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| Well ID: 34-127-20894 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Perry | |
| Municipality: Bearfield Township | |
| Operator Name: M & R INVESTMENTS OHIO LLC | |
| Well Pad ID: | |
| Farm/Lease Name: ALFMAN ALFRED F | |
| License Status: Final Restoration | |
| License Date: 2015-02-02 | |
| Spud Date: 1947-04-28 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1947-07-17 | |
| Well Total Depth: 3918.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.670000 | |
| Longitude: -82.080000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1947-04-28 | GL=969.8 |
| Completed | 1947-07-17 | GL=969.8 |
| Reached Total Depth | 1947-07-17 | GL=969.8 |
| CO | 1991-02-22 | 2936 COLUMBIA NATURAL RES INC |
| Change of Owner | 2005-02-16 | Operator changed from 2936, COLUMBIA NATURAL RES INC to 7774, AMERICAN OIL & GAS LLC |
| Change of Owner | 2007-01-25 | Operator changed from 7774, AMERICAN OIL & GAS LLC to 8154, AB RESOURCES OH LLC |
| Change of Owner | 2010-09-21 | Operator changed from 8154, AB RESOURCES OH LLC to 8685, M & R INVESTMENTS OHIO LLC |
| APP | 2015-02-02 | Proposed Formations:CLINTON, Issued Date:2/2/2015, Expired Date:2/1/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2015-05-07 | GL=969.8 |
| Construction Permit Expires | 2017-02-01 | GL=969.8 |
| Record Last Modified | 2017-02-10 | GL=969.8 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 0 | 0 | 0 |
For data sources see[3]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1058555202 | 2014-4-14 0:00: | PW | No Violations | 1.00 |
| -1077614916 | 2014-4-28 0:00: | PB | No Violations | 3.00 |
| -142490080 | 2014-2-20 0:00: | PW | No Violations | 1.00 |
| -2105795378 | 2013-3-18 0:00: | PW | No Violations | 1.00 |
| -306125067 | 2013-9-10 0:00: | PW | No Violations | 1.00 |
| -546218177 | 2014-6-16 0:00: | PW | No Violations | 1.00 |
| -677045152 | 2013-8-20 0:00: | PW | No Violations | 1.00 |
| -893187554 | 2015-4-24 0:00: | PB | No Violations | 2.50 |
| 0142490080 | 2014-02-20 | Production Wells | No Violations | I inspected this well and it is still shut in. I tried to contact Jody Jasper to see what is going on with the well. I have still not heard back from him. I will try to contact him again by the beginning of next week. |
| 0241162888 | 2015-04-30 | Plug / Plug Back | No Violations | The rig crew was not on location today when I stopped at the well. I contacted Doug Watt the rig operator and he said they would not be out today. |
| 0306125067 | 2013-09-10 | Production Wells | No Violations | During my inspection I found nothing has been done with the well. I contacted M&R Investments to get Jody Jaspers phone number. He is on vacation right now and wont be back until Monday. I will contact him then. |
| 0312225328 | 2014-04-02 | Production Wells | No Violations | I contacted Jody Jasper about this well to let him know that the well is still not in production. I explained to him that this well needs to be plugged or legal actions may be taken. He is having a meeting with his boss tomorrow and will talk to him about the well and what I told him. |
| 0546218177 | 2014-06-16 | Production Wells | No Violations | I returned to this well today to do a follow-up inspection on the Chiefs order that was issued to the company on this well. The valves at the well are still shut in making the well incapable of production. It does not look like the company has made any attempt to put the well back into production. |
| 0677045152 | 2013-08-20 | Production Wells | No Violations | I did a follow up inspection on this well to see if it was in-compliance. The valves are still shut in on this well. Non-compliance on putting this well back in production. I will try to contact company. |
| 0893187554 | 2015-04-24 | Plug / Plug Back | No Violations | I returned to this well today to see how everything was going. The rig crew is still working on getting the 3 free at this time. They will contact me if they get it moving. |
| 1058555202 | 2014-04-14 | Production Wells | No Violations | I have called Jody Jasper to see what the company is going to do with this well. He has not returned my phone call yet. I will call him again tomorrow and try to contact the company. |
| 1077614916 | 2014-04-28 | Plug / Plug Back | No Violations | I was at this well to witness the plugging of it. The rig crew was onsite and trying to rip the 5.5 while I was there. They were able to get telegraph at 2900ft. They were able to rip the pipe but when they were working the pipe free it parted about 10ft down. They will be bringing in a fishing tool to recover the pipe and continue plugging the well. |
| 1288277292 | 2015-05-07 | Plug / Plug Back | No Violations | I was onsite today to finish plugging this well. Barry brought in tubing today to set the surface plug. The day before they were able to rip the 7 at 380ft and retrieve it. We set a 200ft surface cement plug. The well is now plugged. I gave Barry the okay to start reclaiming this location. |
| 1398354687 | 2014-04-24 | Production Wells | No Violations | This is a follow-up inspection for this well being idle and not in production. The compliance notice for this well was sent on 03/18/2013 and the compliance date for this violation to be resolved was 07/18/2013. The well is still not in production and is in violation. The company has not tried to put the well back into production and the well will need to be plugged. I have talked to Jody Jasper about the situation of this well on several occasions. This violation needs to be addressed immediately, legal actions may be taken. |
| 1398940449 | 2014-04-30 | Production Wells | No Violations | I returned to this well to do a follow-up inspection on the well and take some pictures of it. The valves are still shut in at the well. The well is incapable of production. The well is still in violation. |
| 1431090506 | 2015-06-22 | Final Restoration | No Violations | Final restoration meets 1509.072B. |
| 1568643505 | 2015-04-23 | Plug / Plug Back | No Violations | Barry Bowers has moved his rig in on this well to plug it. They have gotten rigged up and are now trying to get the 3 freed up. It was ran in on a packer. |
| 1617841443 | 2014-10-24 | Production Wells | No Violations | I returned to this well to do a follow-up inspection on it. During the inspection of the well I found the well still is not capable of production. All of the valves on the well are shut in. There is no gas chart on the meter to record any gas being sold. I took pictures of my findings during my inspection. |
| 2105795378 | 2013-03-18 | Production Wells | No Violations | The valves are shut in on this well. There has been no production reported since 2001. Make well capable of commercial production within 60 days; or plugging is required within 120 days. Failure to comply may result in Forfeiture of Bond. |
| 241162888 | 2015-4-30 0:00: | PB | No Violations | 1.00 |
| 312225328 | 2014-4-2 0:00:0 | PW | No Violations | 1.00 |
For data sources see[8]