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34-167-26658

Well Details

Well ID: 34-167-26658
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Country: United States
State: Ohio
County: Washington
Municipality: Lawrence Township
Operator Name: CIRCLE PETROLEUM INC
Well Pad ID:
Farm/Lease Name: PATTERSON CLARA
License Status: Orphan Well - Ready
License Date: 1981-09-11
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 39.490000
Longitude: -81.310000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-09-11 247 CIRCLE PETROLEUM INC GeoDate 9/11/81
Unknown 1981-09-11 Issued Date 9/11/81 Expired Date 9/11/82 Acres 0000000 Tool Type RTAF Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Construction Permit Expires 1982-09-11 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/8/03. PERMIT EXPIRED. STATUS CHANGED 4/14/16 TO IA WELL IS IDLE, REFER TO ORPHAN-ALE Orphan Well Case #2017 03 025
Changed to Orphan Well Ready 2017-03-01 Changed Well To Orphan Ready
Record Last Modified 2019-03-25 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/8/03. PERMIT EXPIRED. STATUS CHANGED 4/14/16 TO IA WELL IS IDLE, REFER TO ORPHAN-ALE Orphan Well Case #2017 03 025

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1055711977 2008-6-24 0:00: OR No Violations
-1775601734 2009-1-9 0:00:0 OR No Violations
0000PL2018 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1055711977 2008-06-24 Orphan No Violations Talked to Rob Armstrong - he says Phil Billik - Appalachian Eastern? Is accquiring this well - knows landowner and landowner offered it to him. Paperwork at the lawyers now and should be done shortly. They logged last summer and say it is an Ohio Shale well.
1055862637 2003-06-16 Production Wells No Violations Inspection this day reveals well not producing - not hooked up to line and hasnt produced in years? 4 production casing has 2 swedge on top and valve is shut - not leaking gas or any immediate threat, but probably is orphan well.
1064427072 2003-09-25 Production Wells No Violations Inspection this day found well with 4 1/2 casing not in production, as it was in June, 2003. Valve on top - but has not been produced in long time. 3 pictures taken
1115178657 2016-04-04 Orphan No Violations Performed an inspection of this well in response to a request from DOGRM Permitting Section. Upon inspection, it was observed that the well is idle and incapable of production. The well consists of 8.625 surface casing and 4.5 production casing with a 4-2 swedge and 2 ball valve in the closed position. The well is not currently a hazard and is not leaking oil or gas. The well is ~200 from Mill Fork Rd. and ~50 from a recently built cottage. The landowner has placed an orange construction cone over the well to make it more visible. Previous inspection reports indicate the well is under consideration to go into the Orphan Well Program. Photos were taken.
1127956009 2004-09-02 Orphan No Violations Inspection this day found well still not in production. Finally found someone at home and talked to them about well - they very much want it for house gas - gave them the papers to complete to become registered with State. Their name is Gary Boron, out of Newport, OH.
1354553960 2012-11-30 Orphan No Violations My inspection this day is to begin process for admission into Orphan well program. The well is located approximately 350 off the township road and about 50 from a new cabin that was built since my last visit. The ground is very flat and well consists of 4 casing with a 4 x 2 swedge and valve on top - valves closed and no leaks. This day it had a tall orange road construction cone over it to guard against anyone running into it. SEM is 108 and pictures were taken. I talked with landowner and he verbally gave us permission to plug it - will mail the ROE to get his signature. There is no record of how deep the well was drilled or how much surface casing and production casing is in the hole.
1379015784 2013-09-12 Orphan No Violations I spent time working on Plugging Specs. and Bid
1775601734 2009-01-09 Orphan No Violations Inspection this day found well still not producing. Rob Armstrong said he and Phil Billick had an agreement with landowner to produce well - title work showed landowner did not own well so no longer interested.
PL2018 PL No Violations

For data sources see[3]

References