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| Well ID: 34-151-25608 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Stark | |
| Municipality: Paris Township | |
| Operator Name: ENERVEST OPERATING LLC | |
| Well Pad ID: | |
| Farm/Lease Name: KRINGER LTD | |
| License Status: Plugged and Abandoned | |
| License Date: 2017-01-12 | |
| Spud Date: 2008-01-08 | |
| Spud Drilling Contractor: WHIPSTOCK OHIO DRILLING | |
| Final Drill Date: 2008-01-11 | |
| Well Total Depth: 5297.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.780000 | |
| Longitude: -81.170000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2007-12-14 | Proposed Formations:CLINTON, Issued Date:12/14/2007, Expired Date:12/13/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
| Completed | 2008-01-11 | UPDATE COORDS SURVEYOR-07/07/2017 ALE. |
| Reached Total Depth | 2008-01-11 | UPDATE COORDS SURVEYOR-07/07/2017 ALE. |
| Completion Report Received | 2008-01-24 | UPDATE COORDS SURVEYOR-07/07/2017 ALE. |
| Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
| APP | 2017-01-12 | Proposed Formations:CLINTON SAND, Issued Date:1/12/2017, Expired Date:1/12/2019 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2017-04-18 | UPDATE COORDS SURVEYOR-07/07/2017 ALE. |
| Record Last Modified | 2017-07-07 | UPDATE COORDS SURVEYOR-07/07/2017 ALE. |
| Construction Permit Expires | 2019-01-12 | UPDATE COORDS SURVEYOR-07/07/2017 ALE. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2008-03-31 | 5112 | 5194 | 31 |
| 5112 | 5194 | 31 | |
| 5112 | 5194 | 31 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 3759 Bbl | 0 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2008 | RANGE RESOURCES-APPALACHIA LLC | 3052.00 | 426.00 | 245 |
| 2009 | RANGE RESOURCES-APPALACHIA LLC | 1236.00 | 230.00 | 304 |
| 2010 | ENERVEST OPERATING LLC | 784.00 | 152.00 | 365 |
| 2011 | ENERVEST OPERATING LLC | 919.00 | 113.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 760.00 | 131.00 | 366 |
| 2013 | ENERVEST OPERATING LLC | 737.00 | 53.00 | 365 |
| 2014 | ENERVEST OPERATING LLC | 101.00 | 0.00 | 365 |
| 2015 | ENERVEST OPERATING LLC | 20.00 | 0.00 | 281 |
| 2016 | ENERVEST OPERATING LLC | 25.00 | 0.00 | 326 |
| 2017 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 108 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2008 | RANGE RESOURCES-APPALACHIA LLC | Brine | 2158 | 245 |
| 2009 | RANGE RESOURCES-APPALACHIA LLC | Brine | 140 | 304 |
| 2010 | ENERVEST OPERATING LLC | Brine | 388 | 365 |
| 2011 | ENERVEST OPERATING LLC | Brine | 357 | |
| 2012 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
| 2013 | ENERVEST OPERATING LLC | Brine | 959 | 365 |
| 2014 | ENERVEST OPERATING LLC | Brine | 1874 | 365 |
| 2015 | ENERVEST OPERATING LLC | Brine | 508 | 281 |
| 2016 | ENERVEST OPERATING LLC | Brine | 671 | 326 |
| 2017 | ENERVEST OPERATING LLC | Brine | 40 | 108 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1348624424 | 2015-4-28 0:00: | PW | No Violations | 6.00 |
| -671365997 | 2015-4-29 0:00: | PW | No Violations | 0.00 |
| 0597917359 | 2008-01-11 | Drill / Deepen / Reopen | No Violations | Drilling at 4700. Pits and liners are intact. |
| 0671365997 | 2015-04-29 | Production Wells | No Violations | I was on location to follow up to the final remediation of the brine spill for this well. The sump holes have been vacuumed out and the location has been flushed with a load of freshwater to flush any residual brine from the location. The water was vacuumed and taken to an injection well. A total of 30 tons of dirt have been excavated and taken to the Kimble Landfill for disposal. The track hoe was hooked up to the pumpjack and straightened over the wellbore to prevent any future stuffing box wearing out prematurely. A dike around the wellhead was constructed and the location seeded. The tank battery was cleaned up and the identification made to be more visible. At this time the brine spill has been remediated and the well made to no longer leak. There are no violations at this time. |
| 1084141493 | 2016-08-23 | Production Wells | No Violations | I conducted a status check inspection on this well. The well is equipped with a pumpjack with an electric motor and there is a domestic gas connection at the well. The RBDMS record shows the well has a production report submitted for 2015. The well is shut-in. The diked tank battery consists of one 210 barrel tank, one 50 barrel brine tank, and a vertical separator with a meter. The well is legibly identified. There are no compliance issues noted at this time. |
| 1212514537 | 2008-06-03 | Preliminary Restoration | No Violations | The well has been completed. The location is reclaimed. I did not pass the Preliminary Restoration at this time. |
| 1241200171 | 2009-05-01 | Preliminary Restoration | No Violations | The location is reclaimed. The Preliminary Restoration is PASSED. |
| 1348624424 | 2015-04-28 | Production Wells | No Violations | I was contacted by Troy Wells of Enervest at 14:20 indicating that a brine spill had occurred at this well. Joe Little Excavating has been called to the location to excavate and remediate the location. The pumpjack well was set on the well at an angle and the polishing rod was causing excessive wear on the stuffing box. The stuffing box failed and a maximum amount of brine that spilled was 5bbls during the production period. A 60x3 kill area is present near the tank battery from the spill. A 15x10 kill spot is present near the wellhead and the brine migrated down the fence line of the pasture causing a 90x3 kill spot. No roadways or waterways were impacted. The kill spots were excavated and disposed of at the Kimble Landfill. While excavating the soil around the tank battery it was discovered that a clay and plastic liner from the drilling of the well has trapped the brine in the gravel on location. Two sump holes were dug and the stone excavated. Six bags of dolomitic lime were spread on the spill area and flushed with a load of fresh water. The water was vacuumed up and brought to an injection well. The excavated soil will be left exposed overnight and the area flushed again in the morning to complete the remediation. |
| 1430747581 | 2015-05-04 | Production Wells | No Violations | I was on location to follow up to the spill that occurred on this well 4/28/2015. A new dike has been built around the pumpjack well and the contaminated soil has been removed and disposed at the Kimble Landfill. There is no evidence of the spill on location and there are no violations at this time. |
| 1499768928 | 2017-06-29 | Plug / Plug Back | No Violations | With Luke Smith (ODNR Oil & Gas -Survey Tech) - A partial inspection was done to log the well coordinates. The well is plug and the site is graded and stabile. |
| 1744834020 | 2008-06-26 | Preliminary Restoration | No Violations | The well is in production and the location is reclaimed. The vegetation is not fully established. I did not pass the Preliminary Restoration at this time. |
| 597917359 | 2008-1-11 0:00: | DD | No Violations |
For data sources see[9]