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Well ID: 34-133-21431 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Palmyra Township | |
Operator Name: HUNTER ROBERT J & RITA M | |
Well Pad ID: | |
Farm/Lease Name: KRISCHNER | |
License Status: Domestic Well | |
License Date: 2018-03-07 | |
Spud Date: 1978-06-11 | |
Spud Drilling Contractor: | |
Final Drill Date: 1978-06-19 | |
Well Total Depth: 4733.00 ft | |
Configuration: Vertical | |
Latitude: 41.120000 | |
Longitude: -81.030000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1978-04-28 | 224 ATLAS ENERGY GROUP INC GeoDate 4/28/78 |
Original Spud | 1978-06-11 | LOCATION UPDATED PER SURVEYOR COORIDNATES 06/27/17 ALE. |
Completed | 1978-06-19 | LOCATION UPDATED PER SURVEYOR COORIDNATES 06/27/17 ALE. |
Reached Total Depth | 1978-06-19 | LOCATION UPDATED PER SURVEYOR COORIDNATES 06/27/17 ALE. |
CO | 1985-06-27 | 224 ATLAS ENERGY GROUP INC GeoDate 6/27/85 |
Unknown | 1985-06-27 | Issued Date 6/27/85 Expired Date 6/27/86 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Change of Owner | 2001-12-13 | Operator changed from 224, ATLAS ENERGY GROUP INC to 6805, GAS ACQUISITION COMPANY LTD |
APP | 2002-03-05 | Proposed Formations:CLINTON, Issued Date:3/5/2002, Expired Date:3/5/2003 6:00:00 AM, Drilling unit acres:85.02, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2011-11-22 | Operator changed from 6805, GAS ACQUISITION COMPANY LTD to 8863, STK INVESTMENTS LLC |
APP | 2018-03-07 | Proposed Formations:QUEENSTON/WHITE CLINTON, Issued Date:3/7/2018, Expired Date:3/6/2020 12:00:00 PM, Drilling unit acres:85.02, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2018-03-14 | LOCATION UPDATED PER SURVEYOR COORIDNATES 06/27/17 ALE. |
Construction Permit Expires | 2020-03-06 | LOCATION UPDATED PER SURVEYOR COORIDNATES 06/27/17 ALE. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4530 | 4564 | 30 |
4530 | 4564 | 30 | |
4530 | 4564 | 30 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 82390 Gal | 62000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 0 |
1986 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 0 |
1988 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 0 |
1989 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 0 |
1990 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 365 |
1992 | CARLESS RESOURCES INC | 0.00 | 0.00 | 0 |
1993 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 0 |
1994 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 365 |
1995 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 365 |
2001 | ATLAS ENERGY GROUP INC | 0.00 | 0.00 | 365 |
2009 | GAS ACQUISITION COMPANY LTD | 0.00 | 0.00 | 0 |
2012 | STK INVESTMENTS LLC | 0.00 | 0.00 | 0 |
2014 | STK INVESTMENTS LLC | 0.00 | 0.00 | 0 |
2015 | STK INVESTMENTS LLC | 0.00 | 0.00 | 0 |
2017 | STK INVESTMENTS LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ATLAS ENERGY GROUP INC | Brine | 0 | 0 |
1986 | ATLAS ENERGY GROUP INC | Brine | 0 | 0 |
1988 | ATLAS ENERGY GROUP INC | Brine | 0 | 0 |
1989 | ATLAS ENERGY GROUP INC | Brine | 0 | 0 |
1990 | ATLAS ENERGY GROUP INC | Brine | 0 | 365 |
1992 | CARLESS RESOURCES INC | Brine | 0 | 0 |
1993 | ATLAS ENERGY GROUP INC | Brine | 0 | 0 |
1994 | ATLAS ENERGY GROUP INC | Brine | 0 | 365 |
1995 | ATLAS ENERGY GROUP INC | Brine | 0 | 365 |
2001 | ATLAS ENERGY GROUP INC | Brine | 0 | 365 |
2009 | GAS ACQUISITION COMPANY LTD | Brine | 0 | 0 |
2012 | STK INVESTMENTS LLC | Brine | 0 | 0 |
2014 | STK INVESTMENTS LLC | Brine | 0 | 0 |
2015 | STK INVESTMENTS LLC | Brine | 0 | 0 |
2017 | STK INVESTMENTS LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-742852921 | 2018-6-14 0:00: | PB | No Violations | 2.10 |
0337521109 | 2018-06-12 | Plug / Plug Back | No Violations | Status check inspection of this Clinton Sandstone well that is scheduled to be plugged this week to satisfy Compliance Notice #1489436312. Diamond Energy Services (DES) service rig is currently parked on location. I spoke with Matt Kleese (DES), who is overseeing the plugging operations, and he will be bringing in the rest of the equipment tomorrow. I have requested that the bottom plug be set through tubing due to the fact that the well has not been produced in thirty years. This violation will be resolved after the well is plugged and final restoration is achieved. |
0353360880 | 2018-06-13 | Plug / Plug Back | No Violations | I returned to location to witness plugging operations on this Clinton Sandstone well. This well is being plugged to satisfy Compliance Notice #1489436312. The service rig was spotted and began rigging up. The tubing trailer and pump truck were spotted. The valve at the wellhead was opened and there was minor pressure and natural gas vented from the wellhead. The fluid level was determined to 800 and it was decided not to run the tools to total depth until the circulating tank was spotted and the wellhead plumbed to the tank. The circulating tank will not be delivered until the morning (6/14/18). This Compliance Notice will be satisfied when the well is plugged and Final Restoration is achieved. |
0742852921 | 2018-06-14 | Plug / Plug Back | No Violations | I was on location to witness plugging operations at this Clinton Sandstone well. This well is being plugged under Compliance Notice #1489436312 for non-production. Diamond Energy Services spotted the half-round and bulk truck. They plumbed a flow line from the wellhead to the half round and chained the line to the tank. They rigged up the lubricator and swabbed the top of the fluid at 800 two (2) times. Both times the well unloaded and flowed oil and brine, and was surging natural gas. Matt Kleese decided to get a load of brine to kill the well and it will take several hours to get the truck to location. The Compliance Notice will be satisfied when the well is plugged and abandoned and Final Restoration is achieved. |
1198991427 | 2020-8-20 0:00: | EX | No Violations | 1.00 |
1489436312 | 2017-03-13 | Production Wells | Violations Noted | I conducted a status check inspection of this Clinton Sandstone well. My inspection today found a wellhead consisting of 4.5 production casing packed in an 8.625 Hercules casing head. The annular ports for the 8.625 surface casing were just above grade, one being fitted with a steel plug and the other was plumbed with a valve. There is no gauge on the 4.5 casing and 8.625 casing annulus and I could not determine if the valve on the annular port was open. The 4.5 casing is equipped with a 4.5 flanged ball valve, a 4 x 2 reducer, and a 2 flow tee. The top of the flow tee is fitted with a steel plug and the tee port is plumbed with a 2 x 1 reducer and 1 steel domestic line. The domestic line is equipped with a 1 ball valve, needle gauge, regulator, and vertical drip bottle. The valve is open and a needle gauge on the drip bottle indicates a domestic supply pressure of 4psi. The needle gauge upstream of the regulator is broken and the wellhead pressure is unknown at this time. A search of the surrounding area found no evidence of production equipment (tanks or separator) that would allow this well to be commercially produced and there is no flow line at the wellhead. A review of records on file with the Division of Oil & Gas Resources Management shows that this well was drilled in June of 1978 by Warren Energy, Inc. (aka: Atlas Energy Group, Inc.) and was completed on 10-25-1978. Two (2) plugging permits have been issued for this well under different ownership since the well was completed: #1 was issued to Atlas Energy Group, Inc. on 6/27/1985 and #2 was issued to Gas Acquisition Company, Ltd on 3/5/2002. STK Investments became the owner of the Kirschner #1 well on 11/22/2011. Production records, dating from the reporting year of 1985 through the reporting year of 2015, show that this well has produced 0 Mcf of natural gas, 0 barrels of oil, and 0 barrels of brine over the past 30 years. Based on the information gathered today and evidence on file with th |
1515071327 | 2018-01-04 | Production Wells | No Violations | Follow-up to Compliance Notice #1489436312 issued on 3/15/17 that required the well to be plugged and abandoned within 180 days. My inspection today found that the well has not been plugged and no plugging permit has been issued to plug and abandon this well. The wellhead consists of 4.5 casing equipped with a ball valve, a 4 X 2 reducer and tee, and a 2 X 1 reducer. The 4.5 valve is open and a 1 domestic line is plumbed to the 2 X 1 reducer. The domestic line is equipped with ball valve, regulator, and drip bottle. The 1 valve is open and there are two (2) gauges on the line that indicate a pressure of 0psi on both gauges. This violation continues. |
1565579275 | 2018-06-13 | Plug / Plug Back | No Violations | I was on location and met with Inspector John Fleming. This well is being plugged to satisfy Compliance Notice #1489436312. There is currently no activity or personnel on location. I gave Inspector Fleming my plug outline and we reviewed the plugs. I left location and I will return later to witness operations. This Compliance Notice will be satisfied when the well is plugged and Final Restoration is achieved. |
1945774844 | 2018-06-14 | Plug / Plug Back | No Violations | I was back on location to check on plugging operations. I received a call from Inspector John Fleming this afternoon, that he had been contacted by Matt Kleese (Diamond Energy Services) stating that the property was auctioned off and the new landowner was on location and wants to take ownership of the well for domestic use. There is currently no personnel on location and I met with the new landowner Rob Hunter. He said that he has been in contact with STK Investments and that they are going to file the required paperwork to transfer the well for domestic use. This well was being plugged under Compliance Notice #1489436312 and will be satisfied and closed when the well is transferred to domestic ownership. |
337521109 | 2018-6-12 0:00: | PB | No Violations | 1.50 |
353360880 | 2018-6-13 0:00: | PB | No Violations | 2.40 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1489436312 | US-OH-113883 | 2017-05-26 | Well shall be plugged |
For data sources see[9]