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Well ID: 34-133-23622 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Freedom Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: CHAPPELL | |
License Status: Final Restoration | |
License Date: 2013-05-08 | |
Spud Date: 1988-01-10 | |
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]] | |
Final Drill Date: 1988-01-16 | |
Well Total Depth: 4500.00 ft | |
Configuration: Vertical | |
Latitude: 41.220000 | |
Longitude: -81.140000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-09-24 | 132 NOBLE OIL CORP GeoDate 9/24/87 |
Oil and Gas | 1987-09-24 | Issued Date 9/24/87 Expired Date 9/23/88 Acres 0087590 Tool Type RTF Proposed Formation CLINTON Proposed Depth 04500 Proposed Drill Depth 04500 |
Original Spud | 1988-01-10 | |
Completed | 1988-01-16 | |
Reached Total Depth | 1988-01-16 | |
Completion Report Received | 1988-02-05 | |
CO | 1996-06-07 | 4884 EASTERN STATES OIL & GAS GeoDate 9/24/87 |
Change of Owner | 2003-04-09 | Operator changed from 4884, EASTERN STATES OIL & GAS INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
APP | 2013-05-08 | Proposed Formations:CLINTON, Issued Date:5/8/2013, Expired Date:5/8/2015 12:00:00 PM, Drilling unit acres:87, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-01-24 | |
Construction Permit Expires | 2015-05-08 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4378 | 4483 | 0 |
4378 | 4483 | 0 | |
2006-09-11 | 4415 | 4452 | 19 |
4415 | 4452 | 19 | |
4378 | 4483 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1780 Bbl | 55000 | |||
ACID | 0 | 500 Gal | 0 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | NOBLE OIL CORP | 1431.00 | 1590.00 | 334 |
1989 | NOBLE OIL CORP | 1644.00 | 839.00 | 365 |
1990 | NOBLE OIL CORP | 1152.00 | 577.00 | 365 |
1991 | NOBLE OIL CORP | 588.00 | 359.00 | 365 |
1992 | NOBLE OIL CORP | 751.00 | 369.00 | 365 |
1993 | NOBLE OIL CORP | 603.00 | 141.00 | 365 |
1994 | NOBLE OIL CORP | 698.00 | 252.00 | 365 |
1995 | NOBLE OIL CORP | 407.00 | 253.00 | 365 |
1996 | EASTERN STATES OIL & GAS INC | 518.00 | 235.00 | 365 |
1997 | EASTERN STATES OIL & GAS INC | 659.00 | 396.00 | 365 |
1998 | EASTERN STATES OIL & GAS INC | 9110.00 | 688.00 | 365 |
1999 | EASTERN STATES OIL & GAS INC | 557.00 | 656.00 | 365 |
2000 | EASTERN STATES OIL & GAS INC | 515.00 | 0.00 | 365 |
2001 | EASTERN STATES OIL & GAS INC | 536.00 | 1626.00 | 365 |
2002 | EASTERN STATES OIL & GAS INC | 813.00 | 308.00 | 365 |
2003 | EASTERN STATES OIL & GAS INC | 99.00 | 31.00 | 59 |
2004 | RANGE RESOURCES-APPALACHIA LLC | 189.00 | 48.00 | 365 |
2005 | RANGE RESOURCES-APPALACHIA LLC | 214.00 | 111.00 | 365 |
2006 | RANGE RESOURCES-APPALACHIA LLC | 10.00 | 59.00 | 181 |
2007 | RANGE RESOURCES-APPALACHIA LLC | 1.00 | 0.00 | 28 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1019988233 | 2014-1-21 0:00: | PB | No Violations | 1.00 |
-546311683 | 2014-1-23 0:00: | PB | No Violations | 8.70 |
0000PL5844 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0492378811 | 2015-11-02 | Final Restoration | No Violations | I was on location to inspect for Final Restoration approval. The well was plugged and abandoned on 1/24/2014. I have received the landowner waiver from Enervest and Doug Smith (landowner) has waived restoration of the lease road and removal of the flow line. My inspection found that the site is graded and vegetative cover is well established. All production equipment has been removed. Final Restoration is approved. No violations. |
0546311683 | 2014-01-23 | Plug / Plug Back | No Violations | I was on location to witness the plugging of this well. Nicks Well Plugging was on location to conduct operations. Extremely cold conditions caused numerous delays throughout the morning in getting the equipment thawed out. After testing equipment, a 30 sack plug was bullheaded to the perforations in the Clinton Sandstone. The well locked up at 1700psi and pumping stopped. After 30 minutes, the pressure had disapated to 0psi and the cement head was removed. The pipe was ripped at 2976 and 4 joints of 9.5lb/ft, 4.5 casing was pulled to the depth of the next plug. At this point, it was decided to shut down for the day and bring out a different pump truck to finish the job in the morning. The wellhead was packed off and I left location. No violations. See plugging report for more details on this job. |
0676779898 | 2014-01-24 | Plug / Plug Back | No Violations | I was on location to witness the plugging of this well. Plugs were set across the top of the Big Lime, at the bottom of the 8.625 surface casing, and at the top of the surface casing. All plugs circulated prior to pumping the slurry and were set through 9.5lb/ft, 4.5 casing. The final plug circulated to surface and the hole was topped of after pulling the final joint of casing. The plug held at the surface, the casing was cut off below grade and was fitted with an ID plate. See plug report for details on this job. No violations. |
1019988233 | 2014-01-21 | Plug / Plug Back | No Violations | I was on location to check the progress of pulling the rods and tubing from this well. Heavy paraffins have built up in the tubing and require stripping. Nicks Well Plugging is making progress and will be ready to start plugging the well by 1/23/14. No violations. |
492378811 | 2015-11-2 0:00: | FR | No Violations | 0.50 |
676779898 | 2014-1-24 0:00: | PB | No Violations | |
PL5844 | PL | No Violations |
For data sources see[9]