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34-119-24153

Well Details

Well ID: 34-119-24153
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Country: United States
State: Ohio
County: Muskingum
Municipality: Monroe Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: FRENCH RAY ETAL
License Status: Producing
License Date: 1977-12-28
Spud Date: 1978-02-17
Spud Drilling Contractor:
Final Drill Date: 1978-02-26
Well Total Depth: 4347.00 ft
Configuration: Vertical
Latitude: 40.090000
Longitude: -81.770000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-12-28 84 EVERFLOW EASTERN PTNS L P GeoDate 12/28/77
Original Spud 1978-02-17
Completed 1978-02-26
Reached Total Depth 1978-02-26
Construction Permit Expires 1978-12-28
CO 1994-08-29 1333 BARR ROBT/dba BIG SKY PET GeoDate 12/28/77
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4262 4304 7
4262 4304 7
4262 4304 7

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1290 Bbl 55000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 EVERFLOW EASTERN PARTNERS LP 4615.00 0.00 365
1986 EVERFLOW EASTERN PARTNERS LP 3698.00 0.00 365
1987 EVERFLOW EASTERN PARTNERS LP 2839.00 0.00 365
1988 EVERFLOW EASTERN PARTNERS LP 1550.00 0.00 365
1989 EVERFLOW EASTERN PARTNERS LP 2531.00 0.00 365
1990 EVERFLOW EASTERN PARTNERS LP 3325.00 160.00 365
1991 EVERFLOW EASTERN PARTNERS LP 1788.00 0.00 365
1992 EVERFLOW EASTERN PARTNERS LP 433.00 0.00 365
1993 EVERFLOW EASTERN PARTNERS LP 507.00 0.00 365
1994 EVERFLOW EASTERN PARTNERS LP 403.00 0.00 365
1995 EVERFLOW EASTERN PARTNERS LP 0.00 0.00 365
1996 EVERFLOW EASTERN PARTNERS LP 0.00 0.00 365
1998 BIG SKY ENERGY INC 195.00 0.00 365
2000 BIG SKY ENERGY INC 2409.00 70.00 365
2001 BIG SKY ENERGY INC 2823.00 87.00 365
2003 BIG SKY ENERGY INC 3324.00 126.00 365
2004 BIG SKY ENERGY INC 1967.00 0.00 365
2005 BIG SKY ENERGY INC 2677.00 87.00 365
2006 BIG SKY ENERGY INC 2170.00 0.00 365
2007 BIG SKY ENERGY INC 0.00 82.00 365
2008 BIG SKY ENERGY INC 2036.00 156.00 365
2009 BIG SKY ENERGY INC 5361.00 0.00 365
2011 BIG SKY ENERGY INC 4290.00 0.00 365
2012 BIG SKY ENERGY INC 442.00 49.00 366
2013 BIG SKY ENERGY INC 0.00 0.00 250
2014 BIG SKY ENERGY INC 0.00 0.00 250
2016 BIG SKY ENERGY INC 0.00 0.00 0
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1986 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1987 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1988 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1989 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1990 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1991 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1992 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1993 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1994 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1995 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1996 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1998 BIG SKY ENERGY INC Brine 0 365
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 1787 365
2008 BIG SKY ENERGY INC Brine 0 365
2009 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 250
2014 BIG SKY ENERGY INC Brine 0 250
2016 BIG SKY ENERGY INC Brine 0 0
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1208378422 2020-7-6 0:00:0 PW No Violations 0.50
-1222786684 2016-6-10 0:00: AM No Violations 0.50
-179200595 2014-11-5 0:00: PW No Violations 1.00
-1896613083 2015-5-4 0:00:0 PW No Violations 1.00
-1952316010 2006-12-7 0:00: PW No Violations
-378091605 2005-4-26 0:00: PW No Violations
-983929526 2014-6-30 0:00: PW No Violations
0103247542 2014-03-14 Administrative Inspection No Violations I called Greg Hendreson of Big Sky Energy by phone at 3-14-14 at 12:18pm. He said that they are planning to get packer and 2.875tubing to run in well due to the hole in 4.5 casing. I stated that well needs fixed due to the complaint made by Guy French on complaint #3873.
0179200595 2014-11-05 Production Wells No Violations Rig has 4.5casing hanging in elevators. The casing is setting in the slips and bowl. No one at the rig at the current time.
0321451627 2016-06-07 Production Wells No Violations The purpose of my inspection is due to a follow-
0378091605 2005-04-26 Production Wells No Violations All messes cleaned up flowline repaired ID on tank Very impressive
0754908296 2014-06-26 Administrative Inspection No Violations Guy French the land owner called with an update that Big Sky was having WCS move equipment in to start work but took the equipment back out. The site is very soft in the field.
0869082305 2015-07-22 Production Wells No Violations The well is sitting open with the 8.625casing in the ground. Approximately 900of 4.5casing has been pulled out and there has been a rock or ledge that has slid across the casing. This will not allow to get back down in the casing. The rods and tubing are laying on the ground. The rig is still set up over the well bore. The company has lost the rig operator and the crew. I called Bob Barr on trying to get the well back into Production or Plugging the well. He said he would contact a company to get the work performed. The surface water will enter the 8.625casing when it rains profusely.
0943958070 2004-07-14 Production Wells No Violations
0983929526 2014-06-30 Production Wells No Violations I stopped by well site to inspect the area where Big Sky started to move the equipment in. They were getting truck and trailers stuck so they decided to move to the Powelson well api#119-23897.
103247542 2014-3-14 0:00: AM No Violations
1112879032 2005-04-07 Production Wells Violations Noted
1222786684 2016-06-10 Administrative Inspection No Violations The purpose of this Administrative Inspection is per Chiefs Order #2016-194. Greg Henderson with Big Sky Energy called and stated that the well had been addressed and is sufficiently closed up with the necessary equipment. The well is isolated from the ground water infiltration. He also texted me with a picture of the well head. There is a picture on file.
1267673400 2012-11-20 Administrative Inspection No Violations I called Bob Barr on well. He stated that all production has been turned in on wells. The form 10 was filed and should be in with in 2 weeks. The down hole issue is there and needs a 2 7/8 upset tubing string on a packer so 1.5tubing can be ran inside. Bob also stated that this might be 2 months before he can get to it.
1289349813 2012-07-10 Production Wells Violations Noted On day of inspection well was called in by Guy French. The landowner claims that well was producing and stated water has come into the well. The gas from well is the main source of heat and cooking. I called pumper Greg Henderson and he stated that he told the landowner of an alternative source of heat would be needed because well would be down. Upon farther investigation the company has not been reporting production for 2010 to present. By date of remedy come up with plan of getting violations in compliance.
1307450483 2014-10-29 Production Wells No Violations Well is being worked on by CWS. The rig will have to pull two sections of broke 4.5casing out with a spear. Then go in and run over shot in and casing cut the 4.5off at 1200. Then run in with overshot over the cut and run tubing and packer in. This will get well into production.
1353428851 2012-11-20 Production Wells No Violations Well is capable but is shut-in. There has been no production records filed since 2009. Well has down hole problems. I met Guy French and he stated that he does not have gas at all. He has had to purchase propane for heat. I stated that you always need a second source of heat in case of such a problem. I will call Bob Barr.
1370540557 2013-06-06 Production Wells No Violations Per request of landowner Guy French made the original complaint. Jesse Dodds and I met with Guy and looked at well and site. There has been no change and Greg Henderson told complainant not to call him anymore. I took updated pictures.
1413996276 2014-10-22 Production Wells No Violations Roger Barr of CWS was pulling 2.375tubing out of the well. He had a knife on the tubing trying to get the cable down the hole. The well had had problems with a hole of an unknown depth in the 4.5casing. Jet wire line was hired to run in and find the hole and pop the pipe with primer cord. Roger would then pick up 27of stretch on the 4.5casing and back the pipe off. The pipe had unscrewed at 550. Roger then screwed back on and tried again. The 4.5casing backed off this time at 950. Roger then went in and screwed 950 of good pipe back on and pulled string weight. Then roger went in with 3.5swab tools with out swab cups and got stuck at 950. Then pulled the cable into. They lost a some 2.375tubing it may have unscrewed. He will attempt to get on the 2.375tubing and pull all out.
1445445406 2015-10-21 Production Wells No Violations

Service Rig has been removed from well site. Rig has been stripped down because there are tools left on site. The 8.625casing has been left open to the atmosphere. There is no control at the well at all. There are bales and elevators to the rig left next to wellbore. There is a 2flow line open that goes from well to the tank site. There are rods, 2tubing and 4.5casing lying at the well site. There is a basket of safety equipment lying at the site. There are small hand tools lying out on a wire rope spool. The pumping unit has been slid back. There is a pipe trailer setting at the lease road. The tank site has not changed yet. There was a small gas compressor removed from site.

1461081876 2015-12-15 Production Wells No Violations

--10:00am 2hrs. 46 degrees and cloudy and light rain.

1461236995 2016-04-20 Production Wells No Violations

-

1475232879 2016-09-01 Production Wells No Violations The purpose of the inspection is a follow-up to Chiefs Order 2016--210 barrel steel tank and 1-50 barrel steel tank. There is a horizontal separator that is not functional and all valves are shut in. The vegetation is very heavy around all the equipment at tank site. There are pictures on file.
1552646525 2016-04-04 Administrative Inspection No Violations I called Guy French back and he wants to know when Barr will plug the well. I stated that it is Attorneys hands now. He wants the Fishing equipment moved from the site or placed next to the casing and tubing pile.
1896613083 2015-05-04 Production Wells No Violations The rig is over the well. There is a 5 gallon bucket over the 8.625 casing. There is heavy wall pipe with sections of 4.5casing and pieces of cable that have been fished out of the well laying on the ground. There is 2.375 tubing, 4.5casing and rods stacked out on racks. There were pictures taken on day of inspection.
1952316010 2006-12-07 Production Wells No Violations Producing
2142065518 2013-04-04 Administrative Inspection No Violations I called Bob Barr and Left a phone message. Need to get something done with well. Iam going to submit to Enforcement action request. Big Sky has failed to comply on all issues.
321451627 2016-6-7 0:00:0 PW No Violations 3.00
754908296 2014-6-26 0:00: AM No Violations
869082305 2015-7-22 0:00: PW No Violations
943958070 2004-7-14 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1112879032 US-OH-102836 2005-04-07 Failure to properly bury pipeline
1112879032 US-OH-102837 2005-04-07 Well operation causing pollution and contamination
1112879032 US-OH-102838 2005-04-07 Failure to legibly identify well
1112879032 US-OH-102839 2005-04-07 No SPCC dike/or failure to keep dike free of water or oil
1289349813 US-OH-108166 2012-07-14 Nonproduction; well shall be plugged or placed in temporary inactive status
1289349813 US-OH-108167 2012-07-14 Statement of annual production not filed

For data sources see[9]

References