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34-151-21261

Well Details

Well ID: 34-151-21261
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Country: United States
State: Ohio
County: Stark
Municipality: Osnaburg Township
Operator Name: G & O RESOURCES LTD
Well Pad ID:
Farm/Lease Name: WALTERS ADDITION
License Status: Final Restoration
License Date: 2014-05-22
Spud Date: 1967-07-28
Spud Drilling Contractor:
Final Drill Date: 1967-08-25
Well Total Depth: 5000.00 ft
Configuration: Vertical
Latitude: 40.790000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Unknown 1802-01-01
Original Spud 1967-07-28
Completed 1967-08-25
Reached Total Depth 1967-08-25
CO 1993-07-29 1071 FIDELITY PETROLEUM CORP
CO 1993-07-29 4280 JRD ENERGY GeoDate
Change of Owner 1997-08-04 Operator changed from 4280, JRD ENERGY to 5894, G & O RESOURCES LTD
APP 2014-05-22 Proposed Formations:CLINTON, Issued Date:5/22/2014, Expired Date:5/21/2016 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-10-20
Construction Permit Expires 2016-05-21
Record Last Modified 2017-10-12

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4849 4936 2
4849 4936 2
4849 4936 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 79000 Gal 80500

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 FIDELITY PETROLEUM CORP 522.00 328.00 0
1987 FIDELITY PETROLEUM CORP 769.00 191.00 180
1988 FIDELITY PETROLEUM CORP 517.00 164.00 180
1989 FIDELITY PETROLEUM CORP 290.00 212.00 180
1990 FIDELITY PETROLEUM CORP 694.00 191.00 180
1991 FIDELITY PETROLEUM CORP 627.00 202.00 180
1992 FIDELITY PETROLEUM CORP 772.00 200.00 120
1993 JRD ENERGY 0.00 104.00 150
1994 JRD ENERGY 294.00 195.00 365
1995 JRD ENERGY 247.00 180.00 365
1996 JRD ENERGY 608.00 287.00 365
1997 JRD ENERGY 352.00 90.00 197
1998 G & O RESOURCES LTD 565.00 212.00 365
1999 G & O RESOURCES LTD 493.00 151.00 360
2000 G & O RESOURCES LTD 451.00 144.00 330
2001 G & O RESOURCES LTD 345.00 183.00 365
2002 G & O RESOURCES LTD 247.00 88.00 365
2003 G & O RESOURCES LTD 321.00 142.00 365
2004 G & O RESOURCES LTD 47.00 135.00 365
2005 G & O RESOURCES LTD 23.00 146.00 365
2006 G & O RESOURCES LTD 0.00 47.00 365
2007 G & O RESOURCES LTD 0.00 161.00 365
2008 G & O RESOURCES LTD 0.00 86.00 366
2009 G & O RESOURCES LTD 0.00 0.00 0
2010 G & O RESOURCES LTD 0.00 31.00 365
2011 G & O RESOURCES LTD 0.00 0.00 0
2012 G & O RESOURCES LTD 0.00 0.00 0
2013 G & O RESOURCES LTD 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 FIDELITY PETROLEUM CORP Brine 35 0
1987 FIDELITY PETROLEUM CORP Brine 19 180
1988 FIDELITY PETROLEUM CORP Brine 15 180
1989 FIDELITY PETROLEUM CORP Brine 20 180
1990 FIDELITY PETROLEUM CORP Brine 18 180
1991 FIDELITY PETROLEUM CORP Brine 20 180
1992 FIDELITY PETROLEUM CORP Brine 20 120
1993 JRD ENERGY Brine 79 150
1994 JRD ENERGY Brine 165 365
1995 JRD ENERGY Brine 173 365
1996 JRD ENERGY Brine 174 365
1997 JRD ENERGY Brine 94 197
1998 G & O RESOURCES LTD Brine 252 365
1999 G & O RESOURCES LTD Brine 480 360
2000 G & O RESOURCES LTD Brine 83 330
2001 G & O RESOURCES LTD Brine 42 365
2002 G & O RESOURCES LTD Brine 23 365
2003 G & O RESOURCES LTD Brine 39 365
2004 G & O RESOURCES LTD Brine 28 365
2005 G & O RESOURCES LTD Brine 24 365
2006 G & O RESOURCES LTD Brine 14 365
2007 G & O RESOURCES LTD Brine 8 365
2008 G & O RESOURCES LTD Brine 0 366
2009 G & O RESOURCES LTD Brine 0 0
2010 G & O RESOURCES LTD Brine 0 365
2011 G & O RESOURCES LTD Brine 0 0
2012 G & O RESOURCES LTD Brine 0 0
2013 G & O RESOURCES LTD Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1479616099 2015-5-21 0:00: FR No Violations 2.00
-356197404 2014-10-23 0:00 FR No Violations 2.00
-498598961 2015-4-30 0:00: FR No Violations 2.00
-571113752 2014-12-30 0:00 FR No Violations 1.50
-955474631 2015-6-16 0:00: FR No Violations 1.00
0178961674 2015-01-23 Final Restoration No Violations I was on location to follow up to complaint #4668. The concrete pad located inside the tank battery has been identified as the base for the vertical separator in the well. I have contacted G&O Resources and informed them that they must remove the power poles present at the location, the separator concrete pad and grade and seed the location. The contractor has my contact and will inform me when they will be on location to perform the work.
0349078641 2014-10-20 Plug / Plug Back No Violations
0356197404 2014-10-23 Final Restoration No Violations I was on location to check the status of restoration of this location following the plugging of the this well. The well has been plugged and the casing cut down below grade and covered with soil. The location is muddy and will be graded flat and seeded. The tank battery and steam tubs from the tubing are still on location and will need removed from location and cleaned.
0498598961 2015-04-30 Final Restoration No Violations I was on location to follow up to complaint #4668. The final restoration for this well has not been completed at this time. The location has been seeded but not graded. The concrete pad for the separator is still present and the power poles for the pumpjack are still on location and have not been removed. The landowner was contacted by Lakeside regarding the restoration of the location. The landowner and Lakeside would like to set up a meeting at the location to discuss the final restoration on the well. I have left a message for Ron at Lakeside regarding the meeting. The 6 month period for final restoration has passed at this time.
0571113752 2014-12-30 Final Restoration No Violations I was on location to check the status of final restoration. The location has been seeded and had straw layer down. The location was not graded, the flow lines are still present, the brine vault is still present in the former tank battery and the power line poles to the pumpjack have not been removed. I have called the G&O office and left a message with the secretary and Bill Lavin informing the company that these issues need addressed before final restoration will be passed.
0955474631 2015-06-16 Final Restoration No Violations I was on location to check the status of reclaim. The location has been seeded and straw has been spread on location. Lakeside has graded the location flat and straw has been spread to assist in vegetation growing. There is no evidence of the well leaking the complaint associated with this well has been closed.
1398095295 2014-04-21 Production Wells Violations Noted I was on location to perform an inspection of this well regarding complaint #4668. During my inspection I found a graveled lease road that is used as a residential driveway. The tank battery consists of two empty 210 bbls production tanks and a vertical separator, all within an earthen dike. The tank battery and well have an I.D. sign present but it is not legible. The pump jack well does not have the required shroud around the drive belts and electric motor. There is a house gas connection on the well but it is not currently functioning. I have contacted the operator and informed them of the issues. This well is currently on the G&O Resources plugging list when plugging funds are available. The only production shown for this well since 2009 is 31 barrels of oil produced in 2010. This well shall be plugged with 180 days as required by ORC 1509.12B.
1413304733 2014-10-14 Plug / Plug Back No Violations I was on location to check the status of Steve Hagen Well Service plugging this well. The rig is on location and the area is being lined with plastic. The plugging of the well and the plug schedule was discussed and it was decided plugs would be set through tubing due to concerns with 4.5 diameter production casing integrity. They will pull rods today and prepare to cement tomorrow 10-15-2014.
1413893168 2014-10-16 Plug / Plug Back No Violations

-in for the night.

1427900506 2015-04-01 Final Restoration No Violations I was on location to follow up to complaint #4668. No additional restoration work has been conducted on this well since the last inspection on 1/23/2015. The 6 month timeframe for final restoration will be on 4/20/2015. Currently the power poles, concrete base for the separator, lease road and ruts in the straw covered ground are present. These issue must be addressed before restoration will be passed.
1430919431 2015-05-05 Final Restoration No Violations I was on the location with the landowner and Ron of Lakeside to agree upon the final restoration for this well. The power poles will be pulled from the ground and left on location for a contractor to remove. The concrete pad for the separator will be removed and the lease road up to the driveway will be graded and seeded. The location will be graded level, rocks removed and seeded so that the yard can be brought back to a condition that will allow for it to be mowed with a lawnmower. This work will begin within a week and at when the work completed final restoration can be passed.
1479287150 2015-01-13 Final Restoration No Violations I was on location to check the final restoration for this well and complaint #4668. The location has been seeded and straw spread, but restoration not passed. The location needs to be graded flat, the power poles removed and the brine vault removed from the ground. The G & O office has been contacted and informed of these findings. The final restoration requirements need to be completed before it can be passed.
1479616099 2015-05-21 Final Restoration No Violations I was on location to follow up to complaint #4668. The final restoration for this well has not been completed at this time. The location has been graded. The concrete pad for the separator and the power poles for the pumpjack have been removed. A dozer and tractor with a rake is on location for the final dirt work, the location is going to be seeded and when vegetation has been established final restoration will be passed.
1505481067 2017-09-15 Final Restoration No Violations I did a Final Restoration status check on this well. The well was plugged on10-20-2014 and witnessed by Inspector Fred Romeo. There is no visual evidence of the well. The well site has been graded and is being maintained as a lawn. There is a plugging report on file. The final restoration is passed.
178961674 2015-1-23 0:00: FR No Violations 2.00
349078641 2014-10-20 0:00 PB No Violations 4.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1398095295 US-OH-111782 2014-11-03 General Safety
1398095295 US-OH-111783 2014-11-03 Failure to legibly identify well
1398095295 US-OH-111784 2014-11-03 Well shall be plugged

For data sources see[9]

References