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34-111-24622

Well Details

Well ID: 34-111-24622
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Country: United States
State: Ohio
County: Monroe
Municipality: Malaga Township
Operator Name: ANTERO RESOURCES CORPORATION
Well Pad ID: US-OH-001329
Farm/Lease Name: LAYTON UNIT
License Status: Producing
License Date: 2015-10-23
Spud Date: 2015-10-29
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2016-01-23
Well Total Depth: 16700.00 ft
Configuration: Horizontal
Latitude: 39.850000
Longitude: -81.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2015-10-23 Proposed Formations:POINT PLEASANT, Issued Date:10/23/2015, Expired Date:10/22/2017 12:00:00 PM, Drilling unit acres:561.971, Proposed Well Type:OG, Proposed Well Class:NWC
Reached Total Depth 2016-01-23
Correction to Well 2016-04-22 CHANGE IN TARGET/TAKE PER AS DRILLED PLAT-ALE
Completion Report Received 2016-09-23
Construction Permit Expires 2017-10-22
Record Last Modified 2018-07-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2016-09-26 8780 16615 0
8780 16615 0
8780 16615 0

For data sources see[3]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 05/03/2016 05/30/2016 8576 11,977,400.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 WFRA-405 U.S. Well Services Friction Reducer Hydrated light distillate (petroleum) 64742-47-8 30 0.02444 27432.2
2-Propenoic acid, polymer with 2 propenamide 9003-06-9 30 0.03036 34077.2
Ethoxylated alcohol blend 68002-97-1 4 0.00405 4543.63
Water 7732-18-5 60 0.06072 68154.5
AI-302 U.S. Well Services Acid Corrosion Inhibitors Water 7732-18-5 95 0.0004 443.688
2-Propyn-1-olcompound with methyloxirane 38172-91-7 15 0.00006000 70.056
Water Antero Resources Base Fluid Water 7732-18-5 100 88.9974 99,891,100.0
Sand U.S. Well Services, LLC Proppant Crystalline Silica, quartz 14808-60-7 100 10.4803 11,763,100.0
K-BAC 1020 U.S. Well Services Anti-Bacterial Agent Deionized Water 7732-18-5 28 0.00233 2620.09
2,2-dibromo-3-nitrilopropionamide 10222-01-2 20 0.00409 4587.04
HCL Acid (12.6%-18.0%) U.S. Well Services, LLC Bulk Acid Hydrogen Chloride 7647-01-0 18 0.04386 49225.7
Water 7732-18-5 87.5 0.18361 206079
AP One U.S. Well Services Gel Breakers Ammonium Persulfate 7727-54-0 100 0.00234 2625
LGC-15 U.S. Well Services Gelling Agents Surfactant 68439-51-0 3 0.00421 4719.74
Petroleum Distillates 64742-47-8 60 0.06637 74497.9
Suspending agent (solid) 14808-60-7 3 0.01072 12030.7
Guar Gum 9000-30-0 50 0.07008 78662.4
SI-1100s U.S. Well Services Scale Inhibitor Water 7732-18-5 80 0.00998 11202.3
Hexamethylene diamine penta (methylene phosphonic acid) 23605-74-5 2 0.00032 364.074
Phosphino carboxylic acid polymer 71050-62-9 5 0.00081 910.186
Potassium salt of diethylene triamine

penta (methylene phosphonic acid)

15827-60-8 7.5 0.00126 1417.79
Hexamethylene tramine penta (methylene phosphonic acid) 34690-00-1 5 0.00081 910.186
Copolymer of Maleic and Acrylic acid 52255-49-9 10 0.00147 1652.34

For data sources see[4]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2016-05-31 H2O 0 6716 Bbl 264860 US Well Services Inc STAGE 1/45

60 SHOTS STAGES 2-44 SEE IMAGES

2016-06-09 H2O 0 5738 Bbl 264960 US Well Services Inc STAGE 45/45

60 SHOTS

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2016 ANTERO RESOURCES CORPORATION 1966764 376 153
2017 ANTERO RESOURCES CORPORATION 2049217 400 365
2018 ANTERO RESOURCES CORPORATION 754975 310 363
2019 ANTERO RESOURCES CORPORATION 143542 110 90

For data sources see[6] [7]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2016 ANTERO RESOURCES CORPORATION Brine 19178 153
2017 ANTERO RESOURCES CORPORATION Brine 11925 365
2018 ANTERO RESOURCES CORPORATION Brine 4371 363
2019 ANTERO RESOURCES CORPORATION Brine 756 90

For data sources see[8] [9]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1139518333 2016-9-22 0:00: PL No Violations 0.50
-1281218981 2015-12-7 0:00: DD No Violations 1.60
-238858520 2016-5-9 0:00:0 CT No Violations 0.50
-356622103 2016-1-12 0:00: DD No Violations 1.50
-656446912 2017-12-29 0:00 PW No Violations 0.20
-839615888 2019-1-24 0:00: PW No Violations 0.20
0154493872 2015-10-30 Casing String Witnessed No Violations The said well was spudded on 10/2913/2015 by Express Energys top hole rig with a 85 x 32 conductor borehole being drilled and 85 of .375 wall 26 conductor being set. Permission was granted to set the conductor at 85 due to being in solid bedrock. Express Energys Cement service cemented the casing using 270 sacks of class A cement with the cement mix water verified chloride free and PH of 7 and circulation established prior to cementing with the cement displaced with 46.45 barrels of fresh water and good cement returns witnessed to surface.
0238858520 2016-05-09 Completion Testing No Violations Status check inspection on the well bore completion process found US Well service rigging up to begin the stimulation process on the 4 existing wells on the pad. Allied Horizontal Wire Line Service is on location and has initiated a wire line bond log on each of the wells, also noted is the well bore toe key preparation work has been completed. All equipment on location is located on polymer containment and the well pad perimeter drainage valves are in the closed position and the company has a vacuum truck service identified as ECM recovering any product that may accumulate in the well pad sumps or on the location surface. Bass Well Head is the well head control company. The company Representative also indicated that they are conducting weekly gas alarm and emergency shut down drill for the location in case of a on site emergency during stimulation operations.
0356622103 2016-01-12 Drill / Deepen / Reopen No Violations
0656446912 2017-12-29 Production Wells No Violations Status check inspection found the well head equipped with a casing and tubing well head with both the casing and tubing well head production valves open and feeding into a production sales line that leads to a gas processing unit on location near the well head. Annular pressure monitoring gauges are present on the well head. There is a total of 4 completed wells on the location along with 4 gas processing units and 8 -400 barrel capacity steel construction production tanks. The well pad has a earthen berm perimeter and the well pad surface is of stone construction. The lease road is gravel construction and in good repair. Also 4 additional wells were spudded on the pad and the conductor casing only was set.
0839615888 2019-01-24 Production Wells No Violations On this day, I found the pad gated with signage at the entrance. There are (4) producing wells, (4) additional wells that have had only the conductor drilled and set, (4) gas processing units (GPU), (2) 400-barrel steel production tanks within polymer lined steel containment, and an Emergency Shutdown (ESD) button is present at the pad entrance. Additionally, concrete barriers surround the perimeter of the wellheads. Identification and annular pressure monitoring devices are present. The 9.625 inch diameter intermediate casing has a pressure of 260 pounds per square inch (psi), and the 13.375 inch diameter surface casing has a pressure of 50 psi.
0889462006 2016-05-31 Completion Testing No Violations Status check inspection on the well stimulation process found US Well Service pressure pumping crew rigging up on the well to begin the stimulation process, Annular pressure monitors are installed on both the 5.5 and 9.625. Allied Hrizontal wireline service is the perforation contractor. Bass Well Head is the well head control service provider.
0937033223 2016-09-22 Preliminary Restoration No Violations Preliminary Restoration status check inspection accompanied on this day by ODNR Division Staff member Jimmy Wiles. Upon inspection of the well it was observed that the well drilling and completion process is now complete with a casing head and tubing production head installed. Warrior Energy service is on location with their flow back equipment monitoring the well flow back process. There is 4 wells now complete on the well pad and on line with 4 gas processing units in place. There is 8 -400 barrel capacity production tanks on location located inside a poly lined steel containment dike area. Addressing the restoration- The well site meets ORC 1509.072 with vegetation established and erosion control in place. The company also still has all perimeter filter sock and super silt fence in place at this time and will be removed at their discretion at a later date.
1139518333 2016-09-22 Preliminary Restoration No Violations Preliminary Restoration status check inspection accompanying Inspector Bill Stolarik with the following being observed on this day. The affected area of the well site construction has been restored according to ORC 1509.072 with erosion control and vegetation being established, all ditch lines are rock lined and the well pad construction perimeter still has super silt fence and filter sock in place to be removed at a later date by the company. There is 4 wells on the well pad now in production with more well permitted and not complete as of the date of my inspection. Inspector Stolarik signed off on the restoration on his report for this day.
1281218981 2015-12-07 Drill / Deepen / Reopen No Violations Status check inspection on the current drilling progress found Patterson Drilling rig # 343 on location currently drilling the 12.250 intermediate well bore at a measured depth of 4,228 -the company is mist drilling on air at 35 gpm. The drilling rig is located on polymer containment and the well location perimeter containment drain valves are in the closed position.
1451567922 2015-12-31 Drill / Deepen / Reopen No Violations On the day of my inspection I witnessed Patterson UTI Drilling Rig #343 was preparing to trip in the wellbore and drill out the 9.625 inch float equipment and begin building their curve. Completed walk around with Antero Consultant Roesendo Perez revealing safe simultaneous operations ongoing as Express Energy was rigging up to cement conductor on the 34111246390000 Atwater 3H.
1451922182 2016-01-04 Drill / Deepen / Reopen No Violations
1452270717 2016-01-08 Drill / Deepen / Reopen No Violations Status check inspection on the well drilling status found Patterson Drilling rig 343 on locating and currently attempting to recover the stuck drilling bottom hole assembly at a depth of 12,084 by the means of using Hydraulic jars and working the drill string.
1453383752 2016-01-21 Drill / Deepen / Reopen No Violations
1498586138 2017-06-27 Production Wells No Violations Status check inspection found the well equipped with a production tree casing head and the production valve in the open position. Annular pressure monitoring gauges are present. At the production fluid storage facility a total of (8) steel tanks capable of holding 400 barrels of fluid each are present inside a polymer lined steel containment dike area. A total of 4 gas processing units are present on location one each for each existing well present on the pad.
1502966102 2016-01-07 Drill / Deepen / Reopen No Violations Status check inspection on the well drilling process found Paterson Drilling rig # 343 on location with the drill string currently sitting on bottom stuck at 12,084. CLX wireline is on location and has perforated the drill string with 24 perforations at 11,924 to 11,930 in attempt to gain circulation and free the drill string and Weathorford Directional drilling bottom hole assembly, while circulation was gained to surface the rig was pulling 400,000# along with jarring with the hydraulic jars and was unable to free the directional assembly. The Company men on site reported they were preparing to run in the hole and shoot off the drill string and abandon the tools still in the hole, the company will run in and set a cement plug and deviate around the lost tools in the hole.
154493872 2015-10-30 0:00 CS No Violations 3.00
1734374510 2020-4-24 0:00: PW No Violations 1.50
889462006 2016-5-31 0:00: CT No Violations
937033223 2016-9-22 0:00: PL No Violations 5.00

For data sources see[10]

References