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34-119-28154

Well Details

Well ID: 34-119-28154
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Country: United States
State: Ohio
County: Muskingum
Municipality: Newton Township
Operator Name: BAKERWELL INC
Well Pad ID:
Farm/Lease Name: BURCHFIELD UNIT
License Status: Final Restoration
License Date: 2013-03-12
Spud Date: 1997-12-04
Spud Drilling Contractor: CRYSTAL DEVELOPMENT
Final Drill Date: 1997-12-15
Well Total Depth: 5550.00 ft
Configuration: Directional
Latitude: 39.900000
Longitude: -82.160000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 1997-12-02 254 EDCO DRILLING & PRODUCING Proposed Formation CLINTON thru ROSE RUN Issued Date 12/2/97 Expired Date 12/2/98 6:00:00 AM
Original Spud 1997-12-04 RBDMS Rec
Completed 1997-12-15 RBDMS Rec
Reached Total Depth 1997-12-15 RBDMS Rec
Completion Report Received 1998-03-09 RBDMS Rec
Correction to Well 1998-03-26 CORRECTION IN TARGET FOOTAGE DESCRIPTION. TARGET SHOULD BE 1036'NL & 528'WL OF SEC. 2 (W); X AND Y TARGET COORDINATES CORRECTED TO X=2,095,156 AND Y=694,498; TARGET ELEVATION SHOULD BE 815 AND SOURCE OF LOCATION--AS DRILLED SURVEYOR'S PLAT.
Change of Owner 2007-06-06 Operator changed from 254, EDCO DRILLING & PRODUCING to 432, BAKERWELL INC
APP 2010-07-06 Proposed Formations:ROSE RUN, Issued Date:7/6/2010, Expired Date:7/6/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
APP 2013-03-12 Proposed Formations:ROSE RUN, Issued Date:3/12/2013, Expired Date:3/12/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-04-07 RBDMS Rec
Construction Permit Expires 2015-03-12 RBDMS Rec
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1998 EDCO DRILLING & PRODUCING 69094.00 166.00 365
2000 EDCO DRILLING & PRODUCING 35187.00 212.00 365
2001 EDCO DRILLING & PRODUCING 17413.00 960.00 365
2002 EDCO DRILLING & PRODUCING 584.00 243.00 60
2003 EDCO DRILLING & PRODUCING 49.00 602.00 300
2005 EDCO DRILLING & PRODUCING 0.00 313.00 365
2006 EDCO DRILLING & PRODUCING 0.00 155.00 365
2007 BAKERWELL INC 0.00 0.00 365
2008 BAKERWELL INC 0.00 0.00 365
2009 BAKERWELL INC 0.00 67.00 365
2010 BAKERWELL INC 0.00 32.00 365
2011 BAKERWELL INC 0.00 25.00 365
2012 BAKERWELL INC 0.00 0.00 366
2013 BAKERWELL INC 0.00 0.00 365
2014 BAKERWELL INC 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1998 EDCO DRILLING & PRODUCING Brine 0 365
2000 EDCO DRILLING & PRODUCING Brine 110 365
2001 EDCO DRILLING & PRODUCING Brine 70 365
2002 EDCO DRILLING & PRODUCING Brine 210 60
2003 EDCO DRILLING & PRODUCING Brine 300 300
2005 EDCO DRILLING & PRODUCING Brine 0 365
2006 EDCO DRILLING & PRODUCING Brine 0 365
2007 BAKERWELL INC Brine 0 365
2008 BAKERWELL INC Brine 0 365
2009 BAKERWELL INC Brine 675 365
2010 BAKERWELL INC Brine 370 365
2011 BAKERWELL INC Brine 0 365
2012 BAKERWELL INC Brine 0 366
2013 BAKERWELL INC Brine 0 365
2014 BAKERWELL INC Brine 45 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1489090163 2014-4-4 0:00:0 PB No Violations 5.00
-318137109 2014-8-13 0:00: FR No Violations 0.50
0318137109 2014-08-13 Final Restoration No Violations Final Restoration passed on 8-13-14 by Patrick Shreve.
1396529921 2014-04-02 Plug / Plug Back No Violations Baker well shot pipe off at 4370 with Appalachain wirline. The joints are 44 long. They are dragging and the rig is pulling 80,000lbs. The pipe weighs 15.5lb/ft so the string weight would be 67,735lbs. Hooked Formation to string and pumped on casing. There was 800 psi on fluid pressure. They pulled 6 joints after getting pipe moving. From 4106-3906 set a Trenton plug. Pulled up to the Clinton plug and shut down. No circulation at this point.
1396623836 2014-04-03 Plug / Plug Back No Violations Bakerwell pulled 5.5casing up to 3468 to set Clinton plug. The plug was at 3468-3257. The cement plug was set with class A cement and 2% CaCl with Cotton seed hulls. There was no circulation. The decision was made to pull all casing and run tubing after tagging cement top.
1396762631 2014-04-01 Plug / Plug Back No Violations Setting Bottom plug on well. Bakerwell is running 2.375upset 8 round tubing. Formation is going to pump the cement plug at 5474. There is 100 of 4.875open hole and 5.5casing is at 5336. Formation pumped 60 sacks of regular class A cement. Plug was set at 5474-5074. There was good circulation.
1396888533 2014-04-07 Plug / Plug Back No Violations The 2.375upset tubing was ran to depth of 2466. The Big Lime was set from 2466-2266. The bottom of the Surface was set at 1114-914 with 52 sacks ran of 2% gelled cement. Then tubing was pulled up to 350 where the plug was set at fluid level. From 350-150 set plug and ran 50 sacks of class A cement @ 2% gelled cement. The rig was instructed to pull all tubing out and then a bridge plug was set at 250. Then set top plug of 96 sacks of regular class A cement. Well did not drop back.
1399229674 2014-04-08 Plug / Plug Back No Violations Well was plugged and stopped in to check and see if cement dropped back. The plug was at top.
1489090163 2014-04-04 Plug / Plug Back No Violations Baker well was running tools in to tag cement plug. Set down was at 2970. The plug could have had cave in on top of plug. Rig was running 2.375tubing at 2466 for the lime plug.
iDIAN00101 1999-05-03 Preliminary Restoration No Violations
iDIAN001014 1999-5-3 0:00:0 PL No Violations

For data sources see[8]

References