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34-111-62495

Well Details

Well ID: 34-111-62495
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Country: United States
State: Ohio
County: Monroe
Municipality: Green Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: FOX-TUBAUGH
License Status: Final Restoration
License Date: 2012-12-13
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.670000
Longitude: -81.000000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Change of Owner 1999-08-23 Operator changed from 3735, CHRISTMAN NOVA A to 4695, P P & G OIL
Change of Owner 2009-11-17 Operator changed from 4695, P P & G OIL to 1634, NORTHWOOD ENERGY CORP
APP 2012-12-13 Proposed Formations:, Issued Date:12/13/2012, Expired Date:12/13/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-03-28
Construction Permit Expires 2014-12-13
Record Last Modified 2019-06-14

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 P P & G OIL 0.00 0.00 365
2009 P P & G OIL 0.00 0.00 365
2010 P P & G OIL 0.00 0.00 365
2011 NORTHWOOD ENERGY CORP 0.00 0.00 0
2012 NORTHWOOD ENERGY CORP 0.00 0.00 0
2013 NORTHWOOD ENERGY CORP 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 P P & G OIL Brine 0 365
2009 NORTHWOOD ENERGY CORP Brine 0 0
2010 NORTHWOOD ENERGY CORP Brine 0 0
2011 NORTHWOOD ENERGY CORP Brine 0
2012 NORTHWOOD ENERGY CORP Brine 20 0
2013 NORTHWOOD ENERGY CORP Brine 63 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1563118393 2013-7-18 0:00: FR No Violations 1.00
1354037880 2012-11-27 Production Wells No Violations Inspection of the well head found 6.625 production casing - 2 tubing and pumping rods with the production valves open and the well set up to be produced by the means of a pumping unit. A 100 barrel and 50 barrel production tank are present on location near the well head. Inspector will note that both Northwood Energy and PP&G are reporting production status on the said well.
1361473617 2013-02-21 Production Wells Violations Noted Inspection found the well idle and not in production with no reported production in the database. A 1 gas line is present running to a domestic meter but has been disconnected and by-passed by what appears to be a adjoining landowner. Well shall be made capable of commercial production within 30 days; or plugging is required within 90 days; Failure to comply may result in forfeiture of bond. Inspector will note that company must obey Division rules pertaining to the 50 set back from the traveled portion of the road way and diking of the tank battery before attempting to place the well into production along with the posting of proper identification. 03/28/2013 The said well has been plugged and the location rough graded in resolving compliance notice.
1364124598 2013-03-22 Production Wells No Violations Notification was made to me by Bill Arnholt that they had applied for and received a plugging permit before I issued the violation against the said well. Mr. Arnholt also stated that they would be moving on to plug the well on Monday. The violation written against the well shall be resolved when the well is plugged.
1364335487 2013-03-26 Plug / Plug Back No Violations Inspector on site to witness the setting of the bottom plug. 1500 of 2 tubing was pulled out of the borehole and the service rig ran in with their stem and jars to check bottom, the tools set down at 1500 and the tubing was ran back in to 1500 and a 500 bottom plug was set. I had the cementers wait and circulate the oil out of the hole that was displaced above the plug to avoid contaminating the surface area. No company or State casing or completion records available.
1364435737 2013-03-27 Plug / Plug Back No Violations Inspector on site 9 hrs setting the plug at the estimated bottom of the surface casing depth, The lower plug was tagged at 837 and a plug was set from 715 to 415. No records State or past company available but known drilling activity indicates that surface is typically set within 300 of Ground Level Elevation, Well location elevation is 800. The 7 surface pipe was attempted to be pulled out of the hole unsuccessfully and was ripped at 240 and pulled out of the hole, 2 tubing was ran in and the surface plug was attempted to be set from 240 to surface with circulation established and no cement returns to surface. After phone conversation with Bill Arnholt later in the day a mutual decision was made to grout the remainder of the open surface hole with a State certified Redi-mix contractor on the proceeding day.
1563118393 2013-07-18 Final Restoration No Violations The well site meets 1509:072.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1361473617 US-OH-110499 2013-03-28 Well shall be plugged
1361473617 US-OH-110500 2013-03-28 Failure to meet well and/or tank battery setbacks from a railroad or roads

For data sources see[7]

References