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| Well ID: 34-151-24733 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Stark | |
| Municipality: Lake Township | |
| Operator Name: PIN OAK ENERGY PARTNERS LLC | |
| Well Pad ID: | |
| Farm/Lease Name: CLOVIS | |
| License Status: Producing | |
| License Date: 2009-10-27 | |
| Spud Date: 1991-12-05 | |
| Spud Drilling Contractor: SHERMAN DRLG | |
| Final Drill Date: 1991-12-11 | |
| Well Total Depth: 4700.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.910000 | |
| Longitude: -81.390000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1990-12-31 | 169 SMAIL JAMES R GeoDate 12/31/90 |
| Oil and Gas | 1990-12-31 | Issued Date 12/31/90 Expired Date 12/31/91 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04700 Proposed Drill Depth 04700 |
| Original Spud | 1991-12-05 | |
| Completed | 1991-12-11 | |
| Reached Total Depth | 1991-12-11 | |
| Completion Report Received | 1991-12-31 | |
| CO | 1992-01-09 | 3442 CUTTER EXPLORATION INC GeoDate 12/31/90 |
| Change of Owner | 2009-09-16 | Operator changed from 3442, CUTTER EXPLORATION INC to 169, SMAIL JAMES R INC |
| APP | 2009-10-27 | Proposed Formations:CLINTON, Issued Date:10/27/2009, Expired Date:10/27/2010 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
| Construction Permit Expires | 2010-10-27 | |
| Change of Owner | 2018-11-29 | Operator changed from 169, JAMES R SMAIL INC to 9722, PIN OAK ENERGY PARTNERS LLC |
| Record Last Modified | 2018-11-29 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 4530 | 4626 | 38 |
| 4530 | 4626 | 38 | |
| 4530 | 4626 | 38 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| CO2 | 0 | 20 Tons | 0 | |||
| H2O | 0 | 3000 Bbl | 60000 | FRAC W/3000 BW,600 SX SAND AND 20 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1992 | CUTTER EXPLORATION INC | 7907.00 | 438.00 | 265 |
| 1993 | CUTTER EXPLORATION INC | 7588.00 | 301.00 | 365 |
| 1994 | CUTTER EXPLORATION INC | 5682.00 | 168.00 | 365 |
| 1995 | CUTTER EXPLORATION INC | 4397.00 | 167.00 | 365 |
| 1996 | CUTTER EXPLORATION INC | 3680.00 | 78.00 | 365 |
| 1997 | CUTTER EXPLORATION INC | 3244.00 | 72.00 | 365 |
| 1998 | CUTTER EXPLORATION INC | 2303.00 | 75.00 | 365 |
| 1999 | CUTTER EXPLORATION INC | 1587.00 | 0.00 | 365 |
| 2000 | CUTTER EXPLORATION INC | 0.00 | 0.00 | 0 |
| 2001 | CUTTER EXPLORATION INC | 1666.00 | 69.00 | 365 |
| 2002 | CUTTER EXPLORATION INC | 2501.00 | 72.00 | 365 |
| 2003 | CUTTER EXPLORATION INC | 2029.00 | 0.00 | 365 |
| 2004 | CUTTER EXPLORATION INC | 2221.00 | 77.00 | 365 |
| 2005 | CUTTER EXPLORATION INC | 1916.00 | 84.00 | 365 |
| 2006 | CUTTER EXPLORATION INC | 2293.00 | 0.00 | 365 |
| 2008 | CUTTER EXPLORATION INC | 698.00 | 0.00 | 365 |
| 2009 | CUTTER EXPLORATION INC | 1932.00 | 69.00 | 365 |
| 2010 | JAMES R SMAIL INC | 1712.00 | 59.00 | 330 |
| 2011 | JAMES R SMAIL INC | 1701.00 | 73.00 | 365 |
| 2012 | JAMES R SMAIL INC | 2039.00 | 62.00 | 366 |
| 2013 | JAMES R SMAIL INC | 2029.00 | 46.00 | 365 |
| 2014 | JAMES R SMAIL INC | 1686.00 | 78.00 | 365 |
| 2015 | JAMES R SMAIL INC | 1817.00 | 43.00 | 365 |
| 2016 | JAMES R SMAIL INC | 1766.00 | 45.00 | 365 |
| 2017 | JAMES R SMAIL INC | 1587.00 | 0.00 | 365 |
| 2018 | JAMES R SMAIL INC | 1517.00 | 71.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1992 | CUTTER EXPLORATION INC | Brine | 112 | 265 |
| 1993 | CUTTER EXPLORATION INC | Brine | 539 | 365 |
| 1994 | CUTTER EXPLORATION INC | Brine | 230 | 365 |
| 1995 | CUTTER EXPLORATION INC | Brine | 132 | 365 |
| 1996 | CUTTER EXPLORATION INC | Brine | 136 | 365 |
| 1997 | CUTTER EXPLORATION INC | Brine | 155 | 365 |
| 1998 | CUTTER EXPLORATION INC | Brine | 70 | 365 |
| 1999 | CUTTER EXPLORATION INC | Brine | 80 | 365 |
| 2000 | CUTTER EXPLORATION INC | Brine | 0 | 0 |
| 2001 | CUTTER EXPLORATION INC | Brine | 40 | 365 |
| 2002 | CUTTER EXPLORATION INC | Brine | 80 | 365 |
| 2003 | CUTTER EXPLORATION INC | Brine | 160 | 365 |
| 2004 | CUTTER EXPLORATION INC | Brine | 130 | 365 |
| 2005 | CUTTER EXPLORATION INC | Brine | 110 | 365 |
| 2006 | CUTTER EXPLORATION INC | Brine | 75 | 365 |
| 2008 | CUTTER EXPLORATION INC | Brine | 75 | 365 |
| 2009 | CUTTER EXPLORATION INC | Brine | 70 | 365 |
| 2010 | JAMES R SMAIL INC | Brine | 202 | 330 |
| 2011 | JAMES R SMAIL INC | Brine | 137 | 365 |
| 2012 | JAMES R SMAIL INC | Brine | 231 | 366 |
| 2013 | JAMES R SMAIL INC | Brine | 116 | 365 |
| 2014 | JAMES R SMAIL INC | Brine | 116 | 365 |
| 2015 | JAMES R SMAIL INC | Brine | 0 | 365 |
| 2016 | JAMES R SMAIL INC | Brine | 184 | 365 |
| 2017 | JAMES R SMAIL INC | Brine | 65 | 365 |
| 2018 | PIN OAK ENERGY PARTNERS LLC | Brine | 0 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| 0000003873 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 2/18/94 INSPECTOR BRETT FARNSWORTH DATE 02/1819/94 DATA FROM OLD VAX INFO | |
| 1255133867 | 2009-10-08 | Production Wells | No Violations | The Uniontown office received a complaint call on 10-8-09 from Ron Heinlein (330-904-6438) of 2594 Chadwell Circle NW, North Canton, OH regarding safety issues (no fencing, clamped tubing, broken gauges) at this site. I called Ron Heinlein and told him that I would inspect the site next week. |
| 1255528251 | 2009-10-13 | Production Wells | Violations Noted | The Uniontown office received a complaint call on 10-8-09 from Ron Heinlein (330-904-6438) of 2594 Chadwell Circle NW, North Canton, OH regarding safety issues (no fencing, clamped tubing, broken gauges) at this site. I called Ron Heinlein and told him that I would inspect the site next week. On 10-13-2009 I met with Ron Heinlein and inspected the site. The well is an 1-1/2 dia rabbit well with the remnants of an old pump jack pad. There is a line clamp on the 1-1/2 dia tubing located between the Demco valve and the wellhead. The gauges are rusted and broken. Repair the tubing leak, replace the gauges, post a current owner I.D. sign, and fence off the wellhead. I called Ted Cutright (330-697-7117) and discussed the status of the well. |
| 1258141750 | 2009-11-13 | Production Wells | No Violations | See Complaint # 09-006. The tubing leak has been repaired and new wellhead plumbing has been installed. New fencing has been installed around the wellhead. A plugging permit has been issued for the well. The Complaint and the N.O.V. have been RESOLVED. |
| 3873 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1255528251 | US-OH-106876 | 2009-10-14 | General Safety | |
| 1255528251 | US-OH-106877 | 2009-10-14 | Well insufficiently equipped to prevent escape of oil and gas | |
| 1255528251 | US-OH-106878 | 2009-10-14 | Failure to legibly identify well |
For data sources see[9]