X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-119-27849

Well Details

Well ID: 34-119-27849
Loading map...
Country: United States
State: Ohio
County: Muskingum
Municipality: Licking Township
Operator Name: KING PETROLEUM 2
Well Pad ID:
Farm/Lease Name: KING-CASEY
License Status: Final Restoration
License Date: 2012-07-24
Spud Date: 1994-02-15
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1994-02-26
Well Total Depth: 5560.00 ft
Configuration: Vertical
Latitude: 40.090000
Longitude: -82.130000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1994-02-02 Issued Date 2/2/94 Expired Date 2/2/95 Acres 0040000 Tool Type RTAF Proposed Formation TRENTON/TPLU Proposed Depth 05560 Proposed Drill Depth 05560
Original Spud 1994-02-19 IP. NAT. 1.5MMCFG & S/OIL
Completed 1994-02-26 IP. NAT. 1.5MMCFG & S/OIL
Reached Total Depth 1994-02-26 IP. NAT. 1.5MMCFG & S/OIL
CO 1994-03-22 28 CGAS EXPLORATION,INC GeoDate 2/2/94
Completion Report Received 1994-04-22 IP. NAT. 1.5MMCFG & S/OIL
CO 1994-04-25 1493 KING PETROLEUM GeoDate 2/2/94
APP 2012-04-09 Proposed Formations:TRENTON THRU TREMPEALEAU, Issued Date:4/9/2012, Expired Date:4/9/2014 12:00:00 PM, Drilling unit acres:44, Proposed Well Type:OG, Proposed Well Class:
APP 2012-07-24 Proposed Formations:ROSE RUN, Issued Date:7/24/2012, Expired Date:7/24/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2012-10-12 IP. NAT. 1.5MMCFG & S/OIL
Construction Permit Expires 2014-07-24 IP. NAT. 1.5MMCFG & S/OIL
Record Last Modified 2016-08-13 IP. NAT. 1.5MMCFG & S/OIL

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5333 5444 88
5332 5418 0
1997-06-29 5332 5418 0
5333 5444 88
5332 5418 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 2400 Gal 0 TREATED W/2400 GAL 15% FE ACID
0 0 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1995 CGAS EXPLORATION 7196.00 2737.00 365
1996 CGAS EXPLORATION 4671.00 1996.00 365
1997 CGAS EXPLORATION 7506.00 1549.00 365
1998 KING PETROLEUM 2 4735.00 837.00 320
1999 KING PETROLEUM 2 2769.00 587.00 320
2000 KING PETROLEUM 2 316.00 180.00 300
2001 KING PETROLEUM 2 311.00 145.00 208
2002 KING PETROLEUM 2 132.00 0.00 208
2003 KING PETROLEUM 2 272.00 0.00 208
2004 KING PETROLEUM 2 24.00 0.00 104
2005 KING PETROLEUM 2 38.00 97.00 156
2006 KING PETROLEUM 1 0.00 0.00 36
2007 KING PETROLEUM 2 0.00 0.00 52
2008 KING PETROLEUM 2 0.00 0.00 104
2009 KING PETROLEUM 2 0.00 0.00 104
2010 KING PETROLEUM 2 0.00 0.00 104
2011 KING PETROLEUM 2 0.00 0.00 72

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1995 CGAS EXPLORATION Brine 0 365
1996 CGAS EXPLORATION Brine 0 365
1997 CGAS EXPLORATION Brine 0 365
1998 CGAS EXPLORATION Brine 0 365
1999 CGAS EXPLORATION Brine 0 365
2000 CGAS EXPLORATION Brine 0 365
2001 KING PETROLEUM 2 Brine 80 208
2002 KING PETROLEUM 2 Brine 0 208
2003 KING PETROLEUM 2 Brine 80 208
2004 KING PETROLEUM 2 Brine 80 104
2005 KING PETROLEUM 2 Brine 80 156
2006 KING PETROLEUM 1 Brine 0 36
2007 KING PETROLEUM 2 Brine 80 52
2008 KING PETROLEUM 2 Brine 160 104
2009 KING PETROLEUM 2 Brine 160 104
2010 KING PETROLEUM 2 Brine 160 104
2011 KING PETROLEUM 2 Brine 160 72

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1684582801 2012-10-10 0:00 PB No Violations 4.00
-1784768670 2012-10-12 0:00 PB No Violations
-86998140 2012-10-10 0:00 PB No Violations 6.00
0000019084 Preliminary Restoration No Violations PASSED Y WITNESSED 11/18/94 INSPECTOR GERALD YOUNG DATE 11/1819/94 DATA FROM OLD VAX INFO
0086998140 2012-10-10 Plug / Plug Back No Violations Matheny well service ripped 4.5casing at 4353 and pulled up to 3800 due to pulling tight. Formation Cementing set 100 rip plug. Formation set clinton plug at 3321-3129. Chris Grimm witnessed rest of plug job.
0963468757 2016-06-14 Final Restoration No Violations The Final Restoration passed on 6-14-16 by Patrick Shreve. Well was plugged in compliance OAC 1501-9-11. The land was restored back under ORC 1509.072.
1369242556 2013-05-22 Final Restoration No Violations On day of inspection site has not vegetated back yet. I will look at later date.
1522861497 2008-07-21 Production Wells No Violations Producing, no problems noted. Pumping when I was there.
1684582801 2012-10-10 Plug / Plug Back No Violations Matheny well service is running 2.375tubing in to set Bottom plug at 5300-4900. Formation Cementing spotted 30 sack plug. 18.9 barrel was the displacement with brine water.
1784768670 2012-10-12 Plug / Plug Back No Violations On the day of my inspection Matheny Well Svc pulled 4353 of 11.6# 4.5 casing from the well, and Formation Cementing set 6 cement plugs at various intervals from 3880 to surface. See plug report for details.
19084 PL No Violations
963468757 2016-6-14 0:00: FR No Violations 1.00

For data sources see[9]

References