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Well ID: 34-169-20705 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Franklin Township | |
Operator Name: BUCKEYE OIL PRODUCING CO | |
Well Pad ID: | |
Farm/Lease Name: TAYLOR C H | |
License Status: Plugged and Abandoned | |
License Date: 2013-02-15 | |
Spud Date: 1958-01-29 | |
Spud Drilling Contractor: | |
Final Drill Date: 1958-03-16 | |
Well Total Depth: 3632.00 ft | |
Configuration: Vertical | |
Latitude: 40.680000 | |
Longitude: -81.920000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1958-01-29 | GL=1144.1 |
Completed | 1958-03-16 | GL=1144.1 |
Reached Total Depth | 1958-03-16 | GL=1144.1 |
Completion Report Received | 1958-06-27 | GL=1144.1 |
APP | 2013-02-15 | Proposed Formations:CLINTON, Issued Date:2/15/2013, Expired Date:2/15/2015 12:00:00 PM, Drilling unit acres:160, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-08-15 | GL=1144.1 |
Construction Permit Expires | 2015-02-15 | GL=1144.1 |
Record Last Modified | 2017-02-15 | GL=1144.1 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 135 Bbl | 8500 | 95 BRL KERO |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1041168185 | 2014-7-31 0:00: | PB | No Violations | 1.00 |
1041168185 | 2014-07-31 | Plug / Plug Back | No Violations | On location to set bottom plug when it was discovered there is 3 tubing in the hole. No records of this any place. Suspect there is a packer in well. Matheny has no equipment with him to pull 3. Shutting down and resuming in morning. |
1249734640 | 2014-08-13 | Plug / Plug Back | No Violations | On location to set bottom plug and rip casing. See plug report for complete details. |
1397158027 | 2014-10-20 | Final Restoration | No Violations | Well head area has good amount of vegetation established. Cattle are grazing in the area. FINAL RESTORATION IS APPROVED. |
1407158884 | 2014-08-04 | Production Wells | No Violations | Met with producer on location to discuss plugging procedure. Decision has been made to place well back into production. String of 2 7/8 EUE tubing being ran. |
1408119071 | 2014-08-15 | Plug / Plug Back | No Violations | This well plugged and abandoned this date. See plug report for details. |
For data sources see[8]