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34-155-22037

Well Details

Well ID: 34-155-22037
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Country: United States
State: Ohio
County: Trumbull
Municipality: Brookfield Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: MCCALLION-UNIT
License Status: Producing
License Date: 1982-04-20
Spud Date: 1982-05-05
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1982-05-12
Well Total Depth: 4954.00 ft
Configuration: Vertical
Latitude: 41.270000
Longitude: -80.600000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-04-20 Issued Date 4/21/82 Expired Date 10/18/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04954 Proposed Drill Depth 04954
Original Spud 1982-05-07
Completed 1982-05-12
Reached Total Depth 1982-05-12
CO 1982-06-23 54 TITAN ENERGY CORP GeoDate 4/20/82
Construction Permit Expires 1982-10-18
Completion Report Received 1984-09-18
Change of Owner 1998-01-26 Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4745 4801 21
4745 4801 21
4745 4801 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 62000 Gal 70000
N2 0 225 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TITAN ENERGY CORP 10895.00 127.00 0
1985 TITAN ENERGY CORP 7131.00 63.00 365
1986 TITAN ENERGY CORP 4804.00 73.00 365
1987 TITAN ENERGY CORP 4474.00 0.00 365
1988 TITAN ENERGY CORP 5224.00 68.00 365
1989 TITAN ENERGY CORP 4144.00 50.00 365
1990 TITAN ENERGY CORP 3680.00 57.00 365
1991 TITAN ENERGY CORP 1705.00 0.00 365
1992 TITAN ENERGY CORP 2896.00 70.00 365
1993 TITAN ENERGY CORP 3433.00 0.00 365
1994 TITAN ENERGY CORP 1758.00 0.00 365
1997 TITAN ENERGY CORP 2060.00 67.00 245
2000 BIG SKY ENERGY INC 2159.00 41.00 365
2001 BIG SKY ENERGY INC 2307.00 38.00 365
2002 BIG SKY ENERGY INC 2081.00 0.00 365
2003 BIG SKY ENERGY INC 728.00 23.00 365
2004 BIG SKY ENERGY INC 2432.00 0.00 365
2005 BIG SKY ENERGY INC 2492.00 0.00 365
2006 BIG SKY ENERGY INC 2106.00 0.00 365
2007 BIG SKY ENERGY INC 1603.00 44.00 365
2008 BIG SKY ENERGY INC 280.00 0.00 365
2010 BIG SKY ENERGY INC 1940.00 40.00 365
2011 BIG SKY ENERGY INC 1634.00 10.00 365
2012 BIG SKY ENERGY INC 1341.00 0.00 366
2013 BIG SKY ENERGY INC 1562.00 0.00 365
2014 BIG SKY ENERGY INC 1343.00 0.00 365
2016 BIG SKY ENERGY INC 539.00 0.00 98
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TITAN ENERGY CORP Brine 0 0
1985 TITAN ENERGY CORP Brine 0 365
1986 TITAN ENERGY CORP Brine 0 365
1987 TITAN ENERGY CORP Brine 0 365
1988 TITAN ENERGY CORP Brine 0 365
1989 TITAN ENERGY CORP Brine 0 365
1990 TITAN ENERGY CORP Brine 0 365
1991 TITAN ENERGY CORP Brine 0 365
1992 TITAN ENERGY CORP Brine 0 365
1993 TITAN ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 0 365
1997 TITAN ENERGY CORP Brine 44 245
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 365
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2008 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 365
2014 BIG SKY ENERGY INC Brine 55 365
2016 BIG SKY ENERGY INC Brine 0 98
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-11246676 2017-8-17 0:00: PW No Violations 0.30
-1233824530 2016-4-18 0:00: PW No Violations 0.50
-1389840781 2012-12-11 0:00 PW No Violations 0.50
-1673650616 2013-11-12 0:00 PW No Violations 0.50
-1798784683 2017-5-24 0:00: PW No Violations 1.00
-2046038363 2006-3-16 0:00: PL No Violations
-2105710245 2006-3-28 0:00: PL No Violations
-222928621 2017-12-12 0:00 PW No Violations 0.50
-529728429 2019-1-31 0:00: PW No Violations
-846525528 2017-8-28 0:00: PW No Violations 1.50
0000PL4057 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0011246676 2017-08-17 Production Wells No Violations
0215847331 2017-08-25 Production Wells No Violations



Discussions with Inspector Fleming and Mr. Moisio developed a plan to shut--

0222928621 2017-12-12 Production Wells No Violations
0529728429 2019-01-31 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice #1495639844 and complaint # 5609. The well was equipped with a plunger lift assembly and the annulus and flow line valves were open. The site was snow covered which was not allowing me to see if the well was still leaking gas from the 8.625 inch casing. Big Sky has not filled in the hole around the wellhead. The hole was full of water and snow covered. A Vortex Energy LLC identification sign is posted at the well. The tank battery consisted of one 100 BBL production tank, one 50 BBL tank and a mechanical separator. The flow line ball valve and sales line ball valve at the separator are open. The well is still registered under Big Skys name, but the chart on the sales line dated 12/7/17 had Vortex Energys name on it. A Vortex Energy stenciled identification sign was also still present at the separator. Access to the tank battery and well was stable.
0613329005 2017-08-31 Production Wells No Violations

-in. I spoke with Mr. Moisio. Mr. Moisio stated he has been stuck working on wells in Ashtabula County. Mr. Moisio stated he would have Mason Barr install the pressure gauge today (8/31/17). A follow-up inspection will be conducted by Tuesday, September 5, 2017. Photos were taken and are available upon request.

0846525528 2017-08-28 Production Wells No Violations

-in. I spoke with Mr. Moisio. Mr. Moisio stated the pressure gauge would be installed by tomorrow morning, 8/29/2017. Photo were taken and are available upon request.

1057069858 2017-09-07 Production Wells No Violations

-


1129083168 2016-09-15 Production Wells No Violations
1233824530 2016-04-18 Production Wells No Violations I conducted this inspection to follow---105 requiring Big Sky Energy Incorporated to suspend all oil and gas operations in the State of Ohio. My inspection found the wellhead equipped with a 1.5 plunger lift system. The hammer unions on the casing and tubing flow lines as well as the flow line tee have oil staining and need to be tightened. No oil has reached the ground surface. The gate valve and flow line valve at the wellhead are open and the casing valve is closed. The well is producing to a horizontal separator and the flow line and sales line valves are open. The 31 day production chart in the separator was changed on 2-29-2016 and is currently recording production and overprinting previous production data. The electronic controls are on and set to cycle the well in five (5) hours. The well produces to a diked tank battery containing one (1) 100 barrel production tank and one (1) 50 barrel brine tank. The 50 barrel tank is disconnected from service. The ID on the tank remains legible, but is very faded. Big Sky Energy Incorporated has failed to comply with the above orders to suspend oil and gas operations in the State of Ohio and shall immediately cease the production operations of this well as required by the temporary restraining order issued by the Trumbull County Court of Common Pleas, dated 4/11/2016.
1383766850 2013-11-06 Production Wells No Violations I responded to complaint #4530 listed as a brine leak. My inspection found the 4 load line plug on the production tank slowly dripping brine. I called Bob Barr, Jr. at 740-624-0434 and informed him of the complaint. Bob stated a well tender would respond to tighten the plug.
1389840781 2012-12-11 Production Wells No Violations I completed a production well inspection status check. My inspection found the well equipped with a plunger lift unit and located southwest of the tank battery. The tank battery contained one, 100 barrel oil storage tank with a stenciled identification sign, one, 50 barrel brine storage tank, and a weathered dike. The heat treated separator was located outside the tank battery that appeared in good working condition. The lease road was in good working condition. I noticed no visible spills or leaks.
1495639844 2017-05-22 Production Wells Violations Noted

-up line. There is a stenciled identification sign on the 100 bbl. storage tank with Big Sky listed at the well owner. The separator is outside of the dike. There is a stenciled identification sign on the separator. The well owner on the stenciled identification sign is Vortex Energy LLC. There is a deduct meter and 31 day chart dated 4/2/17 inside of the separator. The access road is in good repair. Photos were taken and are available upon request. I called and left a message with Vortex Energy for a return call concerning the well. Next, I spoke with Charlie Momosis, contractor well tender for Vortex Energy. Mr. Momosis stated he knew about the gas leak at the well. Mr. Momosis stated he is currently working on another well and plans to move the rig onto this well as soon as possible. Mr. Momosis stated he would stop by the well to blow down the well through the separator. I told Mr. Momosis follow-up inspections will continue until the gas leak is repaired.

A compliance notice has been issued: Big Sky needs to repair the gas leak at the well by June 2, 2017.

The equipment on site:



1522869119 2018-03-20 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice #1495639844. The well was equipped with a plunger lift assembly and the annulus and flow line valves were open. The well was still leaking gas from the 8.625 inch casing. Big Sky has not filled in the hole around the wellhead. The hole is full of water and is bubbling from the gas leak. A Vortex Energy LLC identification sign is posted at the well. The tank battery consisted of one 100 BBL production tank, one 50 BBL tank and a mechanical separator. The flow line ball valve and sales line ball valve at the separator are open. There is a chart box and 31 day chart dated 12/7/17 with Vortex Energy and McCallion written on the chart. A Vortex Energy stenciled identification sign is on the separator. Lease access was stable.
1582647051 2020-2-25 0:00: PW No Violations
1588779002 2020-5-6 0:00:0 PW No Violations
1669381280 2017-10-17 Production Wells No Violations
1673650616 2013-11-12 Production Wells No Violations My inspection of complaint #4530 found the 4 load line plug tightened and the brine leak at the production tank stopped. I called the landowner and left a message that the leak was repaired.
1798784683 2017-05-24 Production Wells No Violations I was on location to assess complaint 5609 and compliance notice #1495639844. I found the water in the dug hole around the well still leaking gas on the day of my inspection. The complaint log has been updated.
1955711644 2017-11-29 Production Wells No Violations
2046038363 2006-03-16 Preliminary Restoration Violations Noted Case# 06-001 , Dave McCallion . Inspection showed sales line needs final grading .
2060624900 2017-08-25 Production Wells No Violations I met with Inspector Rick Skidmore and Charlie Moisio at the above location to verify the pressures on the 8-5/8 annulas and the 4.5 casing The pressure were checked 4.5 casing had 150 psi / 8-5/8 was 144 psi / 1.5 tubing was 148 psi. The 8-5/8 casing was put in line to sell down to line pressure 50 / 60 psi. Charlie will install a pressure gage on t 8-5/8 casing. Inspector Rick Skidmore will monitor the 4.5 casing pressure.
2105710245 2006-03-28 Preliminary Restoration No Violations Case# 06-001 , Dave McCallion . Sales line final graded . Resolved .
215847331 2017-8-25 0:00: PW No Violations 0.80
414513705 2020-8-31 0:00: PW No Violations
613329005 2017-8-31 0:00: PW No Violations 0.40
682740782 2019-6-6 0:00:0 PW No Violations
PL4057 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1495639844 US-OH-113996 2017-05-26 Well insufficiently equipped to prevent escape of oil and gas
2046038363 US-OH-120829 2006-05-08 Failure to restore land surface within 9 mos. (CHANGE) (REPLACE)

For data sources see[9]

References