUISITION COMPANY LTD to 8863, STK INVESTMENTS LLC
APP 2012-12-13 Proposed Formations:CLINTON, Issued Date:12/13/2012, Expired Date:12/13/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2017-06-02 Proposed Formations:CLINTON, Issued Date:6/2/2017, Expired Date:6/2/2019 12:00:00 PM, Drilling unit acres:55.8, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2017-06-29 RI 9-14-77 LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE.
Construction Permit Expires 2019-06-02 RI 9-14-77 LOCATION UPDATED PER SURVEYOR COORDINATES 06/29/17 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5175 5235 30
5175 5235 30
5175 5235 30

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 820 Bbl 60000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 EXCO - NORTH COAST ENERGY INC 4885.00 0.00 0
1985 EXCO - NORTH COAST ENERGY INC 2284.00 0.00 365
1986 EXCO - NORTH COAST ENERGY INC 311.00 0.00 365
1987 EXCO - NORTH COAST ENERGY INC 1782.00 0.00 365
1988 EXCO - NORTH COAST ENERGY INC 697.00 0.00 60
1989 EXCO - NORTH COAST ENERGY INC 537.00 0.00 365
1990 EXCO - NORTH COAST ENERGY INC 112.00 0.00 365
1991 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
1992 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
1993 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2009 GAS ACQUISITION COMPANY LTD 0.00 0.00 0
2012 STK INVESTMENTS LLC 0.00 0.00 0
2014 STK INVESTMENTS LLC 0.00 0.00 0
2015 STK INVESTMENTS LLC 0.00 0.00 0
2017 STK INVESTMENTS LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 EXCO - NORTH COAST ENERGY INC Brine 20 0
1985 EXCO - NORTH COAST ENERGY INC Brine 0 365
1986 EXCO - NORTH COAST ENERGY INC Brine 0 365
1987 EXCO - NORTH COAST ENERGY INC Brine 0 365
1988 EXCO - NORTH COAST ENERGY INC Brine 0 60
1989 EXCO - NORTH COAST ENERGY INC Brine 0 365
1990 EXCO - NORTH COAST ENERGY INC Brine 0 365
1991 EXCO - NORTH COAST ENERGY INC Brine 0 365
1992 EXCO - NORTH COAST ENERGY INC Brine 65 365
1993 EXCO - NORTH COAST ENERGY INC Brine 0 365
2009 GAS ACQUISITION COMPANY LTD Brine 0 0
2012 STK INVESTMENTS LLC Brine 0 0
2014 STK INVESTMENTS LLC Brine 0 0
2015 STK INVESTMENTS LLC Brine 0 0
2017 STK INVESTMENTS LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1008204486 2012-7-12 0:00: PW No Violations 2.00
-1455523171 2017-5-30 0:00: PW No Violations 1.00
-1698674230 2017-7-28 0:00: PB No Violations 7.00
-714850996 2012-12-11 0:00 PW No Violations
0096700559 2017-04-12 UrbanProduction Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice inspection report 1343237660. The well has not been plugged. The well consisted of a 4.5 inch casing that was swaged with a ball valve and the valve on the wellhead was closed. The conductor casing and 8 5/8 inch casing were exposed. Ports on the 8 5/8 inch casing were equipped with a plug on one side and a closed ball valve on the other side. The well site was overgrown with brush. The last reported production for this well was in 1990. From 1991 to 2015 production has been reported as zero. The tank battery consisted of one 210 BBL production tank, one 50 BBL steel brine tank, and a mechanical separator. The tank battery was shared with well 2-0896 (Schnurrrenberger #1). The valves on the separator were closed and flow lines from the wells were disconnected from the separator. The chart box has been removed. There was a some seepage of oil around the plate on the 210 BBL production tank at the vent stack/heater tube location. Tank valves were equipped with flat plugs. The tank battery dike was very weathered and needed rebuilt and the entire tank battery was very overgrown with trees and brush. No signage was present at the well or tank battery locations. The lease access was stable.
0714850996 2012-12-11 Production Wells No Violations On 12/11/2012, I spoke to Kurt Schannaberger from STK Investments about the plugging permit for the above well, he said that they had applied for the permit. On 12/13/2012 I received the plugging permit in the US Mail at my residents. Date issued 12/13/2012 permit expires on 12/13/2014.
1008204486 2012-07-12 Production Wells Violations Noted I received a phone call from Mr. Schnurrenberger about an idle well on his property. I checked our database and there has been no production reported from 1996 to present. There was a plugging permit issued in 2008 but the well was not plugged. I met with Mr. Schurrenberger on 7/12/2012 and we located the above well. At the present time this well is not capable of production the flow lines are disconnected and the production unit needs repaired. There is no identification signs at well head. I recommend that this well be plugged.
1343237660 2012-07-12 Production Wells Violations Noted I receive a phone call from Mr. Schnurrenberger about an idle well on his property. I looked in our database, there has been no production from 1996 to present, there was a plugging permit issued in 2008 but was not plugged. I met with him on 7/12/2012, we located the above well, at present time this well is not capable of production . There is no ID signs at well head. I recommend that this well be plugged.
1382627467 2013-10-07 Preliminary Restoration No Violations On 10/7/2013, I called Kurt Shanaberger from STK Investment about the Compliance Noticed that was issued on 7/11/2012. I explained to him that the landowner was asking about a plugging time frame. There was a plugging permit issued on 12/13/2012 and expires on 12/13/2014. Kurt stated that they were putting a plan togather to plug this well.
1455523171 2017-05-30 Production Wells No Violations I meet with Jay Adams of Js Well Service and Dave Schnurrenberger landowner of the STK Investments about the ingress and egress of the property to the plug the well. Jay Adams will walk the property and discuss the best way to get equipment in to perform the plugging.
1501851533 2017-07-27 Plug / Plug Back No Violations I was on location to witness the plugging of the above well. This well was plugged back to the Newburg by the Division of Mines. 3/7/1995. J-Well Service is the contractor on location. They ran inside of the 4.5 casing to tag cement top. The tools stopped at 88 from surface. These tools are 3.5 in diameter. They tripped out with these tools and picked up a small set and went back in the well and stopped at the same spot. Packed well of will bring 1.5 tubing out and a 3tri-cone bit and try tomorrow. 7/282017.
1510167467 2017-10-24 Plug / Plug Back No Violations J- Well Service was on location. They set up to pull stretch on the 4.5 casing as they pulled the casing it was parted at 77below ground. Unable to get center spear or tri-cone bit inside of 4.5 casing At this time there is a consultant working with STK and Matt Kleese with a plan to go forward with the plugging operation. Compliance notice #-1343237660 remains open at this time.
1698674230 2017-07-28 Plug / Plug Back No Violations J- Well Service was on location. They set up to pull stretch on the 4.5 casing as they pulled the casing was already parted. They pulled 77 of casing. They ran 1.5 tubing with a tri-cone bit on the bottom of the tubing. They started rotating the bit with the tongs. There was some progress. They tripped the bit out and inspected it. Jay Adams thinks they may be setting on metal . Ran an impression block but did not show us any thing of value. The decision was made to pack the well of and move to the #1- 0896. Check about tools and over shot casing to finish plugging operation.
96700559 2017-4-12 0:00: UP No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1008204486 US-OH-100377 2012-08-24 Well shall be plugged
1343237660 US-OH-109911 2014-04-10 Failure to legibly identify well
1343237660 US-OH-109912 2014-04-10 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[9]

References