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34-127-23005

Well Details

Well ID: 34-127-23005
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Country: United States
State: Ohio
County: Perry
Municipality: Reading Township
Operator Name: HUFFMAN-BOWERS INC
Well Pad ID:
Farm/Lease Name: HARLAN JOEL
License Status: Final Restoration
License Date: 2014-05-30
Spud Date: 1970-12-11
Spud Drilling Contractor:
Final Drill Date: 1975-01-15
Well Total Depth: 2907.00 ft
Configuration: Vertical
Latitude: 39.780000
Longitude: -82.340000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1970-12-11 1804 EMMERT LEO R GeoDate 12/11/70
Original Spud 1970-12-11
Completed 1975-01-15
Reached Total Depth 1975-01-15
CO 1989-12-04 1804 EMMERT LEO R GeoDate 12/4/89
Unknown 1989-12-04 Issued Date 12/4/89 Expired Date 12/4/90 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 2006-02-28 Operator changed from 1804, EMMERT LEO R to 5155, HUFFMAN-BOWERS INC
APP 2010-07-13 Proposed Formations:, Issued Date:7/13/2010, Expired Date:7/13/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2014-05-30 Proposed Formations:CLINTON, Issued Date:5/30/2014, Expired Date:5/29/2016 12:00:00 PM, Drilling unit acres:92, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-08-01
Construction Permit Expires 2016-05-29
Record Last Modified 2017-02-10

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2000 Bbl 20000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 RELIANCE ENERGY INC 0.00 161.00 0
1986 RELIANCE ENERGY INC 0.00 379.00 365
1987 RELIANCE ENERGY INC 0.00 228.00 365
1988 RELIANCE ENERGY INC 0.00 224.00 365
1989 RELIANCE ENERGY INC 0.00 151.00 273
1993 EMMERT LEO R 0.00 290.00 365
1995 EMMERT LEO R 0.00 228.00 365
1996 EMMERT LEO R 0.00 193.00 365
1997 EMMERT LEO R 0.00 295.00 365
1998 EMMERT LEO R 0.00 231.00 365
1999 EMMERT LEO R 0.00 214.00 365
2000 EMMERT LEO R 0.00 153.00 365
2001 EMMERT LEO R 0.00 110.00 300
2002 EMMERT LEO R 0.00 62.00 211
2003 EMMERT LEO R 0.00 2.00 21
2004 EMMERT LEO R 0.00 3.00 24
2006 HUFFMAN-BOWERS INC 0.00 0.00 365
2007 HUFFMAN-BOWERS INC 0.00 0.00 365
2008 HUFFMAN-BOWERS INC 0.00 0.00 365
2009 HUFFMAN-BOWERS INC 0.00 0.00 365
2010 HUFFMAN-BOWERS INC 0.00 0.00 365
2011 HUFFMAN-BOWERS INC 0.00 0.00 365
2012 HUFFMAN-BOWERS INC 0.00 0.00 366
2013 HUFFMAN-BOWERS INC 0.00 0.00 365
2014 HUFFMAN-BOWERS INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 RELIANCE ENERGY INC Brine 0 0
1986 RELIANCE ENERGY INC Brine 0 365
1987 RELIANCE ENERGY INC Brine 0 365
1988 RELIANCE ENERGY INC Brine 0 365
1989 RELIANCE ENERGY INC Brine 0 273
1993 EMMERT LEO R Brine 20 365
1995 EMMERT LEO R Brine 0 365
1996 EMMERT LEO R Brine 0 365
1997 EMMERT LEO R Brine 0 365
1998 EMMERT LEO R Brine 0 365
1999 EMMERT LEO R Brine 0 365
2000 EMMERT LEO R Brine 0 365
2001 EMMERT LEO R Brine 1210 300
2002 EMMERT LEO R Brine 1210 211
2003 EMMERT LEO R Brine 0 21
2004 EMMERT LEO R Brine 0 24
2006 HUFFMAN-BOWERS INC Brine 0 365
2007 HUFFMAN-BOWERS INC Brine 0 365
2008 HUFFMAN-BOWERS INC Brine 0 365
2009 HUFFMAN-BOWERS INC Brine 0 365
2010 HUFFMAN-BOWERS INC Brine 0 365
2011 HUFFMAN-BOWERS INC Brine 0 365
2012 HUFFMAN-BOWERS INC Brine 0 366
2013 HUFFMAN-BOWERS INC Brine 0 365
2014 HUFFMAN-BOWERS INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1426211526 2014-7-21 0:00: PW No Violations 2.00
-1758017315 2014-6-2 0:00:0 PW No Violations 1.00
-1848872293 2014-7-29 0:00: PB No Violations 9.00
-2081762447 2014-7-30 0:00: PB No Violations 0.50
-301411290 2015-6-25 0:00: FR No Violations 1.00
-747563117 2013-12-16 0:00 PW No Violations 1.00
0017581166 2014-04-23 Production Wells No Violations I did a follow-up inspection on this well to check the status of it. The well is not capable of production. I contacted Barry Bowers and he informed me he would be applying for a plug permit for this well. The compliance date to have this well plugged is 6/24/14.
0121933304 2014-07-23 Plug / Plug Back No Violations The rig crew was able to get the tubing out of the well today. After they pulled the tubing out of the well they washed in the bottom plug with clay.
0301411290 2015-06-25 Final Restoration No Violations The final restoration meets 1509.072B.
0394504009 2014-07-24 Plug / Plug Back No Violations I stopped by the rig to check on there status and no one was there. I contacted Doug the rig operator and he told me that the clay was bridged off at 100ft so they will have to drill it out. They will contact me when they get set up.
0523996085 2006-10-25 Production Wells No Violations No violations.
0747563117 2013-12-16 Production Wells Violations Noted The pumping unit has been removed from this well. The flow lines are still at the well. The well appears not to be in production. This well has had no production reported since 2004. The plugging permit for this well has expired. This well will need put back in production within 90days or plugging is required within 180days.
0970139109 2014-07-28 Plug / Plug Back No Violations I was onsite to witness the plugging of this well. The clay was bridges so Barry used his pump truck to push the clay down. We got to bottom them worked on ripping the 4. After we found telegraph we washed in more clay before we ripped. Then we ripped the 4 and pilled out 90ft then washed in more plugging clay for the lime plug.
121933304 2014-7-23 0:00: PB No Violations 6.00
1426211526 2014-07-21 Production Wells No Violations Barry Bowers has moved his service rig in on this well to plug it. The rig crew is working on getting the rods and tubing out of the well today. The tubing is stuck down hole. They will rig up the weight indicator tomorrow.
1566202742 2014-08-04 Plug / Plug Back No Violations The service rig has been moved off of location. The fluid is down 15-20ft in the well. There is still clay on location. The rig crew has been topping the well off and letting it settle. Once the clay stays at the surface I will let them know they can cover the well and reclaim the location.
1758017315 2014-06-02 Production Wells No Violations I met with Barry Bowers to discuss the status of this well. Barry has applied for a plugging permit to plug the well. He said he would be plugging the well this summer.
17581166 2014-4-23 0:00: PW No Violations 1.00
1848872293 2014-07-29 Plug / Plug Back No Violations The rig crew was on location today to work on plugging the well. They were able to get ripped at 800ft. That is where they found free pipe. Once they pulled out the 4 I had them run tubing back in the well to set a 200ft cement plug. They set the plug then pulled the tubing back out of the well. The rest of the hole will be filled with plugging clay to the surface. The rig worked on getting the 8 free.
2081762447 2014-07-30 Plug / Plug Back No Violations I talked with Barry Bowers to see how the plug job was going. He said they tagged the cement plug at 700ft. They were able to recover all of the 8 and are washing in plugging clay at this time.
394504009 2014-7-24 0:00: PB No Violations 1.00
523996085 2006-10-25 0:00 PW No Violations
970139109 2014-7-28 0:00: PB No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0747563117 US-OH-128497 2014-07-24 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[8]

References