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Well ID: 34-119-28610 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Madison Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: CONSOLIDATION COAL CO | |
License Status: Final Restoration | |
License Date: 2013-02-27 | |
Spud Date: 2007-04-23 | |
Spud Drilling Contractor: G & H DRLG | |
Final Drill Date: 2007-05-02 | |
Well Total Depth: 6112.00 ft | |
Configuration: Vertical | |
Latitude: 40.110000 | |
Longitude: -81.950000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-02-16 | Proposed Formations:CLINTON, BLACK RIVER, KNOX, Issued Date:2/16/2007, Expired Date:2/16/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2007-05-02 | |
Reached Total Depth | 2007-05-02 | |
Completion Report Received | 2008-01-02 | |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-02-27 | Proposed Formations:ROSE RUN, Issued Date:2/27/2013, Expired Date:2/27/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-02-28 | |
Construction Permit Expires | 2015-02-27 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2008-01-18 | 5962 | 5991 | 30 |
5962 | 5991 | 30 | |
5962 | 5991 | 30 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 2940 Gal | 0 | ALSO USED 28% ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | EXCO - NORTH COAST ENERGY INC | 6592.00 | 295.00 | 208 |
2008 | EXCO - NORTH COAST ENERGY INC | 976.00 | 314.00 | 366 |
2009 | ENERVEST OPERATING LLC | 906.00 | 0.00 | 92 |
2010 | ENERVEST OPERATING LLC | 664.00 | 334.00 | 365 |
2011 | ENERVEST OPERATING LLC | 258.00 | 91.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 294 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | EXCO - NORTH COAST ENERGY INC | Brine | 949 | 208 |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 1020 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 1221 | 365 |
2010 | ENERVEST OPERATING LLC | Brine | 663 | 365 |
2011 | ENERVEST OPERATING LLC | Brine | 741 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 294 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-412085943 | 2013-4-10 0:00: | AM | No Violations | |
-830125891 | 2018-3-26 0:00: | PB | No Violations | 1.00 |
-865579516 | 2018-2-21 0:00: | FR | No Violations | 1.00 |
0074215975 | 2008-11-13 | Production Wells | No Violations | there is now a pump jack on this well. Pumping. No problems noted. |
0119739994 | 2011-01-14 | Production Wells | No Violations | The well is not producing. Last years production shows that the well made a lot of brine some oil and not much gas. Produce or plug |
0407919772 | 2011-04-18 | Production Wells | No Violations | Moving big rig off and smaller rig on to swab. Big water from Black River. |
0412085943 | 2013-04-10 | Administrative Inspection | No Violations | Per Request on the status of the well. Well is not in compliance with 1509. Waiting on Enervest to Plug well. Plug Permit in hand. |
0830125891 | 2018-03-26 | Plug / Plug Back | No Violations | Accompanied Muskingum County Inspector Pat Shreve, Reference his Report for further details |
0865579516 | 2018-02-21 | Final Restoration | No Violations | On the day of my inspection I had Mike Zalenski of Ohio Department of Natural Resources Division of Wildlife. The well was plugged and some pipe was found and I called Enervest and Chipco will remove the pipe lying on the ground. The old tank site had an existing riser pipe that will need cut out and removed. |
0954656162 | 2007-06-27 | Preliminary Restoration | No Violations | Final grade, seeded and mulching in progress. Looks good. |
119739994 | 2011-1-14 0:00: | PW | No Violations | |
1214409849 | 2018-04-02 | Final Restoration | No Violations | The inspection revealed that Chipco was on site removing some material to complete the Final Restoration. The material removed was 2 risers, 1 - 4-inch x 4-foot bumper pipe and 32 feet of 2-inch flowline. The Final Restoration passed on this date. |
1366823323 | 2013-04-24 | Production Wells | No Violations | This is a follow up to NOV # 119739994. Well is on plugging list and I have permit in hand. Tanks and pumping unit have been removed. |
1393434470 | 2014-02-26 | Plug / Plug Back | No Violations | Chipco is setting Bottom plug thru 1.5tubing. They ran in to depth of 5949. They will set plug from 5949-5549. Set a 30 sack plug with Class A cement. The well circulated. |
1393564448 | 2014-02-27 | Plug / Plug Back | No Violations | Chipco is setting a rip/Clinton plug. They ripped at 4470. Chipco pumped an 80 barrel load of 10lb per gallon brine down. The well did not circulate but it was blowing on backside. After the pump shut down well went on vacume. The truck went to get 2nd load of brine water. The decision was made to pull up to the bottom of the clinton and set the clinton and rip plug together. Rig pulled casing to 3878 and then Chipco set a 400cement plug. The plug was set from 3878-3478. After the displacing down the rig could not pull the pipe. The rig shut down and will tag in morning. |
1393600894 | 2014-02-28 | Plug / Plug Back | No Violations | Chipco ran tools in hole and tagged cement at 3200. They then ripped pipe at 3100. They pulled 8 joints at 42per joint. The Big Lime plug will be set at 2750-2450. Ran 86 sacks at the Lime. Bottom of 8.625plug is at 1250-1050 with 60 sacks of class A ran. 200-0 there were 60 sacks of class A cement ran. |
1393958706 | 2014-02-28 | Plug / Plug Back | No Violations | Well was plugged by Chipco for Enervest resolving the Compliance Notice on 2-28-14 by Patrick Shreve. |
1394025722 | 2014-02-24 | Plug / Plug Back | No Violations | Chipco is running in 2.375upset tubing with tools and they can not get past 2000. They decided to pull tubing and run in with 1.5 tubing and spot bottom plug tomarrow. |
1399912941 | 2014-05-12 | Final Restoration | No Violations | Final Restoration passed on 5-12-14 by Patrick Shreve. |
1431818926 | 2018-03-26 | Final Restoration | No Violations | |
1700450860 | 2011-01-14 | Production Wells | No Violations | FOLLOW UP TO NOV # 119739994 The well is not producing. Last years production shows that the well made a lot of brine some oil and not much gas. Produce or plug |
1903438060 | 2007-06-12 | Preliminary Restoration | No Violations | Reclamation in progress. Tanks set and well in producing |
407919772 | 2011-4-18 0:00: | PW | No Violations | |
74215975 | 2008-11-13 0:00 | PW | No Violations | |
954656162 | 2007-6-27 0:00: | PL | No Violations |
For data sources see[9]