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34-155-22920

Well Details

Well ID: 34-155-22920
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Country: United States
State: Ohio
County: Trumbull
Municipality: Weathersfield Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: OHIO EDISON CO
License Status: Final Restoration
License Date: 2013-06-27
Spud Date: 1986-01-17
Spud Drilling Contractor:
Final Drill Date: 1986-01-24
Well Total Depth: 4950.00 ft
Configuration: Vertical
Latitude: 41.160000
Longitude: -80.740000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1986-01-03 1702 LOMA ENTERPRISES INC GeoDate 1/3/86
Oil and Gas 1986-01-03 Issued Date 1/3/86 Expired Date 1/3/87 Acres 0060229 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04950 Proposed Drill Depth 04950
Original Spud 1986-01-17
Completed 1986-01-24
Reached Total Depth 1986-01-24
Completion Report Received 1986-05-23
Change of Owner 1999-10-14 Operator changed from 1702, LOMA ENTERPRISES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2010-05-06 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2013-06-27 Proposed Formations:CLINTON, Issued Date:6/27/2013, Expired Date:6/27/2015 12:00:00 PM, Drilling unit acres:60, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-07-23
Construction Permit Expires 2015-06-27
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4712 4818 21
4712 4818 21
4712 4818 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 80500 Gal 0
N2 0 220 Mscf 0
H2O 0 500 Gal 60000 15% HCL

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 LOMA ENTERPRISES INC 22501.00 394.00 216
1987 LOMA ENTERPRISES INC 28217.00 332.00 365
1988 LOMA ENTERPRISES INC 19857.00 164.00 365
1989 LOMA ENTERPRISES INC 16487.00 147.00 365
1990 LOMA ENTERPRISES INC 14454.00 90.00 365
1991 LOMA ENTERPRISES INC 12694.00 60.00 365
1992 LOMA ENTERPRISES INC 10130.00 0.00 365
1993 LOMA ENTERPRISES INC 9279.00 45.00 365
1994 LOMA ENTERPRISES INC 6376.00 65.00 365
1995 LOMA ENTERPRISES INC 7861.00 56.00 365
1996 LOMA ENTERPRISES INC 7109.00 33.00 365
1997 LOMA ENTERPRISES INC 7751.00 59.00 365
1998 LOMA ENTERPRISES INC 6399.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 1507.00 47.00 91
2000 EXCO - NORTH COAST ENERGY INC 2596.00 55.00 365
2001 EXCO - NORTH COAST ENERGY INC 2425.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 4388.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 3242.00 0.00 365
2004 EXCO - NORTH COAST ENERGY INC 5335.00 0.00 365
2005 EXCO - NORTH COAST ENERGY INC 4227.00 67.00 365
2006 EXCO - NORTH COAST ENERGY INC 4886.00 0.00 365
2007 EXCO - NORTH COAST ENERGY INC 4073.00 56.00 365
2008 EXCO - NORTH COAST ENERGY INC 3105.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 3698.00 0.00 365
2010 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 2612.00 0.00 0
2012 ENERVEST OPERATING LLC 2451.00 0.00 366
2013 ENERVEST OPERATING LLC 1369.00 0.00 204

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 LOMA ENTERPRISES INC Brine 2970 216
1987 LOMA ENTERPRISES INC Brine 36 365
1988 LOMA ENTERPRISES INC Brine 13 365
1989 LOMA ENTERPRISES INC Brine 16 365
1990 LOMA ENTERPRISES INC Brine 14 365
1991 LOMA ENTERPRISES INC Brine 6 365
1992 LOMA ENTERPRISES INC Brine 2 365
1993 LOMA ENTERPRISES INC Brine 7 365
1994 LOMA ENTERPRISES INC Brine 2 365
1995 LOMA ENTERPRISES INC Brine 2 365
1996 LOMA ENTERPRISES INC Brine 2 365
1997 LOMA ENTERPRISES INC Brine 11 365
1998 LOMA ENTERPRISES INC Brine 0 365
1999 EXCO - NORTH COAST ENERGY INC Brine 91
2000 EXCO - NORTH COAST ENERGY INC Brine 0 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 20 365
2004 EXCO - NORTH COAST ENERGY INC Brine 0 365
2005 EXCO - NORTH COAST ENERGY INC Brine 6 365
2006 EXCO - NORTH COAST ENERGY INC Brine 0 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 365
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 365
2010 EXCO - NORTH COAST ENERGY INC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 366
2013 ENERVEST OPERATING LLC Brine 0 204

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL3473 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1374690222 2013-07-23 Plug / Plug Back No Violations I witnessed Nicks Well Service plugged a well for Enervest Operating. Nick bullheaded the bottom plug with 30 sacks of Class A cement with 50 lbs. of Hulls. The operator displaced with 72 bbls of brine, then shut the well in at 2,000 psi for 1 hour. Plug #1 was set at 4,513 to 4,868. The 4.5 casing was ripped at 3,459 and 10 joints were pulled. Nicks Well Plugging broke circulation with 20 bbls of fresh water and pumped 86 sacks of Class A cement. The operator displaced with 44 bbls of fresh water. Plug #2 was set at 2,776 to 3,076 to cover the Big Lime Formation. Next, Nick pulled 62 joints. The operator established circulation with 12 bbls of fresh water and pumped 60 sacks of Class A cement. The cement was displaced with 5 barrels of fresh water. Plug #3 was set at 320 to 520 to cover the bottom of the surface casing. Next, Nick pulled 7 joints. Circulation was established and 62 sacks of Class A cement was pumped. Plug #4 was set from 200 to surface. I witnessed a good show of cement returned to surface. A total of 84 joints of 4.5 casing was removed from the well.
1382618714 2013-10-24 Final Restoration No Violations My inspection found the well site graded and vegetation established. The pit was filled and debris removed. All of the production equipment was removed. I spoke to Enervests Land Department in Hartville concerning the lease road; they had not received the waiver at this time. Inspection not passed.
PL3473 PL No Violations

For data sources see[9]

References