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Well ID: 34-151-23155 | Loading map...
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Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Bethlehem Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLHONE D & B | |
License Status: Final Restoration | |
License Date: 2012-01-05 | |
Spud Date: 1980-05-28 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1980-06-01 | |
Well Total Depth: 4551.00 ft | |
Configuration: Vertical | |
Latitude: 40.660000 | |
Longitude: -81.490000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-03-03 | 139 MB OPERATING CO INC GeoDate 3/3/80 |
Original Spud | 1980-05-28 | |
Completed | 1980-06-01 | |
Reached Total Depth | 1980-06-01 | |
Change of Owner | 2000-06-30 | Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
APP | 2012-01-05 | Proposed Formations:CLINTON, Issued Date:1/5/2012, Expired Date:1/4/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-05-10 | |
Construction Permit Expires | 2014-01-04 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-11-02 | 4331 | 4384 | 18 |
4331 | 4384 | 18 | |
4331 | 4384 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 4669 Bbl | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MB OPERATING CO INC | 6499.00 | 190.00 | 0 |
1985 | MB OPERATING CO INC | 5681.00 | 204.00 | 365 |
1986 | MB OPERATING CO INC | 4600.00 | 93.00 | 365 |
1987 | MB OPERATING CO INC | 2962.00 | 181.00 | 365 |
1988 | MB OPERATING CO INC | 2658.00 | 167.00 | 366 |
1989 | MB OPERATING CO INC | 2132.00 | 95.00 | 365 |
1990 | MB OPERATING CO INC | 1767.00 | 176.00 | 365 |
1991 | MB OPERATING CO INC | 994.00 | 176.00 | 365 |
1992 | MB OPERATING CO INC | 1559.00 | 75.00 | 366 |
1993 | MB OPERATING CO INC | 1270.00 | 107.00 | 365 |
1994 | MB OPERATING CO INC | 1328.00 | 35.00 | 365 |
1995 | MB OPERATING CO INC | 755.00 | 80.00 | 365 |
1996 | MB OPERATING CO INC | 1210.00 | 170.00 | 366 |
1997 | MB OPERATING CO INC | 885.00 | 84.00 | 365 |
1998 | MB OPERATING CO INC | 903.00 | 83.00 | 365 |
1999 | MB OPERATING CO INC | 0.00 | 26.00 | 273 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MB OPERATING CO INC | Brine | 0 | 0 |
1985 | MB OPERATING CO INC | Brine | 0 | 365 |
1986 | MB OPERATING CO INC | Brine | 0 | 365 |
1987 | MB OPERATING CO INC | Brine | 0 | 365 |
1988 | MB OPERATING CO INC | Brine | 70 | 366 |
1989 | MB OPERATING CO INC | Brine | 0 | 365 |
1990 | MB OPERATING CO INC | Brine | 0 | 365 |
1991 | MB OPERATING CO INC | Brine | 0 | 365 |
1992 | MB OPERATING CO INC | Brine | 0 | 366 |
1993 | MB OPERATING CO INC | Brine | 0 | 365 |
1994 | MB OPERATING CO INC | Brine | 0 | 365 |
1995 | MB OPERATING CO INC | Brine | 0 | 365 |
1996 | MB OPERATING CO INC | Brine | 60 | 366 |
1997 | MB OPERATING CO INC | Brine | 0 | 365 |
1998 | MB OPERATING CO INC | Brine | 70 | 365 |
1999 | MB OPERATING CO INC | Brine | 140 | 273 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1354437066 | 2010-3-23 0:00: | PW | No Violations | |
-182703295 | 2012-5-10 0:00: | PB | No Violations | |
0182703295 | 2012-05-10 | Plug / Plug Back | No Violations | On location to witness plug job. Set Big Lime plug, set Berea/bottom of surface casing plug and surface plug. See plug report for details. |
0691018732 | 2013-01-10 | Production Wells | No Violations | I inspected the Millhone D & B 1 (34151231550000) well on January 10, 2013. My inspection was a follow up for an existing Notice of Violation (NOV) issued by inspector Dave Claus on March 25, 2010. This well was plugged May 10, 2012. All production equipment has been removed and final restoration is passed. |
1336572891 | 2012-05-09 | Plug / Plug Back | No Violations | On 5/9/2012, I inspected a plug job with lead DNR Inspector Chris Grimm. I witnessed the digging and lining of the pit, locating and marking of the flow line, cementing of the bottom plug, and ripping the 4.5 inch casing. Refer to DNR Inspection Chris Grimms plugging report. |
1337008192 | 2012-05-09 | Plug / Plug Back | No Violations | On location to witness plug job. Set bottom plug through Clinton, ripped production casing. See plug report for details. |
1339098466 | 2012-05-10 | Plug / Plug Back | No Violations | This well was plugged and abandoned on 5-10-2012. The idle well Notice of Violation has been RESOLVED. |
1354437066 | 2010-03-23 | Production Wells | Violations Noted | The Uniontown office received a complaint call from Don Millhone (330-327-2089) on 3-22-2010 regarding an idle well located on his property. I inspected the site on 3-23-2010. The well was drilled to the Clinton Sandstone in 1980. There has been zero reported production in the State Database since 1999. The well is idle and there is no I.D. sign posted, only the remnants of an old MB Operating I.D. sign. The well is a 4-1/2 diameter swab well that is shut in. The house gas line hook-up has been disconnected. The tank battery contains 1-210 barrel oil stock tank and 1-buried steel brine tank (possibly 1000 gallon capacity). I called Don Millhone on 3-25-2010. He told me that he swabbed the well several years ago and it produced for 28 days and watered out. PLUG, PRODUCE, or SELL the well. |
691018732 | 2013-1-10 0:00: | PW | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1354437066 | US-OH-110253 | 2010-03-25 | Failure to legibly identify well | |
1354437066 | US-OH-110254 | 2010-03-25 | Well shall be plugged |
For data sources see[9]