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Well ID: 34-111-23131 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Franklin Township | |
Operator Name: GENESIS RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: KELBY | |
License Status: Producing | |
License Date: 1984-08-15 | |
Spud Date: 1984-11-19 | |
Spud Drilling Contractor: CT DRILLING | |
Final Drill Date: 1984-11-22 | |
Well Total Depth: 2550.00 ft | |
Configuration: Vertical | |
Latitude: 39.680000 | |
Longitude: -81.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-08-15 | Issued Date 8/15/84 Expired Date 2/11/85 Acres 0020000 Tool Type RTA Proposed Formation GORDON Proposed Depth 02550 Proposed Drill Depth 02550 |
Original Spud | 1984-11-19 | |
Completed | 1984-11-22 | |
Reached Total Depth | 1984-11-22 | |
CO | 1984-11-30 | 1645 CAPECO INC GeoDate 8/15/84 |
Completion Report Received | 1984-12-31 | |
Construction Permit Expires | 1985-02-11 | |
CO | 1993-07-22 | 4540 PEOPLES PETROLEUM CORP. GeoDate 8/15/84 |
Change of Owner | 2001-02-23 | Operator changed from 4540, PEOPLES PETROLEUM CORP. to 3133, PETROEL |
Change of Owner | 2001-06-25 | Operator changed from 3133, PETROEL to 7007, CARPER WELL SERVICE |
Change of Owner | 2013-08-30 | Operator changed from 7007, CARPER WELL SERVICE to 9086, GENESIS RESOURCES LLC |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1962 | 1964 | 8 |
1966 | 0 | ||
1997-06-29 | 1966 | 0 | |
1962 | 1964 | 8 | |
1962 | 1964 | 8 | |
2006-09-11 | 2212 | 2238 | 15 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 887 Bbl | 41790 | FRAC;H2O,SAND,N2 | ||
H2O | 0 | 511 Bbl | 25494 | |||
N2 | 0 | 120 Mscf | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2002 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2003 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2004 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2005 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2006 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2007 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2008 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 365 |
2009 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 365 |
2011 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2012 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2013 | CARPER WELL SERVICE INC. | 0.00 | 0.00 | 0 |
2014 | GENESIS RESOURCES LLC | 0.00 | 0.00 | 0 |
2015 | GENESIS RESOURCES LLC | 0.00 | 0.00 | 365 |
2016 | GENESIS RESOURCES LLC | 8.00 | 0.00 | 22 |
2017 | GENESIS RESOURCES LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2002 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2003 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2004 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2005 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2006 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2007 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2008 | CARPER WELL SERVICE INC. | Brine | 0 | 365 |
2009 | CARPER WELL SERVICE INC. | Brine | 0 | 365 |
2011 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2012 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2013 | CARPER WELL SERVICE INC. | Brine | 0 | 0 |
2014 | GENESIS RESOURCES LLC | Brine | 0 | 0 |
2015 | GENESIS RESOURCES LLC | Brine | 0 | 365 |
2016 | GENESIS RESOURCES LLC | Brine | 0 | 22 |
2017 | GENESIS RESOURCES LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1097336319 | 2017-1-18 0:00: | PW | No Violations | 0.90 |
-1146344666 | 2008-2-19 0:00: | PW | No Violations | |
-1179618523 | 2003-2-10 0:00: | PW | No Violations | |
-1203047735 | 2019-7-10 0:00: | PW | No Violations | 1.00 |
-1240776357 | 2014-4-9 0:00:0 | PW | No Violations | 1.10 |
-1496575586 | 2008-2-19 0:00: | PW | No Violations | |
-1744608175 | 2020-2-18 0:00: | PW | No Violations | 0.60 |
-547488038 | 2014-1-6 0:00:0 | AM | No Violations | |
000PL10335 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0083170725 | 2013-03-04 | Production Wells | Violations Noted | Status check inspection due to no reported production to the division. Inspection of the well head found the following equipment present 4.5 production casing- 1.5 tubing and pumping rods with the production valves open and the well set up to be produced by the means of a pumping unit. At the production fluid storage area a 100 barrel production tank is present along with a mechanical separator and gas sales meter with no current sales chart present. Tank battery has no dike in place and a livestock fence will need erected before the well is put back into production. Inspector will note that the landowner and Carper well svc both have confirmed that there is a ongoing legal dispute that needs resolved over the lease and notification was made to Carper well svc on 03/01/13 that the division would be addressing the issue of the idle wells in the area. There is also a unresolved Violation issued on 02/28/2008 by Pat Shreve. Sec. 1509.062. (A)(1) The owner of a well that has not been completed, a well that has not produced within one year after completion, or an existing well that has no reported production for two consecutive reporting periods as reported in accordance with section 1509.11 of the Revised Code shall plug the well in accordance with section 1509.12 of the Revised Code, obtain temporary inactive well status for the well in accordance with this section, or perform another activity regarding the well that is approved by the chief of the division of mineral resources management |
0179425311 | 2008-02-19 | Production Wells | No Violations | FOLLOW UP TO NOV # 708395610 ON DAY OF INSPECTION WELL IS A RABBIT WELL.WELL IS SHUT IN.NO PRODUCTION HAS BEEN TURNED IN.WELL IS ONE THAT GEORGE WALKER IS SAID TO HAVE BUT NO TRANSFER HAS TAKEN PLACE. |
0547488038 | 2014-01-06 | Administrative Inspection | No Violations | Administrate inspection to document the transfer of the well from Greg Capadonna - Carper Well Svc to Genesis Resources. I shall monitor the production and the corrective action taken of the new owner and quiet the past violations when the prior problems have been corrected. |
0547693190 | 2008-03-03 | Production Wells | No Violations | RABBIT WELL STILL SHUT IN WAITING FOR TRANSFER OF OWNERSHIP FROM CARPER TO GEORGE WALKER.IN COURT PROCEEDINGS.WILL INSPECT AGAIN AT LATER DATE. |
0616353405 | 2013-07-23 | Production Wells | No Violations | Compliance Notice follow up from 03/04/2013, The required action due date response time has elapsed. The registered owner of the said well known as Carper Well Service has 30 days to respond to the Division in writing as required by law a feasible plan to correct the issues with the said well, or file with the Division a plugging application. If no response is received within 30 days of receiving this notification the Inspector shall move foreword with a Chiefs order requesting a Suspension of activities against the said producer known as Carper Well Service. Inspector Bill Stolarik 1-740-507-6592. |
0708395610 | 2008-02-19 | Production Wells | Violations Noted | ON DAY OF INSPECTION WELL IS A RABBIT WELL.WELL IS SHUT IN.NO PRODUCTION HAS BEEN TURNED IN.WELL IS ONE THAT GEORGE WALKER IS SAID TO HAVE BUT NO TRANSFER HAS TAKEN PLACE. |
0860047236 | 2018-10-02 | Production Wells | No Violations | Inspection request as a complaint filed by the landowner George Walker who indicated the production tank was leaking and the well was idle. Upon inspection of the well head the well was observed to be equipped with a 8.625 diameter surface casing and well head along with a 4.5 diameter production casing and casing well head and also a 1.900 diameter production tubing string and tubing well head. There is a 2 diameter steel flow line present attached to the casing well head that is partially in the open position. There is a 2 diameter steel flow line present attached to the tubing well head that is also in the open position however the valve handle is missing. The well is set up to be produced by the means of a pumping unit however no drive motor or engine is present. Also located on the property is the production facility consisting of a single 100 barrel capacity steel construction tank along with a mechanical separator and gas sales meter. Also observed and photographed was the sales chart in the meter was last dated 02/26/2017 and was in poor condition, both the fluid and gas outlet lines on the mechanical separator were closed. No oil was found out from under the tank or off site. Also noted was no identification was present on the tank or well and no sign of recent human activity was present in the area. The registered owner Andrew Allphin was contacted at 11:51 am with a voice message being left informing him that I believed the tank had started to leak from underneath and the issue needed addressed. My direct Supervisor Brent Bear was notified of my findings along with the landowner George Walker. |
1010985081 | 2019-02-20 | Production Wells | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please reference his comments for a detailed report. We are conducting an inspection in regard to a follow-up for complaint numbers 5365 and 5614. |
1097336319 | 2017-01-18 | Production Wells | No Violations | Compliance Notice # 1466526738 follow up inspection found the 4.5 diameter casing valve now open and the gas sales meter with a current 31 day sales chart. The prior violation and complaint are considered addressed. |
1146344666 | 2008-02-19 | Production Wells | No Violations | FOLLOW UP TO NOV # 179425311 FOLLOW UP TO NOV # 708395610 ON DAY OF INSPECTION WELL IS A RABBIT WELL.WELL IS SHUT IN.NO PRODUCTION HAS BEEN TURNED IN.WELL IS ONE THAT GEORGE WALKER IS SAID TO HAVE BUT NO TRANSFER HAS TAKEN PLACE. |
1179618523 | 2003-02-10 | Production Wells | No Violations | rabbit well,all production equiptment in place ,well appears capable of production. |
1235592755 | 2009-02-06 | Production Wells | No Violations | WELL IS ON A LAND OWNERS FARM BY THE NAME OF GEORGE WALKER THAT CLAIMS HE OWNS LAND BY AFFIDAVIDE OF FORFIETURE.TALKED TO MILLNARD CARPER AND CLAIMS THAT THE WELL IS STILL HIS.WELL IS RABBIT WELL THAT IS MAKING HOUSE GAS FOR WALKER. |
1240776357 | 2014-04-09 | Production Wells | No Violations | Compliance notice follow up inspection found the production valves in the open position and a current gas sales chart in the meter and proper well identification posted. RBDMS records show the well has been transferred from the previous owner to Genesis Resources and in phone conversation with Andrew Allpin the owner of Genesis he stated all production has been submitted. I have resolved the following violations on this day 179425311-708395610 & 83170725. |
1412501486 | 2019-11-15 0:00 | PW | No Violations | 1.00 |
1466526738 | 2016-06-21 | Production Wells | Violations Noted | On site inspection request as a response to complaint # 5356 received by the Division on 06/20/2016 by the Landowner George Walker. On this day I responded to the complaint and made contact with the landowner George Walker who accompanied me while I inspected both the well site and production facility. Upon inspection of the well head it was observed that the well was equipped with 4.5 production casing -1.5 production tubing with a production tree in place on the tubing and pumping rods in the well and a pumping unit in place over the well with no drive motor present on the pumping unit. Also noted the production valves are in the open position. Inspection of the production facility found a single 100 barrel production tank present along with a mechanical separator and gas sales meter with no current sales chart in the gas meter and no reported commercial production found reported to the Division since 2001.No well identification was present. Instructions are as follows- The well owner/operator shall submit a written plugging schedule to (William Stolarik) at (5880 Memory Road Zanesville Oho 43701) within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1496575586 | 2008-02-19 | Production Wells | No Violations | FOLLOW UP TO NOV # 708395610 ON DAY OF INSPECTION WELL IS A RABBIT WELL.WELL IS SHUT IN.NO PRODUCTION HAS BEEN TURNED IN.WELL IS ONE THAT GEORGE WALKER IS SAID TO HAVE BUT NO TRANSFER HAS TAKEN PLACE. |
1538669163 | 2018-10-04 | Production Wells | No Violations | Follow up inspection to complaint # 5365 & # 5614 filed by the landowner George Walker who has indicated the well is idle and not capable of production and the production tank was leaking. On 10/03/2018 I contacted the registered well owner Andrew Allphin and questioned the reported production for 2016 of 8 mcf of gas and requested a meeting on site along with Division management, I informed Mr. Allphin at the time of the meeting that he would be asked to demonstrate how the well is capable of production and produce the production records reported to the Division for the production reported during the reporting year of 2016. At that point Mr. Allphin indicated he did not believe he had the records and asked if plugging the well was acceptable. I indicated to Mr. Allphin that the production tank be emptied to ensure it does not leak, the landowner indicated product was leaking from the tank in his complaint. However only a small amount of old product was found under the valve. The product was less than 12 in diameter and was not current activity. I also discussed that the lease production meter chart posted had not been changed since 02/26/2017. I also requested that Mr. Allphin inform me of when the crews would be on site addressing the issues with the production tank. On this day I visited the tank battery site and found the operator has not removed the product from inside the tank. I spoke with my supervisor Brent Bear and we agreed that I would once again contact Mr. Allphin and request a plan of action including a date to plug the well. I attempted to call Mr. Allphin @ (304) 991-0721 with no answer. I did leave a voicemail with indication that a plan was to be drafted and I needed notification of when the crews would be on site. |
1550678338 | 2019-02-20 | Production Wells | Violations Noted | Follow up inspection to complaint # 5365 & # 5614 filed by the landowner George Walker accompanied n this day by ODNR Inspector Tom Thomas. The well was observed to be equipped with a 4.5 diameter production casing string and a 1.900 diameter production tubing string. Attached to the casing and tubing well heads are 2 diameter flow lines equipped with both check and shut off valves. Both the casing and tubing valves are in the open position. The casing and tubing flow lines are conjoined into a single 2 diameter sales line near the well head. The well is set up to be produced by the means of a pumping unit however no drive motor or engine is present. The production facility is equipped with a single 100 barrel steel tank along with a mechanical separator and gas sales meter with no current or sales chart present in the meter. All production valves are closed at the sales meter and separator. No identification is present at the well or production facility. Historically on 10/03/2018 I contacted the registered well owner Andrew Allphin and questioned the reported production for 2016 of 8 mcf of gas and requested a meeting on site along with Division management, I informed Mr. Allphin at the time of the meeting that he would be asked to demonstrate how the well is capable of production and produce the production records reported to the Division for the production reported during the reporting year of 2016. At that point Mr. Allphin indicated he did not believe he had the records and asked if plugging the well was acceptable. On 01/30/2019 I reached back out to Andrew Allphin by phone for a status update of the plugging permit application and was informed the plugging application had not been applied for to date. Instructions are as follows. The well owner/operator shall submit a written plugging schedule to Inspector Bill Stolarik at 5880 Memory Road Zanesville, Ohio 43701 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operato |
1560515353 | 2019-6-14 0:00: | PW | No Violations | |
1563800292 | 2019-7-22 0:00: | PW | No Violations | 3.00 |
1565010626 | 2019-8-5 0:00:0 | PW | No Violations | 0.50 |
1567521166 | 2019-9-3 0:00:0 | PW | No Violations | 1.00 |
1574184842 | 2019-11-15 0:00 | PW | No Violations | 1.00 |
1585659062 | 2020-3-31 0:00: | PW | No Violations | 0.40 |
1587472413 | 2020-4-21 0:00: | PW | No Violations | 0.70 |
1595262380 | 2020-7-20 0:00: | PW | No Violations | 0.50 |
1599832183 | 2020-9-11 0:00: | PW | No Violations | 0.80 |
179425311 | 2008-2-19 0:00: | PW | No Violations | |
1888636496 | 2019-8-29 0:00: | PW | No Violations | 0.50 |
2016743538 | 2019-9-23 0:00: | PW | No Violations | 1.00 |
547693190 | 2008-3-3 0:00:0 | PW | No Violations | |
616353405 | 2013-7-23 0:00: | PW | No Violations | 0.50 |
708395610 | 2008-2-19 0:00: | PW | No Violations | |
83170725 | 2013-3-4 0:00:0 | PW | No Violations | |
860047236 | 2018-10-2 0:00: | PW | No Violations | 1.00 |
PL10335 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0083170725 | US-OH-129473 | 2019-03-22 | 9-1-03C | Forfeiture of bond |
0083170725 | US-OH-129474 | 2019-03-22 | NONE_ | Nonproduction; well shall be plugged or placed in temporary inactive status |
0083170725 | US-OH-129475 | 2019-03-22 | NONEC | Statement of annual production not filed |
0708395610 | US-OH-127989 | 2008-02-28 | Failure to legibly identify well | |
0708395610 | US-OH-127990 | 2008-02-28 | Well shall be plugged | |
1466526738 | US-OH-113469 | 2016-06-24 | Failure to legibly identify well | |
1466526738 | US-OH-113470 | 2016-06-24 | Well shall be plugged | |
1550678338 | US-OH-115058 | 2019-02-22 | Failure to legibly identify well | |
1550678338 | US-OH-115059 | 2019-02-22 | Well shall be plugged |
For data sources see[9]