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| Well ID: 34-111-24668 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Monroe | |
| Municipality: Center Township | |
| Operator Name: GULFPORT APPALACHIA LLC | |
| Well Pad ID: US-OH-001401 | |
| Farm/Lease Name: CLAUGUS 210245 | |
| License Status: Producing | |
| License Date: 2016-09-08 | |
| Spud Date: 2016-10-06 | |
| Spud Drilling Contractor: H&P DRILLING | |
| Final Drill Date: 2016-12-09 | |
| Well Total Depth: 16510.00 ft | |
| Configuration: Horizontal | |
| Latitude: 39.730000 | |
| Longitude: -81.070000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2016-09-08 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:9/8/2016, Expired Date:9/8/2018 12:00:00 PM, Drilling unit acres:636.901, Proposed Well Type:OG, Proposed Well Class:FWC |
| Reached Total Depth | 2016-12-09 | |
| Correction to Well | 2017-06-30 | UPDATE ACREAGE/TARGET/TAKE PER AS-DRILLED RCVD 6-23-17 ALE |
| Completion Report Received | 2018-05-16 | |
| Record Last Modified | 2018-07-24 | |
| Construction Permit Expires | 2018-09-08 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2018-05-22 | 9755 | 9900 | 50 |
| 2018-05-22 | 16204 | 16358 | 30 |
| 16204 | 16358 | 30 | |
| 9755 | 9900 | 50 | |
| 9755 | 9900 | 50 |
For data sources see[3]
| Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
|---|---|---|---|---|---|
| 1 | 01/07/2018 | 01/25/2018 | 9644 | 15,859,200.0 | 0 |
| Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
|---|---|---|---|---|---|---|---|---|
| 1 | Sand (100 Mesh Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 0.823148 | 1,213,140.0 |
| NEFE-180 | Chemplex SOLVAY | Corrosion Inhibitor/Iron Control | Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00003349 | 49.363 | |
| Methanol | 67-56-1 | 35 | 0.000234458 | 345.539 | ||||
| 2-Ethylhexanol | 104-76-7 | 10 | 0.00006699 | 98.726 | ||||
| Olefin | Proprietary | 5 | 0.00003349 | 49.363 | ||||
| Fatty acids, tall oil | 61790-12-3 | 5 | 0.00003349 | 49.363 | ||||
| 2-Propyn-1-ol | 107-19-7 | 5 | 0.00003349 | 49.363 | ||||
| Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00003349 | 49.363 | ||||
| Acetic acid | 64-19-7 | 65 | 0.000435421 | 641.716 | ||||
| Hydrochloric Acid (28%) | Dover | Acidizing | Water | 7732-18-5 | 72 | 0.00831494 | 12254.4 | |
| Hydrochloric Acid (Hydrogen Chloride) | 7647-01-0 | 28 | 0.00323359 | 4765.6 | ||||
| SI-20W | Moon | Scale Inhibitor | Phosphinocarboxylic Acid | 110224-99-2 | 45 | 0.00601725 | 8868.12 | |
| Water | 7732-18-5 | 55 | 0.00735442 | 10838.8 | ||||
| Water | Gulfport Energy | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 89.7998 | 132,345,000.0 | |
| Plexslick 920 | Chemplex SOLVAY | Friction Reducer | Copolymer of 2-propenamide | 69418-26-4 | 30 | 0.0218864 | 32255.8 | |
| Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00145909 | 2150.39 | ||||
| Ammonium Chloride | 12125-02-9 | 1 | 0.000729547 | 1075.19 | ||||
| Petroleum Distillate | 64742-47-8 | 20 | 0.0145909 | 21503.8 | ||||
| Water | 7732-18-5 | 45 | 0.0328296 | 48383.7 | ||||
| Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00145909 | 2150.39 | ||||
| Sand (40/70 Mesh Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 9.24772 | 13,629,100.0 | |
| Other Chemical(s) | Listed Above | See Trade Name(s) List | Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00145909 | 2150.39 | |
| Water | 7732-18-5 | 72 | 0.00831494 | 12254.4 | ||||
| Didecyldimethylammonium Chloride | 7173-51-5 | 8 | 0.00245962 | 3624.95 | ||||
| Water | 7732-18-5 | 55 | 0.00735442 | 10838.8 | ||||
| Fatty acids, tall oil | 61790-12-3 | 5 | 0.00003349 | 49.363 | ||||
| Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00145909 | 2150.39 | ||||
| Alkyl dimethyl benzyl ammonium chloride | 68424-85-1 | 5.5 | 0.00169099 | 2492.15 | ||||
| Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00003349 | 49.363 | ||||
| Petroleum Distillate | 64742-47-8 | 20 | 0.0145909 | 21503.8 | ||||
| 2-Propyn-1-ol | 107-19-7 | 5 | 0.00003349 | 49.363 | ||||
| 2-Ethylhexanol | 104-76-7 | 10 | 0.00006699 | 98.726 | ||||
| Ammonium Chloride | 12125-02-9 | 1 | 0.000729547 | 1075.19 | ||||
| Olefin | Proprietary | 5 | 0.00003349 | 49.363 | ||||
| Ethanol | 64-17-5 | 2 | 0.000614906 | 906.237 | ||||
| Methanol | 67-56-1 | 35 | 0.000234458 | 345.539 | ||||
| Water | 7732-18-5 | 60 | 0.0184472 | 27187.1 | ||||
| Water | 7732-18-5 | 45 | 0.0328296 | 48383.7 | ||||
| Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00003349 | 49.363 | ||||
| Bio B2512 | Aquaserv | Biocide | Alkyl dimethyl benzyl ammonium chloride | 68424-85-1 | 5.5 | 0.00169099 | 2492.15 | |
| Water | 7732-18-5 | 60 | 0.0184472 | 27187.1 | ||||
| Didecyldimethylammonium Chloride | 7173-51-5 | 8 | 0.00245962 | 3624.95 | ||||
| Ethanol | 64-17-5 | 2 | 0.000614906 | 906.237 | ||||
| Glutaraldehyde | 111-30-8 | 27 | 0.00830123 | 12234.2 |
For data sources see[4]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 2018-01-08 | H2O | 15 | 10264 Bbl | 353480 | STINGRAY PRESSURE PUMPING LLC | STAGE 1/30
STAGES 2-29 SEE IMAGES |
| 2020-01-25 | H2O | 15 | 11364 Bbl | 459 | STINGRAY PRESSURE PUMPING LLC | STAGE 30/30
STAGES 2-29 SEE IMAGES |
For data sources see[5]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2018 | GULFPORT ENERGY CORPORATION | 2533092 | 0 | 276 |
| 2019 | GULFPORT ENERGY CORPORATION | 399137 | 0 | 90 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2018 | GULFPORT ENERGY CORPORATION | Brine | 65318 | 276 |
| 2019 | GULFPORT ENERGY CORPORATION | Brine | 8627 | 90 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1090649937 | 2017-1-24 0:00: | PL | No Violations | 0.50 |
| -122198255 | 2018-5-2 0:00:0 | PW | No Violations | |
| -600453009 | 2016-12-8 0:00: | DD | No Violations | |
| 0122198255 | 2018-05-02 | Production Wells | No Violations | Status check inspection found There is 3 wells now drilled and producing on the pad. Each well is producing off the production tree and the production valves are in the open position, the production flow line valve shows 2,000 psi. There is annular pressure monitoring in place, the 13.375 well head section has 20 psi on the gauge and 400 psi on the 9.625 well head section. The well is equipped with an emergency shut down button that is controlled from multiple point on the well pad. There is a production facility present consisting of (4) steel 400 barrel tanks situated inside a polymer lined steel containment area. |
| 0556908771 | 2018-06-05 | Production Wells | No Violations | On this day, I found the well equipped with annular pressure monitoring devices. The 13.375 inch diameter surface casing pressure gauge is reading 25 pounds per square inch, and the 9.625 inch diameter intermediate casing pressure gauge is reading 200 pounds per square inch. The facility is gated with proper signage and an electronic shutdown button at the entrance. There is a midstream facility at the front left-side of the pad, prior to the gate. (3) gas processing units are located at the front right-side. There are (3) wells in production on this pad, all with electronic shutdown buttons. All wells have concrete barriers surrounding them. The wellheads are properly identified. There are (4) 400 barrel steel tanks within containment, at the back right-side, with an electronic shutdown button. |
| 0600453009 | 2016-12-08 | Drill / Deepen / Reopen | No Violations | Status check inspection on the 9.625 diameter round casing wireline logging evaluation to determine the annular cement top. KLX Energys wireline truck is on location and has ran multiple logs on the well with the following logs noted -3 temperature logs were ran one with the casing annular shut in, one with the casing annular flowing, one with 1,800 psi on the annular side of the 9.625 and one with pressure on the casing internal, a fourth log was ran with the well shut in identified as a Gamma Ray CCL log with the cement top indicated at 7,900. The company also attempted to get the 9.625 annular to take fluid unsuccessfully with no rate achieved. |
| 0974603244 | 2016-12-05 | Drill / Deepen / Reopen | No Violations | |
| 1090649937 | 2017-01-24 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection found the area disturbed within the well pad limits of disturbance has been restored according to ORC 1509.072 with erosion control in place and vegetation established. The wood chip filled filter sock used around the well pad perimeter to control erosion is still in place. The outward slopes of the well pad are stable and the lease road is in good repair, the well pad entrance is gated and signage is posted. Addressing the 4 wells present on the pad, the well drilling is complete and the wells are awaiting stimulation. No production equipment is present. |
| 1481142981 | 2016-12-07 | Drill / Deepen / Reopen | No Violations | Status check inspection on the 9.625 casing string remedial evaluation. On this day a retrievable bridge plug was set off the drill string at 7,815 and pressure tested to 2,700 psi at surface. KLX wireline was on location and rigging up to run a casing temperature log. |
| 1531962708 | 2016-11-22 | Casing String Witnessed | No Violations | On site inspection to witness the surface casing cement job with H&P Drilling rig 628 on the hole and Stingray cement service cementing the 13.375 surface string with a 17.5 well bore drilled to 1,354 and 54.5 lb/ft J-55 ran to 1,351 with a float shoe and collar casing equipment along with proper centralizer placement demonstrated. Stingray cemented the casing by first establishing circulation and then pumping 25 barrels of 6% gel and then 256 barrels or 1,200 sacks of class A cement with 2% calcium chloride and .250 lb/sk loss circulation material additives, the cement was displaced to 1,313 using a wiper plug chased with 203 barrels of recycled fluid and the casing pressure tested to 500 psi over cement displacement pressure upon the landing of the cement plug with cement returns witnessed to surface inside the cellar. |
| 1933126336 | 2020-10-20 0:00 | PW | No Violations | 0.40 |
| 2035825415 | 2020-2-28 0:00: | PW | No Violations | 1.00 |
| 556908771 | 2018-6-5 0:00:0 | PW | No Violations | 0.30 |
| 974603244 | 2016-12-5 0:00: | DD | No Violations | 1.60 |
For data sources see[10]