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Well ID: 34-167-27728 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Ludlow Township | |
Operator Name: HEINRICH ENTERPRISES INC DBA W | |
Well Pad ID: | |
Farm/Lease Name: CLINE DAVID T | |
License Status: Producing | |
License Date: 1984-04-06 | |
Spud Date: 1984-04-20 | |
Spud Drilling Contractor: PACE CO | |
Final Drill Date: 1984-05-17 | |
Well Total Depth: 1530.00 ft | |
Configuration: Vertical | |
Latitude: 39.530000 | |
Longitude: -81.240000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-04-06 | Issued Date 4/6/84 Expired Date 10/3/84 Acres 0049800 Tool Type CT Proposed Formation SQUAW Proposed Depth 01530 Proposed Drill Depth 01530 |
Original Spud | 1984-04-20 | |
Completed | 1984-05-17 | |
Reached Total Depth | 1984-05-17 | |
CO | 1984-07-27 | 1130 H & C OIL CO GeoDate 4/6/84 |
Completion Report Received | 1984-08-27 | |
Construction Permit Expires | 1984-10-03 | |
Change of Owner | 2011-04-05 | Operator changed from 1130, H & C OIL CO to 3412, U S OIL & GAS INC |
Change of Owner | 2011-04-05 | Operator changed from 3412, U S OIL & GAS INC to 2007, HEINRICH ENT INC/WASHINGTON OP. WELL TRANSFERRED FROM H & C OIL TO VUKSIC (US OIL) THEN TO HEINRICH PER OWNERSHIP AFFIDAVIT. SEE OWNER FILE FOR MORE INFO. |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 1295 | 1450 | 0 |
1295 | 1450 | 0 | |
1295 | 1450 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 80 Qts | 0 | SHOT: 8O QT NITRO IN BIG INJUN |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | H & C OIL CO | 101.00 | 39.00 | 0 |
1986 | H & C OIL CO | 411.00 | 83.00 | 365 |
1987 | PACE CO/CHAS E HALL | 512.00 | 61.00 | 365 |
1988 | H & C OIL CO | 249.00 | 61.00 | 365 |
1989 | H & C OIL CO | 147.00 | 65.00 | 365 |
1990 | H & C OIL CO | 154.00 | 65.00 | 365 |
2010 | HEINRICH ENTERPRISES INC DBA W | 17.00 | 0.00 | 365 |
2011 | HEINRICH ENTERPRISES INC DBA W | 39.00 | 35.00 | 0 |
2012 | HEINRICH ENTERPRISES INC DBA W | 71.00 | 0.00 | 366 |
2013 | HEINRICH ENTERPRISES INC DBA W | 18.00 | 0.00 | 365 |
2014 | HEINRICH ENTERPRISES INC DBA W | 10.00 | 0.00 | 365 |
2015 | HEINRICH ENTERPRISES INC DBA W | 34.00 | 0.00 | 365 |
2016 | HEINRICH ENTERPRISES INC DBA W | 23.00 | 0.00 | 365 |
2017 | HEINRICH ENTERPRISES INC DBA W | 15.00 | 0.00 | 365 |
2018 | HEINRICH ENTERPRISES INC DBA W | 3.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | H & C OIL CO | Brine | 0 | 0 |
1986 | H & C OIL CO | Brine | 0 | 365 |
1987 | PACE CO/CHAS E HALL | Brine | 0 | 365 |
1988 | H & C OIL CO | Brine | 0 | 365 |
1989 | H & C OIL CO | Brine | 0 | 365 |
1990 | H & C OIL CO | Brine | 0 | 365 |
2010 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
2011 | HEINRICH ENTERPRISES INC DBA W | Brine | 23 | |
2012 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 366 |
2013 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
2014 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
2015 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
2016 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
2017 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
2018 | HEINRICH ENTERPRISES INC DBA W | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1110423377 | 2011-3-18 0:00: | PW | No Violations | 1.00 |
-1438208443 | 2011-11-17 0:00 | PW | No Violations | 1.00 |
0982706038 | 2011-07-27 | Production Wells | Violations Noted | Inspection this day found well equipped with pumping unit. All valves open on well but annual production indicates well produced only 17 MCF of gas for 2010. Well was serviced in 2010. No identification (ID) signs were posted. Contacted owner/operator about the need to produce, plug or place this well into Temporary Inactive status. Also need to post proper ID signs. 11/17/11 - issues resolved: Well now has proper ID and is capable of producing. |
1110423377 | 2011-03-18 | Production Wells | No Violations | Inspection this day found Stampedes service rig on location - much parafin in hole and they are trying to clean it out with parafin knife. I see this well still has not been put on Heinrichs bond but he is producing it - asked him to get that done several years ago. |
1137597519 | 2006-01-18 | Production Wells | Violations Noted | Inspectin this day found well producing with jack, was pumping on this day, no IDs at well, Heinrichs ID on tank with no information on it, so will send NOV to him. Fuild was being pumped into tank, then traveling out 2 line to a knock-out and onto the ground. Went into a ditch about 1-2 deep - had been cut by years of draining, and then flowed 100? Where it went underground, out into another drainage ditch and eventually ended up in Little Muskingham. Called Jack this morning to see if they owned, said yes - asked to stop dumping, they said Exempt Miss. And landowner approved of their methods. That water froze when cold. Tests showed 650 ppm salt in the water in the ditch and also had slight oil film on water this day. |
1438208443 | 2011-11-17 | Production Wells | No Violations | Inspection found this well equipped with a pumping unit and now in production. Proper identification is posted. Notice of Violation is RESOLVED. |
1494598168 | 2006-04-26 | Production Wells | No Violations | Inspection this day found new plastic water tank has been set, no longer going thru knockout with salt in it. Drainage ditch has been filled in, seeded, and now has good dike around tanks. Good IDs at well. NOV resolved |
982706038 | 2011-7-27 0:00: | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0982706038 | US-OH-131287 | 2011-07-27 | Failure to legibly identify well | |
0982706038 | US-OH-131288 | 2011-07-27 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1137597519 | US-OH-103478 | 2006-01-18 | Well operation causing pollution and contamination | |
1137597519 | US-OH-103479 | 2006-01-18 | Unlawful method of storage or disposal of brine or other wastes |
For data sources see[9]