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34-133-23678

Well Details

Well ID: 34-133-23678
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Country: United States
State: Ohio
County: Portage
Municipality: Deerfield Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: KOR-KEL UNIT
License Status: Producing
License Date: 1988-09-13
Spud Date: 1988-09-21
Spud Drilling Contractor: IPSCO
Final Drill Date: 1988-09-24
Well Total Depth: 4927.00 ft
Configuration: Vertical
Latitude: 41.040000
Longitude: -81.070000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1988-09-13 Issued Date 9/13/88 Expired Date 9/13/89 Acres 0080000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04927 Proposed Drill Depth 04927
Original Spud 1988-09-21
Completed 1988-09-24
Reached Total Depth 1988-09-24
Completion Report Received 1988-10-21
CO 1988-11-15 198 VIKING RESOURCES CORP GeoDate 9/13/88
Construction Permit Expires 1989-09-13
Change of Owner 2017-10-17 Operator changed from 198, VIKING RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-10-17

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4742 4866 0
4742 4866 0
2006-09-11 4750 4829 2
4750 4829 2
4742 4866 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 114440 Gal 75000 FRAC: WATER, SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 VIKING RESOURCES LLC 134.00 447.00 365
1990 VIKING RESOURCES LLC 8739.00 3678.00 184
1991 VIKING RESOURCES LLC 6704.00 2428.00 294
1992 VIKING RESOURCES LLC 7068.00 2513.00 304
1993 VIKING RESOURCES LLC 6230.00 1859.00 365
1994 VIKING RESOURCES LLC 5613.00 1739.00 365
1995 VIKING RESOURCES LLC 5232.00 1399.00 30
1996 VIKING RESOURCES LLC 4666.00 1301.00 0
1997 VIKING RESOURCES LLC 3432.00 947.00 0
1998 VIKING RESOURCES LLC 2370.00 716.00 365
2000 RESOURCE AMERICA INC 2804.00 1243.00 365
2001 VIKING RESOURCES LLC 2691.00 701.00 365
2002 VIKING RESOURCES LLC 2277.00 1006.00 365
2003 VIKING RESOURCES LLC 2870.00 910.00 365
2004 VIKING RESOURCES LLC 2748.00 766.00 365
2005 VIKING RESOURCES LLC 2865.00 763.00 365
2006 VIKING RESOURCES LLC 2996.00 722.00 365
2007 VIKING RESOURCES LLC 3142.00 558.00 365
2008 VIKING RESOURCES LLC 2796.00 601.00 366
2009 VIKING RESOURCES LLC 3002.00 551.00 365
2010 VIKING RESOURCES LLC 2597.00 504.00 365
2011 VIKING RESOURCES LLC 1322.00 207.00 0
2012 VIKING RESOURCES LLC 776.00 186.00 366
2013 VIKING RESOURCES LLC 0.00 0.00 365
2014 VIKING RESOURCES LLC 0.00 0.00 365
2015 VIKING RESOURCES LLC 0.00 0.00 365
2016 VIKING RESOURCES LLC 0.00 0.00 366
2017 VIKING RESOURCES LLC 0.00 0.00 182
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 VIKING RESOURCES LLC Brine 160 365
1990 VIKING RESOURCES LLC Brine 605 184
1991 VIKING RESOURCES LLC Brine 510 294
1992 VIKING RESOURCES LLC Brine 708 304
1993 VIKING RESOURCES LLC Brine 838 365
1994 VIKING RESOURCES LLC Brine 1198 365
1995 VIKING RESOURCES LLC Brine 1054 30
1996 VIKING RESOURCES LLC Brine 838 0
1997 VIKING RESOURCES LLC Brine 660 0
1998 VIKING RESOURCES LLC Brine 675 365
2000 RESOURCE AMERICA INC Brine 0 365
2001 VIKING RESOURCES LLC Brine 0 365
2002 VIKING RESOURCES LLC Brine 854 365
2003 VIKING RESOURCES LLC Brine 0 365
2004 VIKING RESOURCES LLC Brine 0 365
2005 VIKING RESOURCES LLC Brine 0 365
2006 VIKING RESOURCES LLC Brine 0 365
2007 VIKING RESOURCES LLC Brine 0 365
2008 VIKING RESOURCES LLC Brine 0 366
2009 VIKING RESOURCES LLC Brine 0 365
2010 VIKING RESOURCES LLC Brine 0 365
2011 VIKING RESOURCES LLC Brine 40
2012 VIKING RESOURCES LLC Brine 40 366
2013 VIKING RESOURCES LLC Brine 0 365
2014 VIKING RESOURCES LLC Brine 40 365
2015 VIKING RESOURCES LLC Brine 0 365
2016 VIKING RESOURCES LLC Brine 80 366
2017 VIKING RESOURCES LLC Brine 0 182
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL5811 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1469722920 2016-07-28 Production Wells Violations Noted Follow-up to Complaint #5383 concerning a gas odor emanating from this well and creating an unnecessary nuisance and possible hazard for the residents residing at 1923 State Route 14 located 220 NNE of this wellhead. My inspection of the wellhead found the base of the electric pumping has lifted off of the ground 4-5 below the weights. This shift of the units base has forced the polished rod off center, to the front of the wellhead, and damaged the top of the tubing, the pumping tee, and the stuffing box. The tubing and pumping tee are thickly wrapped in black tape to contain gas leaking from the damaged parts. I can hear a minor amount of gas leaking from the top of the well and there is an obvious odor of methane around the wellhead. The man door on the security fencing has been fitted with a lock out-tag out notice to not operate the unit. I spoke with Rusty Morrison (Atlas/Viking) and informed him that a Compliance Notice would be issued for general safety and defective casing (tubing) allowing the well to leak gas to the atmosphere. I asked him to repair the wellhead immediately to stop the release of methane. He told me that they have a service rig scheduled to come in two (2) weeks and I asked him to put this repair at the top of the list. Viking/Atlas will be given two (2) weeks to repair the wellhead and remediate the gas leak or further administrative action will be sought.
1474987246 2016-09-19 Production Wells No Violations Follow-up to Complaint #5383 and Compliance Notice #1469722920. My inspection today found that the pumping unit has been unhooked and the base of the unit is now safely on the ground. Ditty Well Service has removed the damaged pumping tee and polished rod. They pulled the damaged, top joint of tubing and one rod from the wellhead and have secured the tubing in the hole. A pup joint of tubing has been installed in the wellhead with a 2 ball valve and packed off. The well is no longer leaking methane at the wellhead and the safety issue with the pumping unit has been resolved. I spoke with Rusty Morrison (Viking) and he told me that the well would be produced on bypass through the 4.5 production casing until workover of the well takes place. This Complaint and the associated Compliance Notice are resolved and can be closed.
PL5811 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1469722920 US-OH-113512 2017-01-10 General Safety
1469722920 US-OH-113513 2017-01-10 Defective casing, leaking well

For data sources see[9]

References