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Well ID: 34-111-22098 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Green Township | |
Operator Name: GENESIS RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: LONACHER UNIT | |
License Status: Producing | |
License Date: 1980-08-22 | |
Spud Date: 1980-09-16 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-09-22 | |
Well Total Depth: 3228.00 ft | |
Configuration: Vertical | |
Latitude: 39.710000 | |
Longitude: -80.950000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-08-22 | 311 STOCKER & SITLER INC GeoDate 8/22/80 |
Original Spud | 1980-09-16 | I.P. WELL NOT TURNED INTO PRODUCTION AT THIS TIME DUE TO THE LACK OF A GAS MARKET IN THIS AREA. |
Completed | 1980-09-22 | I.P. WELL NOT TURNED INTO PRODUCTION AT THIS TIME DUE TO THE LACK OF A GAS MARKET IN THIS AREA. |
Reached Total Depth | 1980-09-22 | I.P. WELL NOT TURNED INTO PRODUCTION AT THIS TIME DUE TO THE LACK OF A GAS MARKET IN THIS AREA. |
Change of Owner | 2000-04-10 | Operator changed from 311, STOCKER & SITLER INC to 5429, MILEY GAS COMPANY |
Change of Owner | 2006-11-21 | Operator changed from 5429, MILEY GAS COMPANY to 1634, NORTHWOOD ENERGY CORP |
Record Last Modified | 2013-10-03 | I.P. WELL NOT TURNED INTO PRODUCTION AT THIS TIME DUE TO THE LACK OF A GAS MARKET IN THIS AREA. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2306 | 2320 | 39 |
2306 | 2320 | 39 | |
2306 | 2320 | 39 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1228 Bbl | 35000 | GORDON | ||
ACID | 28 | 500 Gal | 0 | WEIR | ||
Not Treated | 0 | 5000 Lbs | 0 | MESH, WEIR | ||
N2 | 0 | 114 Mscf | 0 | GORDON, NOTE: WEIR-TOO TIGHT, SHUT IN | ||
H2O | 0 | 400 Bbl | 0 | WEIR |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2007 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2008 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2009 | NORTHWOOD ENERGY CORP | 845.00 | 0.00 | 365 |
2010 | NORTHWOOD ENERGY CORP | 719.00 | 0.00 | 365 |
2011 | NORTHWOOD ENERGY CORP | 1029.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 931.00 | 0.00 | 366 |
2013 | NORTHWOOD ENERGY CORP | 378.00 | 0.00 | 365 |
2014 | NORTHWOOD ENERGY CORP | 518.00 | 0.00 | 365 |
2015 | NORTHWOOD ENERGY CORP | 192.00 | 0.00 | 365 |
2016 | NORTHWOOD ENERGY CORP | 819.00 | 0.00 | 365 |
2017 | NORTHWOOD ENERGY CORP | 504.00 | 0.00 | 365 |
2018 | NORTHWOOD ENERGY CORP | 416.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2007 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2008 | NORTHWOOD ENERGY CORP | Brine | 30 | 0 |
2009 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2010 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2011 | NORTHWOOD ENERGY CORP | Brine | 0 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 0 | 366 |
2013 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2014 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2015 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2016 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2017 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2018 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1149202594 | 2006-05-30 | Production Wells | No Violations | Request from landowner to inspect well for compliance,upon inspecting well site found leaking 2 valve instructed well owner to repair valve and install 2 plug so livestock cant rub on valve and create leaking valve problems. |
For data sources see[9]