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34-129-20260

Well Details

Well ID: 34-129-20260
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Country: United States
State: Ohio
County: Pickaway
Municipality: Wayne Township
Operator Name: HOCKING HILLS ENERGY AND WELL
Well Pad ID:
Farm/Lease Name: DELONG
License Status: Final Restoration
License Date: 2016-11-29
Spud Date: 2015-08-01
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2016-01-11
Well Total Depth: 2591.00 ft
Configuration: Vertical
Latitude: 39.600000
Longitude: -83.050000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2015-07-20 Proposed Formations:KNOX, Issued Date:7/20/2015, Expired Date:7/19/2017 12:00:00 PM, Drilling unit acres:58.429, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2016-01-11
Completion Report Received 2016-11-25
APP 2016-11-29 Proposed Formations:KNOX, Issued Date:11/29/2016, Expired Date:11/29/2018 12:00:00 PM, Drilling unit acres:58.429, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-03-06
Record Last Modified 2017-10-23
Construction Permit Expires 2018-11-29

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2016-01-28 ACID 15 1500 Gal 0 Producers Service Corporation

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2015 HOCKING HILLS ENERGY AND WELL 0.00 0.00 30
2016 HOCKING HILLS ENERGY AND WELL 0.00 0.00 120
2017 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2015 HOCKING HILLS ENERGY AND WELL Brine 220 30
2016 HOCKING HILLS ENERGY AND WELL Brine 70 120
2017 HOCKING HILLS ENERGY AND WELL Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1010953906 2015-12-11 0:00 PB No Violations 2.00
-1476951622 2017-4-28 0:00: FR No Violations 2.00
-643254434 2015-11-11 0:00 DD No Violations 6.00
-759704396 2015-11-17 0:00 DD No Violations 3.00
0249371270 2015-07-30 Drill / Deepen / Reopen No Violations Kilbarger rig number 1 has reached 664. They ran 660 of 7 surface casing with good cement returns The casing test was performed at 800 PSI for 15 minutes with no loss in pressure.
0395822867 2015-08-31 Production Wells No Violations Production well inspection. The well is being evaluated for future drilling operations. I was informed by Doug Kitchen with Hocking Hills Energy that a coil tubing unit would be brought in to deepen the well . This work will be done before 12/25/2105.
0643254434 2015-11-11 Drill / Deepen / Reopen No Violations A coil tubing drilling has arrived on site. Hocking Hills Energy has drilled a mouse hole.
0759704396 2015-11-17 Drill / Deepen / Reopen No Violations CJ Coil Tubing has attempted to drill horizontally into the Trenton formation. The cement plug that was set to allow the drilling to proceed horizontally had slid 200 Formation Cementing on site on 11-16-15 to bring the plug back up to 1750. No activity today to allow the plug to reach maximum strength.
1010953906 2015-12-11 Plug / Plug Back No Violations The well has been plugged back to 1750. The well was kicked off and drilled from 1745 to 2445. They hit oil and stopped drilling. Hocking Hills Energy is submitting a revised permit showing the new total depth of the well. I spoke with Doug Kitchen regarding closing the pit. Doug said he would have the pit closed by 12-23-15.
1447424552 2015-11-13 Drill / Deepen / Reopen No Violations CJ Coil tubing on site. They are rigging up to begin drilling with the coil tubing rig.
1476951622 2017-04-28 Final Restoration No Violations Final restoration inspection. The well was cut off 4 feet below grade and a identification plate was placed on the cut off casing. The well is located in a agriculture field. No seed or straw will be used. The well meets final restoration requirements.
1488905437 2017-03-06 Plug / Plug Back No Violations Knox Energy along with Formation Cementing on site at 8:30 AM. 50 Sack plug set on bottom with good circulation. 200 feet of 4.5 inch diameter casing was removed. 120 sack plug was set from 900 feet to surface.
1689432246 2015-11-09 Drill / Deepen / Reopen No Violations Hocking Hills Energy has placed 690 of class A cement as a plug. The plug was set from 1750 to 2440. The well was drilled to a total depth of 2591. Surface casing was ran but no production casing was ran. The well was a dry hole. The decision was made to set a cement plug then ran 4.5 production casing to allow coil tubing to be used to drill horizontally to reach the productive part of the formation.
1864040983 2015-11-23 Drill / Deepen / Reopen No Violations CJ Coil tubing on site. They began the project 11-12-15. Antech is providing the expertise with the drill motor used on the coil tubing. They have encountered may technical problems during their attempt to drill horizontally. The technology used to drill with coil tubing has had many problems.
2016055960 2015-07-29 Drill / Deepen / Reopen No Violations Conductor string cementing. Formation Cementing on site 10:30AM. The ran 110 sacks class A neat cement with good cement returns.
249371270 2015-7-30 0:00: DD No Violations 9.00
395822867 2015-8-31 0:00: PW No Violations 3.00

For data sources see[8]

References