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34-133-21703

Well Details

Well ID: 34-133-21703
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Country: United States
State: Ohio
County: Portage
Municipality: Windham Township
Operator Name: EQUITY OIL & GAS FUNDS INC
Well Pad ID:
Farm/Lease Name: L & P INVESTMENTS
License Status: Producing
License Date: 1978-10-24
Spud Date: 1978-11-26
Spud Drilling Contractor:
Final Drill Date: 1978-12-03
Well Total Depth: 4363.00 ft
Configuration: Vertical
Latitude: 41.260000
Longitude: -81.080000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-10-24 317 INLAND DRILLING CO INC GeoDate 10/24/78
Original Spud 1978-11-26
Completed 1978-12-03
Reached Total Depth 1978-12-03
CO 1992-12-04 1171 EQUITY OIL & GAS FUNDS IN GeoDate 10/24/78
Record Last Modified 2019-06-04

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4238 4265 1
4238 4265 1
4238 4265 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 62000 Gal 55000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 INLAND DRILLING CO INC 670.00 0.00 365
1986 INLAND DRILLING CO INC 280.00 0.00 151
1987 INLAND DRILLING CO INC 0.00 0.00 0
1988 INLAND DRILLING CO INC 0.00 73.00 0
1989 INLAND DRILLING CO INC 0.00 189.00 60
1990 INLAND DRILLING CO INC 0.00 300.00 365
1991 INLAND DRILLING CO INC 0.00 426.00 365
1992 INLAND DRILLING CO INC 0.00 220.00 275
1993 EQUITY OIL & GAS FUNDS INC 440.00 331.00 365
1994 EQUITY OIL & GAS FUNDS INC 476.00 429.00 365
1995 EQUITY OIL & GAS FUNDS INC 641.00 312.00 365
1996 EQUITY OIL & GAS FUNDS INC 599.00 236.00 365
1997 EQUITY OIL & GAS FUNDS INC 569.00 279.00 365
1998 EQUITY OIL & GAS FUNDS INC 309.00 187.00 365
1999 EQUITY OIL & GAS FUNDS INC 417.00 194.00 365
2000 EQUITY OIL & GAS FUNDS INC 321.00 156.00 365
2001 EQUITY OIL & GAS FUNDS INC 2.00 94.00 365
2002 EQUITY OIL & GAS FUNDS INC 0.00 124.00 365
2003 EQUITY OIL & GAS FUNDS INC 0.00 253.00 365
2004 EQUITY OIL & GAS FUNDS INC 0.00 118.00 365
2005 EQUITY OIL & GAS FUNDS INC 0.00 123.00 365
2006 EQUITY OIL & GAS FUNDS INC 0.00 245.00 365
2007 EQUITY OIL & GAS FUNDS INC 0.00 249.00 365
2008 EQUITY OIL & GAS FUNDS INC 0.00 95.00 365
2009 EQUITY OIL & GAS FUNDS INC 0.00 117.00 365
2010 EQUITY OIL & GAS FUNDS INC 0.00 120.00 365
2011 EQUITY OIL & GAS FUNDS INC 0.00 177.00 0
2012 EQUITY OIL & GAS FUNDS INC 0.00 121.00 366
2013 EQUITY OIL & GAS FUNDS INC 0.00 124.00 365
2014 EQUITY OIL & GAS FUNDS INC 0.00 360.00 365
2015 EQUITY OIL & GAS FUNDS INC 0.00 122.00 335
2016 EQUITY OIL & GAS FUNDS INC 0.00 0.00 335
2017 EQUITY OIL & GAS FUNDS INC 0.00 125.00 335

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 INLAND DRILLING CO INC Brine 0 365
1986 INLAND DRILLING CO INC Brine 35 151
1987 INLAND DRILLING CO INC Brine 0 0
1988 INLAND DRILLING CO INC Brine 0 0
1989 INLAND DRILLING CO INC Brine 116 60
1990 INLAND DRILLING CO INC Brine 139 365
1991 INLAND DRILLING CO INC Brine 319 365
1992 INLAND DRILLING CO INC Brine 242 275
1993 EQUITY OIL & GAS FUNDS INC Brine 572 365
1994 EQUITY OIL & GAS FUNDS INC Brine 430 365
1995 EQUITY OIL & GAS FUNDS INC Brine 352 365
1996 EQUITY OIL & GAS FUNDS INC Brine 479 365
1997 EQUITY OIL & GAS FUNDS INC Brine 367 365
1998 EQUITY OIL & GAS FUNDS INC Brine 320 365
1999 EQUITY OIL & GAS FUNDS INC Brine 313 365
2000 EQUITY OIL & GAS FUNDS INC Brine 345 365
2001 EQUITY OIL & GAS FUNDS INC Brine 129 365
2002 EQUITY OIL & GAS FUNDS INC Brine 351 365
2003 EQUITY OIL & GAS FUNDS INC Brine 368 365
2004 EQUITY OIL & GAS FUNDS INC Brine 141 365
2005 EQUITY OIL & GAS FUNDS INC Brine 21 365
2006 EQUITY OIL & GAS FUNDS INC Brine 132 365
2007 EQUITY OIL & GAS FUNDS INC Brine 213 365
2008 EQUITY OIL & GAS FUNDS INC Brine 0 365
2009 EQUITY OIL & GAS FUNDS INC Brine 60 365
2010 EQUITY OIL & GAS FUNDS INC Brine 0 365
2011 EQUITY OIL & GAS FUNDS INC Brine 230
2012 EQUITY OIL & GAS FUNDS INC Brine 195 366
2013 EQUITY OIL & GAS FUNDS INC Brine 195 365
2014 EQUITY OIL & GAS FUNDS INC Brine 162 365
2015 EQUITY OIL & GAS FUNDS INC Brine 136 335
2016 EQUITY OIL & GAS FUNDS INC Brine 42 335
2017 EQUITY OIL & GAS FUNDS INC Brine 223 335

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1554937915 2004-2-5 0:00:0 PW No Violations
1055513447 2003-06-02 Production Wells Violations Noted CASE 03-022 The Uniontown office received a complaint from Ms. Connie Bejger regarding abandoned equipment on property she has purchased. The equipment consists of a 210 bbl tank and a pump jack. Equity was contacted and stated that they would removed the equipment as soon as possible.
1057018266 2003-06-16 Production Wells No Violations CASE 03-022 The abandoned 210 bbl stock tank and the abandoned pump jack were loaded on a truck and were being removed. The violation has been corrected.
1250191471 2009-08-11 Production Wells No Violations CASE 09-003

The Columbus office received a complaint from Ms. Connie Bejger at 8553 Werger Road in Windham Township, Portage County. The well involved is the L&P #1 operated by Equity Oil & Gas. The complaint involved the onsite disposal of vines and branches that Equity removed from the tank battery and ruts that were created when Equity worked on the separator. This inspection found no evidence of debris piles in the woods west of the tank battery and the complaintant is mowing next to the containment dike around the tank battery and near the separator. The only issue is the height of vegetation inside the tank battery. There are no violations at this time.

1554937915 2004-02-05 Production Wells No Violations CASE 04-004 Pipeline leak has been repaired.
1964385146 2004-02-04 Production Wells No Violations CASE 04-004 I received a call from the complaintant that the gas leak near the Pascizynk tank battery had returned. An area four feet across 20 feet due south of the tank battery had gas bubbling to surface. There was no sheen. I contacted Everflow who again stated that the gas line inquestion was not theirs. The next well west of the Pascizynk is the L&P #1 operated by Equity Oil & Gas. I contacted Equity who confirmed that the sales line was theirs. I met on site with Don Toth who stated that Wade Pol Contracting would be on site the next day to repair the leak. I informed the complaintant.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1055513447 US-OH-101015 2003-06-13 Improperly located oil tank

For data sources see[9]

References