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34-117-22109

Well Details

Well ID: 34-117-22109
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Country: United States
State: Ohio
County: Morrow
Municipality: Lincoln Township
Operator Name: FISHBURN PRODUCING INC
Well Pad ID:
Farm/Lease Name: POWER
License Status: Active Injection
License Date: 1984-07-09
Spud Date: 1964-09-21
Spud Drilling Contractor:
Final Drill Date: 1964-09-28
Well Total Depth: 3150.00 ft
Configuration: Vertical
Latitude: 40.430000
Longitude: -82.870000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 1381 FISHBURN SERVICES INC
Original Spud 1964-09-21 KB=1916.9', GL=1017.9, LOG TYPE IES.
Completed 1964-09-28 KB=1916.9', GL=1017.9, LOG TYPE IES.
Reached Total Depth 1964-09-28 KB=1916.9', GL=1017.9, LOG TYPE IES.
CO 1984-07-09 1381 FISHBURN SERVICES INC GeoDate 7/9/84
Conversion to Injector 1984-07-09
Salt Water Injection Well 1984-07-09 Issued Date 7/9/84 Expired Date 1/5/85 Acres 0108650 Tool Type RTF Proposed Formation TTREMPEALEAU Proposed Depth 00000 Proposed Drill Depth 00000
Storage Well 1984-07-09 Issued Date 7/9/84 Expired Date 1/5/85 Acres 0108650 Tool Type RTF Proposed Formation TTREMPEALEAU Proposed Depth 00000 Proposed Drill Depth 00000
Construction Permit Expires 1985-01-05 KB=1916.9', GL=1017.9, LOG TYPE IES.
First Injection 1986-10-10 KB=1916.9', GL=1017.9, LOG TYPE IES.
Annulus Pressure Monitoring Approved 1998-04-22 KB=1916.9', GL=1017.9, LOG TYPE IES.
Plugged Back 1998-04-22 KB=1916.9', GL=1017.9, LOG TYPE IES.
Change of Owner 2008-05-23 Operator changed from 1381, FISHBURN SERVICES INC to 3941, FISHBURN PRODUCING INC
Last Compliance Report 2015-06-17 KB=1916.9', GL=1017.9, LOG TYPE IES.
Record Last Modified 2017-10-19 KB=1916.9', GL=1017.9, LOG TYPE IES.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-02 3064 3092 1
3064 3092 1
3064 3092 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 5000 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2004 FISHBURN PRODUCING INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2004 FISHBURN PRODUCING INC Brine 140 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1013587130 2014-12-16 0:00 SW No Violations
-1058018525 2018-3-7 0:00:0 WR No Violations
-1063572179 2018-3-5 0:00:0 WR No Violations
-1069218154 2007-4-11 0:00: SW No Violations
-1101584765 2015-7-20 0:00: SW No Violations
-1167117807 2018-2-27 0:00: WR No Violations
-1178574200 2016-11-30 0:00 SC No Violations
-1198264426 2004-6-23 0:00: SW No Violations
-1230724036 2017-1-31 0:00: SW No Violations
-1323630564 2015-6-16 0:00: WR No Violations
-1407605135 2013-7-3 0:00:0 SW No Violations
-1447398297 2015-6-12 0:00: AM No Violations
-1452134217 2019-4-16 0:00: SW No Violations
-1555389075 2009-2-27 0:00: SW No Violations
-1652238558 2018-4-2 0:00:0 SW No Violations
-1654094679 2005-2-23 0:00: SW No Violations
-1681452290 2018-2-28 0:00: WR No Violations
-1733573140 2008-12-11 0:00 SW No Violations
-1738288428 2013-11-18 0:00 SW No Violations
-1764967798 2020-7-23 0:00: WR No Violations
-1765794718 2020-1-2 0:00:0 SW No Violations
-177972903 2015-5-15 0:00: SW No Violations
-1823760048 2018-1-11 0:00: SW No Violations
-1934545741 2008-6-17 0:00: SW No Violations
-1951171073 2015-9-18 0:00: SW No Violations
-2001039336 2016-1-20 0:00: SW No Violations
-2038979506 2016-4-12 0:00: SW No Violations
-2043248736 2017-9-18 0:00: BH No Violations
-2049086762 2014-6-6 0:00:0 SW No Violations
-2054410500 2017-4-14 0:00: SW No Violations
-2067536710 2007-11-1 0:00: SW No Violations
-2079757969 2019-10-30 0:00 SW No Violations
-2129715135 2018-9-19 0:00: BH No Violations
-30310313 2020-4-8 0:00:0 SW No Violations
-377025592 2020-7-27 0:00: WR No Violations
-388273095 2019-1-15 0:00: SW No Violations
-501955005 2020-7-24 0:00: WR No Violations
-512829788 2014-10-20 0:00 SW No Violations
-548413506 2017-6-22 0:00: SW No Violations
-55853505 2016-12-2 0:00: SC No Violations
-570593019 2010-9-22 0:00: SW No Violations
-664330799 2012-8-21 0:00: SW No Violations
-716330206 2003-5-21 0:00: SW No Violations
-74799573 2016-2-19 0:00: SW No Violations
-772707845 2017-2-15 0:00: SW No Violations
-791835804 2015-5-26 0:00: AM No Violations
-865870310 2014-4-28 0:00: SC No Violations
-884509454 2018-6-27 0:00: SW No Violations
-889024558 2003-3-28 0:00: SW No Violations
-902119672 2006-12-11 0:00 SW No Violations
-935553372 2005-5-5 0:00:0 SW No Violations
-944855962 2015-12-8 0:00: SW No Violations
-988515072 2012-2-23 0:00: SW No Violations
00001229i3 2001-01-12 Salt Water Injection Well No Violations On site to witness the installation of the tubing and packer.
001287i101 2001-06-25 Salt Water Injection Well No Violations test injection pressure
0031873699 2002-08-19 Salt Water Injection Well No Violations Chk well and storage, OK. Needs some clean up around the storage site.
0055853505 2016-12-02 Surface Facility Construction No Violations Inspect construction activities for increasing the capacity of the secondary containment. The operator has constructed the containment and the crew is repairing the exiting tears in the HDPE liner.
0074799573 2016-02-19 Salt Water Injection Well No Violations Inspect well and measure injection pressure for annulus and injection line.
0078785879 2018-08-28 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
0098338905 2014-01-17 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) as part of a standard injection well status check. Check well, pressures, storage, vault and identification. No change in status from previous inspection.
0145239891 2015-10-29 Salt Water Injection Well No Violations Inspect location and measure storage dike area with Jennifer Gingras.
0147925612 2011-05-10 Salt Water Injection Well No Violations Check well and storage, Ok.
0167887326 2014-07-08 Salt Water Injection Well No Violations Inspected the Power Fegley #1 (SWIW #51) as part of a standard injection well status check. Inspect well, storage and identification. Status: ok.
0177972903 2015-05-15 Salt Water Injection Well No Violations Received notification from the operator that the well has a hole in the tubing. Well currently shut-in, service rig is on the well preparing to pull tubing and packer for replacement.
0273814035 2014-09-05 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: ok.
0298389027 2007-03-29 Salt Water Injection Well No Violations Inspect well.
0331643279 2010-05-10 Salt Water Injection Well No Violations Chk well and storage ok. Has positive pressure on the annulus but not enough to measure.
0332687232 2009-06-25 Salt Water Injection Well No Violations No one at the site, rig not repaired yet.
0387655574 2013-03-13 Salt Water Injection Well No Violations Inspect well and tanks. Measure storage tank dike area. One 120 bbl tank, and two 280 bbl lay down horizontal tanks.
0402752551 2012-05-21 Salt Water Injection Well No Violations Inspect Well. Operators gauge reads 14 inches Hg.
0439851774 2008-05-29 Salt Water Injection Well No Violations Chk well and storage, Ok.
0444861437 2013-02-01 Salt Water Injection Well No Violations Inspected the Powers (#2109) (SWIW#51) as part of a standard SWIW status check. Well identification and Emergency contact information is clearly marked at the well, but absent on the storage. No trespassing signs are posted. Contact Donny with Fishburn regarding the well identification.
0508043715 2018-01-19 Salt Water Injection Well No Violations The operator was on location, by request, to attempt to conduct an mechanical integrity test on the well. The operator replaced the well head valve and nipple for the annulus. And, reported there was a small hole in the body of the old valve. Attempted to load the annulus with fresh water but due to the recent extreme cold the water froze on contact and the testing process was not valid. The operator will test the well when the weather conditions are conducive. The well is currently shut in and not in operation.
0508939547 2005-08-05 Salt Water Injection Well No Violations Chk well and storage, pit liner has been put down and gravel has been spread over top of it. New oil storage tanks have been delivered but not installed yet.

The well is not in operation yet.

0512829788 2014-10-20 Salt Water Injection Well No Violations Inspect well for integrity and pressure. The Operators Injection gauge indicates -18 in-Hg.
0521328944 2007-01-31 Salt Water Injection Well No Violations Inspect well.
0530400803 2017-10-05 Salt Water Injection Well No Violations Injection well status check. Status: ok.
0548413506 2017-06-22 Salt Water Injection Well No Violations Inspect surface facility.
0570593019 2010-09-22 Salt Water Injection Well No Violations Check well and storage.
0607167231 2004-10-29 Salt Water Injection Well No Violations Chk well and storage, Ok.
0614444204 2018-03-20 Salt Water Injection Well No Violations Inspect well for integrity.
0652621629 2004-08-17 Salt Water Injection Well No Violations Chk well and storage, Ok. New storage tank installed.
0664330799 2012-08-21 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) with Mr. Jeff Fry as part of a status check. Backside pressure 60 psi, injection -28 on vacuum.. Well identification is displayed at the storage. The dike contains one green 210 barrel tank and two green horizontal tanks. The facility is commingled with the Powers #4 (#2230) containing one green 210 tank (#37706) and a brine tank. Inspected Fishburn brine hauler (PFX-4553) while unloading brine from (#3972) Benington township, inspect log book status OK.
0716330206 2003-05-21 Salt Water Injection Well No Violations Chk well and stoarge,Ok.
0772707845 2017-02-15 Salt Water Injection Well No Violations Operator reported they conducted the monthly inspection and pressured up the well the previous day. Inspect well and measure pressures.
0791835804 2015-05-26 Administrative Inspection No Violations The tubing and packer have been removed. Contacted by operator to report the well was being swabbed for removal of iron sulfide deposits from the borehole.
0792016887 2014-11-07 Administrative Inspection No Violations Visit location with Regional Supervisor William Ziegler and Assistant Director Fred Shimp.
0815624400 2005-03-30 Salt Water Injection Well No Violations Chk well and storage, Ok.
0865870310 2014-04-28 Surface Facility Construction No Violations The operator has moved their crane off location. Status: will continue to monitor repairs.
0884509454 2018-06-27 Salt Water Injection Well No Violations Standard operations site visit with NW Emergency Response Manager Mr. Andrew Adgate.
0889024558 2003-03-28 Salt Water Injection Well No Violations Chk well and storage, Ok.
0902119672 2006-12-11 Salt Water Injection Well No Violations Inspected this well location with Tom Benko. There was 0 psi on the injection and 160 psi on the annulus. There was proper identification posted, however the id at the wellhead was badly faded.
0906770254 2018-09-05 Brine Hauler No Violations The operators brine truck was on location evacuating water from the dike containment because the dresser sleeve failed. There was not any brine that was released out of the secondary containment.
0915448926 2016-07-26 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
0935553372 2005-05-05 Salt Water Injection Well No Violations Chk well and storage ok. The well is shut in untill new storage facilities are installed.
0944855962 2015-12-08 Salt Water Injection Well No Violations Inspect well and tanks. Measure injection pressure and tubing pressure.
0988515072 2012-02-23 Salt Water Injection Well No Violations Inspect Well.
1013587130 2014-12-16 Salt Water Injection Well No Violations Inspect well. Site is ok.
1029928261 2012-10-23 Salt Water Injection Well No Violations Inspected the Power #1 (#2109) (SWIW #51) as part of a standard injection well status check. Injection: -35 Annulus: 63 psi. Well identification and storage OK.
1045072978 2017-09-06 Salt Water Injection Well No Violations Inspect well for pressure and integrity.
1058018525 2018-03-07 Work Over Reconditioning No Violations Service rig is on the well. The Baker Hughes Model AD-1 Tension packer has been set using 91 lined joints of tubing and two un-lined joints of tubing. There are no inserts to protect the collars. The wellhead valves have been replaced. The annulus was loaded with fresh water, the packer was set, the wellhead was assembled. The annulus was pressured up to 400 psi and tested for 15 minutes with no pressure loss. The well passes the mechanical integrity test. The operator was notified he can put the well into operation.
1063572179 2018-03-05 Work Over Reconditioning No Violations Service rig is on the well. The operator ran in the hole with the Baker Hughes Model AD-1 Tension packer. Using 91 lined joints of tubing originally installed in 2015 and two un-lined joints of tubing. There are no inserts installed or available to protect the collars for this pipe. The packer failed to set properly.
1068122575 2015-05-18 Administrative Inspection No Violations Contacted by operator to report the tubing and packer were removed from the well and a hole was located in four joints from the bottom of the tubing string.
1069218154 2007-04-11 Salt Water Injection Well No Violations Horizontal storage tank farthest north is starting a drip leak at bottom connection of sight tube. Vault may need emptied, pad has fluid on it fresh water, not sure if full or drain plugged off. Well was -26 in hg, and 160 psi. on annulus. Tank dike has s
1101584765 2015-07-20 Salt Water Injection Well No Violations Check secondary containment water for chloride content: 352 ppm
1116954339 2014-09-15 Salt Water Injection Well No Violations Inspect tank battery. Identification at tanks has faded. Contacted pumper in person to update identification. An unidentified person has vandalized the storage tank dike liner with a shovel. It appears someone was attempted to thief the gravel placed over the liner. In the process punched through the line twice with a shovel outside of the dike. Then they subsequently vacated the premises.
1147454900 2013-05-16 Surface Facility Construction No Violations Inspected facility. The location looked like the flow line had been replaced recently. Contacted operator and confirmed that flow line had been replaced with 150 lb test plastic line about 30 days prior. Conducted flow line pressure test. Tested at 100 psi for fifteen minutes. With less than 4 percent pressure loss. Line test passed.
1159381165 2006-09-27 Salt Water Injection Well No Violations Chk well and storage, new well head fittings and gages. Storage site is in good condition at this time. How ever some water from recent rain is in the vault and diked area, it should be removed to retain the spill prevention capacity
1167117807 2018-02-27 Work Over Reconditioning No Violations Service rig is on the well. The operator removed the tubing and packer from the well. The packer will be cleaned and a new rubber ordered for replacement.
1170740441 2014-05-21 Brine Hauler No Violations Inspect Fishburn Services brine truck unloading brine at the Power #1 (SWIW #51) disposal well. Truck #115, license number (OH) PHK-9986. Brine UIC #25-03 and other identification clearly and properly displayed. Status: ok.
1178208902 2007-05-03 Salt Water Injection Well No Violations Repairs have beem made that were requested on previous inspection. Did not check well
1178574200 2016-11-30 Surface Facility Construction No Violations The operator has uncovered and pealed back the existing 30 mill liner along the existing dike to modify and increase secondary storage containment capacity. Five foot long 2 3/8 inch pipes were driven into the crown of the existing dike and 2x8 boards with tong and groove were installed to increases the dike wall. The existing liner will be repaired where torn and attached to the top most board with a baton. The exposed liner will be painted with a truck bed liner to protect the HDPE liner from ultraviolet rays.
1182213118 2013-07-02 Brine Hauler No Violations Inspect Fishburn brine truck #118 (Earl) unloading brine from the Barton Fishburn well. 1985 Mack PBG-5537, UIC identification and BRINE clearly marked.
1198264426 2004-06-23 Salt Water Injection Well No Violations Chk well and storage. Moving old tank and preparing to install new ones.
1205242773 2008-03-11 Salt Water Injection Well No Violations Chk well and storage, Ok.
1220535783 2008-09-04 Salt Water Injection Well No Violations Chk well and storage, Ok.
1229i3 2001-1-12 0:00: SW No Violations
1230724036 2017-01-31 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
1234437383 2018-02-15 Salt Water Injection Well Violations Noted Inspect well for integrity and pressure. The Operator was on location to perform a mechanical integrity test on the well. The operator loaded the well with six to seven barrels of water, Then pressured up the well. The pressure on the annulus gradually bled off. The operator dug up the 8 inch surface casing well head. There were no fluids present on the 8 inch well head. The well failed the mechanical integrity test. The well is shut in. The operator will mobilize the service rig to further evaluate the well conditions.
1245851021 2009-06-24 Salt Water Injection Well No Violations On site to witness MIT. Found a hole in the tubing and a hole in the 4.5 inch casing. Unscrewed the casing at 1048 foot. Ran different casing back in. Reconnected to the casing in the hole, set it back on the slips. Started a rebuilt Halliburton R-4 packer in to the well and the rig broke down. Shut down for the day
1247765000 2009-07-16 Salt Water Injection Well No Violations Put in 5bbl of acid and loaded the hole with salt water. The well would not take fluid. Pulled the tubing and packer. Cleaned the well out with a drill bit to the total depth. Put in another 5bbl of acid and opened the perforations, the well went on vacuum. Ran the tubing and packer back in.
1248101893 2009-07-17 Salt Water Injection Well No Violations Ran tubing and packer in to 2980. Load the annulus with 40 bbl fresh water and 5 gal of rust inhibitor. Set the packer and pressure up to 500 psi, with 0 psi loss after 15 minute test.
Past test
1255444982 2009-10-13 Salt Water Injection Well No Violations Chk well and storage, OK. Has positive pressure but not enough to measure.
1261162259 2009-12-18 Salt Water Injection Well No Violations Check well and storage, ok. Has positive pressure on annulus but not enough to measure.
1269867092 2010-03-29 Salt Water Injection Well No Violations Chk well and storage, ok. Annulus has positive pressure but not enough to measure.
1284189289 2017-07-27 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
1287i101 2001-6-25 0:00: SW No Violations
1297350269 2011-02-10 Salt Water Injection Well No Violations The site is snow covered at this time. Approx temp 2 degrees F. the valves on the annulus are frozen, could not check annulus pressure.
1301421606 2011-03-29 Salt Water Injection Well No Violations Check well and storage, Talk briefly with Roy Underwood (pumper).

Has positive pressure on annulus but not enough to measure.

1307262011 2013-09-30 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) as part of a standard injection well status check. Check well, storage, vault and identification. No change in status from previous inspection. Status: ok.
1312415153 2010-08-02 Salt Water Injection Well No Violations Check well and storage, annulus has positive pressure but not enough to measure. Has a small pit by the well head. Needs to be closed.
1323630564 2015-06-16 Work Over Reconditioning No Violations Inspect well and pressure test annulus to put well back into production. Trapped air was bled off and annulus loaded with water and pressure up to 505 psi and tested for 15 minutes, total loss of 10 psi. The well passed and was within the 5% margin. Well was put into production.
1328047561 2012-01-31 Salt Water Injection Well No Violations Site inspection with Jeff fry and Will Ziegler, good tank ID.
1329179173 2012-01-31 Salt Water Injection Well No Violations During this inspection I was accompanied by Jeff Fry and Will Ziegler. We tested the pressure on this well and it read vacuum over 60 psi. The ID is posted at the well.
1344642280 2011-09-27 Salt Water Injection Well No Violations Inspect well. No identification at tank. Identification faded at well head.
1363270303 2013-03-14 Salt Water Injection Well No Violations On site by request from Inspector Benko to retrieve tank measurements. Fishburn Producing has posted the well identification and emergency contact information for the disposal well at the storage as requested. Status: ok.
1368638843 2013-05-15 Brine Hauler No Violations Inspected Fishburn brine hauling brine from his own wells. License number PFX 4553. UIC number and BRINE clearly identified.
1372857345 2013-07-03 Salt Water Injection Well No Violations Inspection of the storage after a Fishburn truck unloaded revealed a leak at the back plate on the unloading tank. Called Fishburn (Chuck Freeman) who came to location. Temporarily plugged hole and called vac truck to remediate brine which was contained to the dike. Fishburn plans to replace back plate and also fix a leak noted at a union on the input line. Status: will continue to monitor.
1373295955 2013-07-08 Salt Water Injection Well No Violations The injection well is currently out-of-service to repair leaks which developed at the storage tank and input line. Status: will continue to monitor.
1373916508 2013-07-15 Salt Water Injection Well No Violations The operator has repaired the storage leaks and the well has been placed back into injection. Status: ok.
1375206410 2013-07-30 Salt Water Injection Well No Violations Horizontal laydown tank in the storage had a valve failure. Brine and residual crude spilled into the storage dike. The well is shut-in and clean up has begun. Release was contained to the lined storage dike. Status: will continue to monitor.
1376496534 2013-08-14 Salt Water Injection Well No Violations The operator is hot water flushing the dike and tanks to clean up from the recent tank failure. Status: ok.
1379700041 2013-09-20 Salt Water Injection Well No Violations Inspected the Powers #1 (SWIW #51) as part of a standard injection well status check. Check well, storage, vault identification. No change in status from previous inspection. Status: ok.
1395413008 2014-03-21 Production Wells No Violations Inspected the Powers #1 (SWIW #51) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: ok.
1398368134 2014-04-24 Surface Facility Construction No Violations The operator is currently in the process of repairing and resetting the two horizontal storage tanks. The northern tank has been raised by the addition of one row of railroad ties for a total of two (to keep tank out of water). The lover valve threads on both sides have been replaced and reinforced patch welded. Status: will continue to monitor storage facility repairs.
1400267612 2014-05-16 Surface Facility Construction No Violations The operator has finished replacing the valves on the second horizontal tank.
1407605135 2013-07-03 Salt Water Injection Well No Violations Inspect injection well pressures. Status: ok.
1415309401 2014-11-06 Administrative Inspection No Violations Visit location accompanied by Northwest Regional Supervisor William Ziegler.
1418893521 2008-01-17 Salt Water Injection Well No Violations Chk well and storage, Ok.
1426780105 2015-03-13 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: ok.
1430267604 2004-04-23 Salt Water Injection Well No Violations Chk well and storage. On site removing and cutting up old storage tanks in preperation to install new ones.
1447398297 2015-06-12 Administrative Inspection No Violations Contacted operator. Operator is finishing cleaning out well bore. Required drilling out iron sulfide accumulations and sand pump swabbing well. Acid was used to assist in cleaning out the well.
145239891 2015-10-29 0:00 SW No Violations
1473805246 2015-06-15 Work Over Reconditioning No Violations Inspect tanks and well. Service rig on well. Operator pulled packer and tubing. Two holes in the tubing were observed in the original pipe string. Used upset 2 3/8 inch 4.75 lb./ft., J55, 8 round, lined pipe tested to 7,000 psi was installed with a Baker packer set at 2973 feet on tension with 13,000 pounds pull over string weight. Total string weight and pull set at 23,000 pounds tension. Top of perforations are at 3065 feet, top of cement is 2373 feet.
147925612 2011-5-10 0:00: SW No Violations
1483550745 2017-01-03 Surface Facility Construction No Violations Inspect secondary storage containment surface facility and tank battery. Approval has been granted for the modifications to be made to the surface facility. Construction of the secondary containment system have been completed and meet the modification requirements. The tanks are in place. Final flow line connections have not been installed at the time of this inspection. The Compliance notice of November 15, 2016 has been resolved.
1539623490 2018-10-03 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
1555389075 2009-02-27 Salt Water Injection Well No Violations Chk well and storage, ok.
1583376732 2018-03-02 Work Over Reconditioning No Violations Service rig is on the well. The operator is working on testing the tubing and replacing collars that have visual corrosion.
1595441232 2019-7-16 0:00: SW No Violations
1597758090 2020-7-13 0:00: WR No Violations
1597758285 2020-7-16 0:00: WR No Violations
1598979995 2020-9-1 0:00:0 SW No Violations
1605788508 2014-01-24 Salt Water Injection Well No Violations Location Information. ENTRANCE: Lat. 40.43750 Long. -82.87375 / WELL HEAD: Lat. 40.43948 Long. -82.87334 / CENTER-OF-STORAGE: Lat. 40.43766 Long. -82.87409.
1623086127 2006-02-03 Salt Water Injection Well No Violations Chk well and storage, Ok.
1652238558 2018-04-02 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
1654094679 2005-02-23 Salt Water Injection Well No Violations Chk well and storage, Ok. The well has not been used for a time now, the storage thanks have been removed. MrFishburn is intending to install different tanks and use the well.
1655310151 2013-12-18 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) as part of a standard injection well status check. Check well, pressures, storage, vault and identification. No change in status from previous inspection. Status: ok.
1671030894 2005-12-22 Salt Water Injection Well No Violations Chk well and storage, Ok.
167887326 2014-7-8 0:00:0 SW No Violations
1681452290 2018-02-28 Work Over Reconditioning No Violations Service rig is on the well. The operator tested the tubing string for integrity and leaks. A Halliburton R-4 packer was installed with a seating nipple in line. A standing valve was set into the seating nipple to allow the tubing string to be loaded with water and pressured tested the tubing. The annulus was also tested to evaluate the condition of the casing. Approximately 20 joints of pipe were run in the hole, the packer was set, loaded with water, and pressure tested. When the tubing successfully held pressure, about 20 more joints of pipe were added and the process was repeated, until a failure. Upon a test failure the operator removed one joint at a time to test and evaluate. This process identified a collar with a hole and one joint of tubing with a hole.
1696303797 2003-09-24 Salt Water Injection Well No Violations Chk well and storage, Ok.
1731269602 2018-06-18 Salt Water Injection Well No Violations Inspect well for pressure and integrity.
1733573140 2008-12-11 Salt Water Injection Well No Violations Check well and storage, Ok.
1738288428 2013-11-18 Salt Water Injection Well No Violations Inspected the Powers #1 (SWIW #51) as part of a standard injection well status check. Check well, pressures, storage, vault and identification. Status: ok.
1738717071 2016-10-12 Salt Water Injection Well No Violations Inspect well for integrity and pressure. The tubing has vacuum.
1783469348 2003-07-15 Salt Water Injection Well No Violations Chk well and storage, Ok.
1823760048 2018-01-11 Salt Water Injection Well No Violations Inspect well for integrity and pressure. The tubing and annulus are on vacuum. Contacted operator by phone to scheduled a mechanical integrity test to evaluate the condition of the well. This test will be conducted when the temperature are above subfreezing conditions. The well is currently not being used.
1841302590 2016-11-15 Salt Water Injection Well Violations Noted Inspect tank battery. The 210 bbl tank was reported to have a leak at the manway hatch. The 210 bbl tank has been removed from the dike area. A new fiberglass 300 bbl replacement tank has been delivered to the site. Installation has not occurred. The operator is required to verify the containment volume of the existing dike area and prepare an updated containment diagram prior to installation of the new tank.
1843951843 2005-08-05 Salt Water Injection Well No Violations Chk well and storage, Ok.
1880973034 2018-03-06 Work Over Reconditioning No Violations Service rig is on the well. The packer and tubing were run in the hole and failed to set. The tubing and packer were tripped out of the hole. The set screw for the J channel was loose and did not allow the slips to properly set. The Baker Hughes Model AD-1 Tension packer was run in the hole again. Using 91 lined joints of tubing originally installed in 2015 and two un-lined joints of tubing. There are no inserts installed or available to protect the collars for this pipe. The annulus was circulated with fresh water, the packer was set. The well head and valves had leaks.
1897758172 2014-05-20 Salt Water Injection Well No Violations Inspect well and tanks. The tanks have been repaired with new fittings. The welds for the fitting on the south tank are leaking. Identification sigh is posted. The current information has not been marked on the sign. Contacted operator to identify issues.
1901405583 2017-11-01 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
1934346206 2013-07-03 Salt Water Injection Well No Violations On site to perform EM survey with Tom Tomastik to investigate possible brine release in the adjacent farmers field.
1934545741 2008-06-17 Salt Water Injection Well No Violations Chk well and storage, Ok.
1951171073 2015-09-18 Salt Water Injection Well No Violations Inspected the Powers #1 (SWIW #51) as part of a standard injection well status check. Check well, pressures, storage and identification. Status: ok.
1994145848 2016-12-16 Surface Facility Construction No Violations Inspect completed modifications activities on the secondary containment dike and liner. The dimensions for the secondary containment are 32 feet by 45 feet by 40 inches in height.
2001039336 2016-01-20 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
2038979506 2016-04-12 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
2043248736 2017-09-18 Brine Hauler No Violations Inspect Fishburn Services Inc. brine truck. Driver log and placarding are incompliance. Collect water sample to measure specific gravity at 1.13 units or 9.33 pounds per gallon. Source water is the; 3411722028; Fisher #1.
2049086762 2014-06-06 Salt Water Injection Well No Violations Inspected the Power #1 (SWIW #51) as part of a standard injection well status check. Inspect well, pressures, storage, vault and identification. Status: ok.
2054410500 2017-04-14 Salt Water Injection Well No Violations Inspect well for integrity and pressure.
2067536710 2007-11-01 Salt Water Injection Well No Violations Chk well and storage, Ok. No pressure on the annulus at this time.
2075980660 Salt Water Injection Well No Violations Chk well and storage, Ok.
2085157901 2018-02-08 Salt Water Injection Well No Violations Inspect well for integrity and pressure. The tubing has 10 psi and annulus is on vacuum. The operator is scheduled to conduct a pressure test when the temperature are above subfreezing conditions.
2129715135 2018-09-19 Brine Hauler No Violations Inspect Fishburn Services brine truck #114 (Dana) unloading at disposal well. UIC number (#25-003), BRINE and other identification properly displayed. Unloading water from the Graham #1869. Status: ok.
2132435813 2014-04-29 Salt Water Injection Well No Violations Inspect tank battery. Operator is installing new valves on horizontal tanks and increasing the cribbing height.
2135442408 2014-07-30 Salt Water Injection Well No Violations Inspect well for integrity and pressure. The tanks have been repaired. The concrete heater-treater base has been excavated and removed from the site.
273814035 2014-9-5 0:00:0 SW No Violations
298389027 2007-3-29 0:00: SW No Violations
300196829 2019-4-25 0:00: BH No Violations
31873699 2002-8-19 0:00: SW No Violations
331643279 2010-5-10 0:00: SW No Violations
332687232 2009-6-25 0:00: SW No Violations
387655574 2013-3-13 0:00: SW No Violations
402752551 2012-5-21 0:00: SW No Violations
439851774 2008-5-29 0:00: SW No Violations
444861437 2013-2-1 0:00:0 SW No Violations
508043715 2018-1-19 0:00: SW No Violations
508939547 2005-8-5 0:00:0 SW No Violations
521328944 2007-1-31 0:00: SW No Violations
530400803 2017-10-5 0:00: SW No Violations
607167231 2004-10-29 0:00 SW No Violations
614444204 2018-3-20 0:00: SW No Violations
652621629 2004-8-17 0:00: SW No Violations
78785879 2018-8-28 0:00: SW No Violations
792016887 2014-11-7 0:00: AM No Violations
815624400 2005-3-30 0:00: SW No Violations
906770254 2018-9-5 0:00:0 BH No Violations
915448926 2016-7-26 0:00: SW No Violations
98338905 2014-1-17 0:00: SW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1234437383 US-OH-106274 2018-03-26 9-3-07(H) Mechanical failure/contamination
1841302590 US-OH-118389 2017-01-20 9-3-08(B) Tanks not liquid tight/Improper burial

For data sources see[9]

References