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Well ID: 34-121-23268 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Jackson Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: JENKINS JOHN B | |
License Status: Final Restoration | |
License Date: 2011-03-11 | |
Spud Date: 1984-10-17 | |
Spud Drilling Contractor: J & B DRILLING | |
Final Drill Date: 1984-10-25 | |
Well Total Depth: 6091.00 ft | |
Configuration: Vertical | |
Latitude: 39.600000 | |
Longitude: -81.550000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-08-17 | 6 BENATTY CORP GeoDate 8/17/84 |
Oil and Gas | 1984-08-17 | Issued Date 8/17/84 Expired Date 2/13/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06091 Proposed Drill Depth 06091 |
Original Spud | 1984-10-17 | |
Completed | 1984-10-25 | |
Reached Total Depth | 1984-10-25 | |
Completion Report Received | 1984-11-14 | |
CO | 1995-01-20 | 182 BELDEN & BLAKE CO GeoDate 8/17/84 |
Change of Owner | 2007-04-27 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC |
APP | 2011-03-11 | Proposed Formations:CLINTON-MEDINA, Issued Date:3/11/2011, Expired Date:3/10/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2011-05-13 | |
Construction Permit Expires | 2013-03-10 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5768 | 5852 | 0 |
5768 | 5852 | 0 | |
2006-09-11 | 5769 | 5810 | 18 |
5769 | 5810 | 18 | |
5768 | 5852 | 0 | |
2006-09-11 | 5906 | 5916 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 148 Mscf | 0 | CLINTON | ||
N2 | 0 | 92 Mscf | 0 | MEDINA | ||
H2O | 0 | 48000 Gal | 40000 | CLINTON | ||
H2O | 0 | 38000 Gal | 40000 | FRAC: H2O,SAND,N2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | BENATTY CORP | 27862.00 | 0.00 | 0 |
1986 | BENATTY CORP | 11995.00 | 0.00 | 365 |
1987 | BENATTY CORP | 8969.00 | 0.00 | 365 |
1988 | BENATTY CORP | 6100.00 | 0.00 | 365 |
1989 | BENATTY CORP | 7103.00 | 0.00 | 365 |
1990 | BENATTY CORP | 4709.00 | 0.00 | 365 |
1991 | BENATTY CORP | 3976.00 | 71.00 | 365 |
1992 | BENATTY CORP | 3924.00 | 0.00 | 365 |
1993 | BENATTY CORP | 3809.00 | 0.00 | 365 |
1994 | BELDEN & BLAKE CORPORATION | 2762.00 | 0.00 | 31 |
1995 | BELDEN & BLAKE CORPORATION | 3433.00 | 0.00 | 344 |
1996 | BELDEN & BLAKE CORPORATION | 2892.00 | 0.00 | 340 |
1997 | BELDEN & BLAKE CORPORATION | 2520.00 | 0.00 | 325 |
1998 | BELDEN & BLAKE CORPORATION | 2305.00 | 36.00 | 359 |
1999 | BELDEN & BLAKE CORPORATION | 1080.00 | 0.00 | 293 |
2000 | BELDEN & BLAKE CORPORATION | 1358.00 | 0.00 | 324 |
2001 | BELDEN & BLAKE CORPORATION | 454.00 | 0.00 | 209 |
2002 | BELDEN & BLAKE CORPORATION | 1290.00 | 0.00 | 259 |
2003 | BELDEN & BLAKE CORPORATION | 912.00 | 0.00 | 329 |
2004 | BELDEN & BLAKE CORPORATION | 814.00 | 0.00 | 361 |
2005 | BELDEN & BLAKE CORPORATION | 223.00 | 0.00 | 0 |
2006 | BELDEN & BLAKE CORPORATION | 0.00 | 0.00 | 0 |
2007 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2008 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2009 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL7518 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0132136376 | 2011-05-11 | Plug / Plug Back | No Violations | On site to witness rig operator run bare tools in well to confirm total depth and then perforate casing in lime and start tubing in ole to set bottom hole and lime plug tomorrow. |
0136082493 | 2010-10-22 | Production Wells | No Violations | FOLLOW UP TO NOV # 1287833655 Upon receiving anonymous complaint of stinking gas well, inspected site and found well area with slight sulfur odor present and researched records and determined owner has not produced well since 2005 suspect hole in casing.
Plug or Produce well or file for temporary abandonment status. Failure to comply may result in bond forfiture. |
0308400187 | 2004-05-13 | Production Wells | No Violations | Open flow gas well slight H2Sodor present at wellhead will call local pumper to advise of potential problem at wellsite. |
0847275448 | 2012-02-06 | Final Restoration | No Violations | Well site meets 1509.72. |
0912690618 | 2013-04-11 | Administrative Inspection | No Violations | Follow up to Compliance Notice #1287833655 and #1292450697. Inspector William Stolarik passed final restoration on 2/6/2012. |
1287833655 | 2010-10-22 | Production Wells | Violations Noted | Upon receiving anonymous complaint of stinking gas well, inspected site and found well area with slight sulfur odor present and researched records and determined owner has not produced well since 2005 suspect hole in casing.
Plug or Produce well or file for temporary abandonment status. Failure to comply may result in bond forfiture. |
1292450697 | 2010-12-15 | Production Wells | No Violations | Inspection revealed that there has been no change in status of well it is still venting sulfur odor gas from well. |
1305453061 | 2011-05-13 | Production Wells | No Violations | Well has been plugged resolving previous Notice of Violation. |
132136376 | 2011-5-11 0:00: | PB | No Violations | |
1328542545 | 2012-02-06 | Final Restoration | No Violations | Well site meets 1509.072 ORC. |
136082493 | 2010-10-22 0:00 | PW | No Violations | |
308400187 | 2004-5-13 0:00: | PW | No Violations | |
847275448 | 2012-2-6 0:00:0 | FR | No Violations | |
912690618 | 2013-4-11 0:00: | AM | No Violations | 1.00 |
PL7518 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1287833655 | US-OH-107966 | 2010-10-23 | Well shall be plugged | |
1287833655 | US-OH-107967 | 2010-10-23 | Temporary inactive; failure to properly shut-in or maintain the well or associated equipment | |
1287833655 | US-OH-107968 | 2010-10-23 | Defective casing, leaking well |
For data sources see[9]