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34-117-24034

Well Details

Well ID: 34-117-24034
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Country: United States
State: Ohio
County: Morrow
Municipality: Franklin Township
Operator Name: EDCO DRILLING & PRODUCING
Well Pad ID:
Farm/Lease Name: HICKSON
License Status: Final Restoration
License Date: 2000-11-03
Spud Date: 1991-08-16
Spud Drilling Contractor: LBJ DRILLING
Final Drill Date: 1991-08-21
Well Total Depth: 3645.00 ft
Configuration: Vertical
Latitude: 40.530000
Longitude: -82.770000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1991-05-09 Issued Date 5/9/91 Expired Date 5/8/92 Acres 0020000 Tool Type RTF Proposed Formation TREMPEALEAU Proposed Depth 03645 Proposed Drill Depth 03645
Original Spud 1991-08-16 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012
Completed 1991-08-21 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012
Reached Total Depth 1991-08-21 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012
Completion Report Received 1991-08-29 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012
CO 1991-09-01 1987 DUBLIN ENERGY CORP. GeoDate 5/9/91
Plugged/Abandoned 1992-05-14 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012
CO 1994-08-10 254 EDCO DRILLING & PRODUCING GeoDate 5/9/91
APP 2000-11-03 Proposed Formations:TREMPEALEAU, Issued Date:11/3/2000, Expired Date:11/3/2001 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2001-11-03 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012
Record Last Modified 2017-02-15 WELL STATUS BASED ON INSPECTOR ERIC DAUGSTRUP'S REPORT 09/19/2012

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3534 3565 124
3552 0
1997-06-29 3552 0
3534 3565 124
3534 3565 124

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 500 Gal 0 ACIDIZED W/500 GAL MUD ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 EXPLORE ENERGY CORP. 208.00 1118.00 115
1992 EXPLORE ENERGY CORP. 64.00 1357.00 345
1993 EXPLORE ENERGY CORP. 0.00 733.00 290
1994 EXPLORE ENERGY CORP. 0.00 273.00 170
1995 EDCO DRILLING & PRODUCING 0.00 357.00 365
1996 EDCO DRILLING & PRODUCING 0.00 190.00 60
1997 EDCO DRILLING & PRODUCING 0.00 139.00 365
1998 EDCO DRILLING & PRODUCING 0.00 139.00 90
1999 EDCO DRILLING & PRODUCING 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 EXPLORE ENERGY CORP. Brine 680 115
1992 EXPLORE ENERGY CORP. Brine 1096 345
1993 EXPLORE ENERGY CORP. Brine 875 290
1994 EXPLORE ENERGY CORP. Brine 465 170
1995 EDCO DRILLING & PRODUCING Brine 615 365
1996 EDCO DRILLING & PRODUCING Brine 56 60
1997 EDCO DRILLING & PRODUCING Brine 681 365
1998 EDCO DRILLING & PRODUCING Brine 0 90
1999 EDCO DRILLING & PRODUCING Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000005978 Preliminary Restoration No Violations PASSED Y WITNESSED 5/14/92 INSPECTOR FAUST, SAMUEL E. DATE 05/1419/92 DATA FROM OLD VAX INFO
1287i43519 2001-05-17 Plug / Plug Back No Violations FINISH PLUG JOB / 4.5 PIPPED SET LIME PLUG
1287i4351955 2001-5-17 0:00: PB No Violations
1764299812 2014-07-01 Final Restoration No Violations Inspected the Hickson #1 (#4034) as a standard final restoration inspection. Crops are currently growing at the well spot, no visual evidence of production equipment, debris or roads. Status: final restoration complete.
1769810339 2012-09-19 Field Inspected, Well Not Found No Violations Inspected the Hickson #1 (#4034) as a standard productive well status check. The well does not exist and a previous inspection report Rocky King reports finishing plug job (no plug job on file). Called Mike Williams geologist (Columbus office) to change status.
5978 PL No Violations

For data sources see[9]

References