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34-133-23828

Well Details

Well ID: 34-133-23828
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Country: United States
State: Ohio
County: Portage
Municipality: Charlestown Township
Operator Name: MAJESTIC OIL & GAS INC
Well Pad ID:
Farm/Lease Name: JONES-ROGERS
License Status: Final Restoration
License Date: 1991-01-02
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1991-01-24
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 41.180000
Longitude: -81.190000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1991-01-02 2336 MAJESTIC OIL & GAS INC GeoDate 1/2/91
Oil and Gas 1991-01-02 Issued Date 1/2/91 Expired Date 1/2/92 Acres 0060000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1991-01-24
Reached Total Depth 1991-01-24
Plugged/Abandoned 1991-01-25
Construction Permit Expires 1992-01-02
Record Last Modified 2013-03-14

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-877237887 2002-6-18 0:00: PW No Violations 1.00
0000003192 Final Restoration No Violations PASSED WITNESSED INSPECTOR DATE 00/0019/00 DATA FROM OLD VAX INFO
0000003194 Final Restoration No Violations PASSED WITNESSED INSPECTOR DATE 00/0019/00 DATA FROM OLD VAX INFO
0000003196 Final Restoration No Violations PASSED WITNESSED INSPECTOR DATE 00/0019/00 DATA FROM OLD VAX INFO
002154i212 2002-06-18 Production Wells Violations Noted Random inspection. Discovered a flowline leak approx. 30 feet from the pumpjack. Found crude oil staining and absorbent pads floating in the tank battery dike. Issued N.O.V. Repair flowline leak; clean up around wellhead and stuffing box; pick up absorbent pads; remove oil staining in dike; and vac out the water in the tank battery dike. Informed Chuck Baker of Equity Oil & Gas.
002154i261 2002-07-02 Production Wells Violations Noted Flowline leak has been repaired. Tank battery has not been cleaned up.
002154i394 2002-08-22 Production Wells Violations Noted Pollution and contamination have been resolved. Still needs I.D. sign.
0028778991 2002-07-17 Production Wells No Violations Tank battery dike has not been cleaned up. Called Chuck Baker. Issued an extension for the clean up.
0877237887 2002-06-18 Production Wells Violations Noted FOLLOW UP TO NOV # 2154i212 Random inspection. Discovered a flowline leak approx. 30 feet from the pumpjack. Found crude oil staining and absorbent pads floating in the tank battery dike. Issued N.O.V. Repair flowline leak; clean up around wellhead and stuffing box; pick up absorbe
2154i212 2002-6-18 0:00: PW No Violations 1.00
2154i261 2002-7-2 0:00:0 PW No Violations 1.00
2154i394 2002-8-22 0:00: PW No Violations 0.50
28778991 2002-7-17 0:00: PW No Violations 0.50
3192 FR No Violations
3194 FR No Violations
3196 FR No Violations
iANGE00046 1997-08-12 Final Restoration No Violations
iANGE000460 1997-8-12 0:00: FR No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
002154i212 US-OH-122070 2002-06-18 Well operation causing pollution and contamination
002154i261 US-OH-122085 2002-07-02 Well operation causing pollution and contamination
002154i394 US-OH-121997 2002-08-22 Failure to legibly identify well
0877237887 US-OH-129989 2002-06-18 Well operation causing pollution and contamination
0877237887 US-OH-129990 2002-08-22 Failure to legibly identify well

For data sources see[3]

References