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Well ID: 34-133-23678 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Deerfield Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: KOR-KEL UNIT | |
License Status: Producing | |
License Date: 1988-09-13 | |
Spud Date: 1988-09-21 | |
Spud Drilling Contractor: IPSCO | |
Final Drill Date: 1988-09-24 | |
Well Total Depth: 4927.00 ft | |
Configuration: Vertical | |
Latitude: 41.040000 | |
Longitude: -81.070000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1988-09-13 | Issued Date 9/13/88 Expired Date 9/13/89 Acres 0080000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04927 Proposed Drill Depth 04927 |
Original Spud | 1988-09-21 | |
Completed | 1988-09-24 | |
Reached Total Depth | 1988-09-24 | |
Completion Report Received | 1988-10-21 | |
CO | 1988-11-15 | 198 VIKING RESOURCES CORP GeoDate 9/13/88 |
Construction Permit Expires | 1989-09-13 | |
Change of Owner | 2017-10-17 | Operator changed from 198, VIKING RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-10-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4742 | 4866 | 0 |
4742 | 4866 | 0 | |
2006-09-11 | 4750 | 4829 | 2 |
4750 | 4829 | 2 | |
4742 | 4866 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 114440 Gal | 75000 | FRAC: WATER, SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | VIKING RESOURCES LLC | 134.00 | 447.00 | 365 |
1990 | VIKING RESOURCES LLC | 8739.00 | 3678.00 | 184 |
1991 | VIKING RESOURCES LLC | 6704.00 | 2428.00 | 294 |
1992 | VIKING RESOURCES LLC | 7068.00 | 2513.00 | 304 |
1993 | VIKING RESOURCES LLC | 6230.00 | 1859.00 | 365 |
1994 | VIKING RESOURCES LLC | 5613.00 | 1739.00 | 365 |
1995 | VIKING RESOURCES LLC | 5232.00 | 1399.00 | 30 |
1996 | VIKING RESOURCES LLC | 4666.00 | 1301.00 | 0 |
1997 | VIKING RESOURCES LLC | 3432.00 | 947.00 | 0 |
1998 | VIKING RESOURCES LLC | 2370.00 | 716.00 | 365 |
2000 | RESOURCE AMERICA INC | 2804.00 | 1243.00 | 365 |
2001 | VIKING RESOURCES LLC | 2691.00 | 701.00 | 365 |
2002 | VIKING RESOURCES LLC | 2277.00 | 1006.00 | 365 |
2003 | VIKING RESOURCES LLC | 2870.00 | 910.00 | 365 |
2004 | VIKING RESOURCES LLC | 2748.00 | 766.00 | 365 |
2005 | VIKING RESOURCES LLC | 2865.00 | 763.00 | 365 |
2006 | VIKING RESOURCES LLC | 2996.00 | 722.00 | 365 |
2007 | VIKING RESOURCES LLC | 3142.00 | 558.00 | 365 |
2008 | VIKING RESOURCES LLC | 2796.00 | 601.00 | 366 |
2009 | VIKING RESOURCES LLC | 3002.00 | 551.00 | 365 |
2010 | VIKING RESOURCES LLC | 2597.00 | 504.00 | 365 |
2011 | VIKING RESOURCES LLC | 1322.00 | 207.00 | 0 |
2012 | VIKING RESOURCES LLC | 776.00 | 186.00 | 366 |
2013 | VIKING RESOURCES LLC | 0.00 | 0.00 | 365 |
2014 | VIKING RESOURCES LLC | 0.00 | 0.00 | 365 |
2015 | VIKING RESOURCES LLC | 0.00 | 0.00 | 365 |
2016 | VIKING RESOURCES LLC | 0.00 | 0.00 | 366 |
2017 | VIKING RESOURCES LLC | 0.00 | 0.00 | 182 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | VIKING RESOURCES LLC | Brine | 160 | 365 |
1990 | VIKING RESOURCES LLC | Brine | 605 | 184 |
1991 | VIKING RESOURCES LLC | Brine | 510 | 294 |
1992 | VIKING RESOURCES LLC | Brine | 708 | 304 |
1993 | VIKING RESOURCES LLC | Brine | 838 | 365 |
1994 | VIKING RESOURCES LLC | Brine | 1198 | 365 |
1995 | VIKING RESOURCES LLC | Brine | 1054 | 30 |
1996 | VIKING RESOURCES LLC | Brine | 838 | 0 |
1997 | VIKING RESOURCES LLC | Brine | 660 | 0 |
1998 | VIKING RESOURCES LLC | Brine | 675 | 365 |
2000 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2001 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2002 | VIKING RESOURCES LLC | Brine | 854 | 365 |
2003 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2004 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2005 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2006 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2007 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2008 | VIKING RESOURCES LLC | Brine | 0 | 366 |
2009 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2010 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2011 | VIKING RESOURCES LLC | Brine | 40 | |
2012 | VIKING RESOURCES LLC | Brine | 40 | 366 |
2013 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2014 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2015 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2016 | VIKING RESOURCES LLC | Brine | 80 | 366 |
2017 | VIKING RESOURCES LLC | Brine | 0 | 182 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL5811 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1469722920 | 2016-07-28 | Production Wells | Violations Noted | Follow-up to Complaint #5383 concerning a gas odor emanating from this well and creating an unnecessary nuisance and possible hazard for the residents residing at 1923 State Route 14 located 220 NNE of this wellhead. My inspection of the wellhead found the base of the electric pumping has lifted off of the ground 4-5 below the weights. This shift of the units base has forced the polished rod off center, to the front of the wellhead, and damaged the top of the tubing, the pumping tee, and the stuffing box. The tubing and pumping tee are thickly wrapped in black tape to contain gas leaking from the damaged parts. I can hear a minor amount of gas leaking from the top of the well and there is an obvious odor of methane around the wellhead. The man door on the security fencing has been fitted with a lock out-tag out notice to not operate the unit. I spoke with Rusty Morrison (Atlas/Viking) and informed him that a Compliance Notice would be issued for general safety and defective casing (tubing) allowing the well to leak gas to the atmosphere. I asked him to repair the wellhead immediately to stop the release of methane. He told me that they have a service rig scheduled to come in two (2) weeks and I asked him to put this repair at the top of the list. Viking/Atlas will be given two (2) weeks to repair the wellhead and remediate the gas leak or further administrative action will be sought. |
1474987246 | 2016-09-19 | Production Wells | No Violations | Follow-up to Complaint #5383 and Compliance Notice #1469722920. My inspection today found that the pumping unit has been unhooked and the base of the unit is now safely on the ground. Ditty Well Service has removed the damaged pumping tee and polished rod. They pulled the damaged, top joint of tubing and one rod from the wellhead and have secured the tubing in the hole. A pup joint of tubing has been installed in the wellhead with a 2 ball valve and packed off. The well is no longer leaking methane at the wellhead and the safety issue with the pumping unit has been resolved. I spoke with Rusty Morrison (Viking) and he told me that the well would be produced on bypass through the 4.5 production casing until workover of the well takes place. This Complaint and the associated Compliance Notice are resolved and can be closed. |
PL5811 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1469722920 | US-OH-113512 | 2017-01-10 | General Safety | |
1469722920 | US-OH-113513 | 2017-01-10 | Defective casing, leaking well |
For data sources see[9]